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Difference between revisions of "34-089-21515"

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| County: [[Licking_County,_Ohio|Licking]]
 
| County: [[Licking_County,_Ohio|Licking]]
 
|-
 
|-
| Municipality: [[Hopewell Township,_Licking_County,_Ohio|Hopewell Township]]
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| Municipality: [[Hopewell_Township,_Licking_County,_Ohio|Hopewell Township]]
 
|-
 
|-
 
| Operator Name: [[PETRO QUEST INC]]
 
| Operator Name: [[PETRO QUEST INC]]

Revision as of 11:47, 29 August 2019

Well Details

Well ID: 34-089-21515
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Country: United States
State: Ohio
County: Licking
Municipality: Hopewell Township
Operator Name: PETRO QUEST INC
Well Pad ID:
Farm/Lease Name: ROBERTS CARL
License Status: Producing
License Date: 1957-03-22
Spud Date: 1957-03-25
Spud Drilling Contractor:
Final Drill Date: 1957-05-20
Well Total Depth: 3163 ft
Configuration: Vertical
Latitude: 39.970202040
Longitude: -82.26053241

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1957-03-25
Completed 1957-05-20
Reached Total Depth 1957-05-20
CO 1987-06-10 2556 WILLS GERALD D
Change of Owner 1999-07-26 Operator changed from 2556, WILLS GERALD D to 5432, ENCZI FRANK & LISA
Change of Owner 2017-11-16 Operator changed from 5432, ENCZI FRANK to 2165, PETRO QUEST INC
Record Last Modified 2017-11-16

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
OIL 0 620 Bbl 20000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 CGAS EXPLORATION 305 260 0
1985 CGAS EXPLORATION 239 230 0
1986 CGAS EXPLORATION 802 99 365
2008 ENCZI FRANK 0 38 365
2009 ENCZI FRANK 0 33 365
2010 ENCZI FRANK 0 18 365
2011 ENCZI FRANK 0 14 365
2012 ENCZI FRANK 0 0 366
2013 ENCZI FRANK 0 25 365
2014 ENCZI FRANK 0 0 365
2015 ENCZI FRANK 0 0 365
2016 ENCZI FRANK 0 0 365
2017 ENCZI FRANK 0 0 365
2018 PETRO QUEST INC 0 0 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 CGAS EXPLORATION Brine 0 0
1985 CGAS EXPLORATION Brine 12 0
1986 CGAS EXPLORATION Brine 35 365
2008 ENCZI FRANK Brine 1 365
2009 ENCZI FRANK Brine 15 365
2010 ENCZI FRANK Brine 51 365
2011 ENCZI FRANK Brine 18 365
2012 ENCZI FRANK Brine 0 366
2013 ENCZI FRANK Brine 0 365
2014 ENCZI FRANK Brine 1 365
2015 ENCZI FRANK Brine 0 365
2016 ENCZI FRANK Brine 0 365
2017 PETRO QUEST INC Brine 0 0
2018 PETRO QUEST INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0498747729 2018-06-04 Production Wells No Violations My inspection revealed that the pumping tee has been repaired. The violation has been resolved. Time of inspection: 9:25 AM. Weather: 65 degrees F, Cloudy
1525265018 2018-05-02 Production Wells No Violations My inspection revealed that the pumping tee has not been replaced. I contacted well owner Larry Baringer and advised him that the pumping tee needs replaced to bring well into compliance. Mr. Baringer said he will look at it tomorrow and should be able to fix it by next week. Time of inspection: 8:00 AM. Weather: 67 degrees F, Sunny
1978202221 2017-12-15 Production Wells Violations Noted My inspection revealed that the well was equipped with a pumping unit and motor. The pumping tee was broke in half and would not prevent the escape of fluids. It was not leaking during inspection. Identification was not observed at the well. The tank battery consists of (1) 100 barrel tank and a plastic brine tank. Identification was not observed at the tank battery. Petro Quest Inc. took ownership of this well on 11/16/2017 and will have 30 more days to post identification. A phone call was placed to Petro Quest Inc. (Larry Baringer) regarding the pumping tee. Mr. Baringer was advised that the pumping tee shall be fixed in order to prevent the escape of fluids. Mr. Baringer agreed to have it fixed. Time of inspection: 9:05 AM. Weather: 19*F, Partly cloudy

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1978202221 US-OH-120002 2018-06-11 9-9-05(A)1 Well insufficiently equipped to prevent escape of oil and gas

For data sources see[8]

References