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Well ID: 34-089-21515 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Hopewell Township | |
Operator Name: PETRO QUEST INC | |
Well Pad ID: | |
Farm/Lease Name: ROBERTS CARL | |
License Status: Producing | |
License Date: 1957-03-22 | |
Spud Date: 1957-03-25 | |
Spud Drilling Contractor: | |
Final Drill Date: 1957-05-20 | |
Well Total Depth: 3163.00 ft | |
Configuration: Vertical | |
Latitude: 39.970000 | |
Longitude: -82.260000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1957-03-25 | |
Completed | 1957-05-20 | |
Reached Total Depth | 1957-05-20 | |
CO | 1987-06-10 | 2556 WILLS GERALD D |
Change of Owner | 1999-07-26 | Operator changed from 2556, WILLS GERALD D to 5432, ENCZI FRANK & LISA |
Change of Owner | 2017-11-16 | Operator changed from 5432, ENCZI FRANK to 2165, PETRO QUEST INC |
Record Last Modified | 2017-11-16 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
OIL | 0 | 620 Bbl | 20000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CGAS EXPLORATION | 305.00 | 260.00 | 0 |
1985 | CGAS EXPLORATION | 239.00 | 230.00 | 0 |
1986 | CGAS EXPLORATION | 802.00 | 99.00 | 365 |
2008 | ENCZI FRANK | 0.00 | 38.00 | 365 |
2009 | ENCZI FRANK | 0.00 | 33.00 | 365 |
2010 | ENCZI FRANK | 0.00 | 18.00 | 365 |
2011 | ENCZI FRANK | 0.00 | 14.00 | 365 |
2012 | ENCZI FRANK | 0.00 | 0.00 | 366 |
2013 | ENCZI FRANK | 0.00 | 25.00 | 365 |
2014 | ENCZI FRANK | 0.00 | 0.00 | 365 |
2015 | ENCZI FRANK | 0.00 | 0.00 | 365 |
2016 | ENCZI FRANK | 0.00 | 0.00 | 365 |
2017 | ENCZI FRANK | 0.00 | 0.00 | 365 |
2018 | PETRO QUEST INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CGAS EXPLORATION | Brine | 0 | 0 |
1985 | CGAS EXPLORATION | Brine | 12 | 0 |
1986 | CGAS EXPLORATION | Brine | 35 | 365 |
2008 | ENCZI FRANK | Brine | 1 | 365 |
2009 | ENCZI FRANK | Brine | 15 | 365 |
2010 | ENCZI FRANK | Brine | 51 | 365 |
2011 | ENCZI FRANK | Brine | 18 | 365 |
2012 | ENCZI FRANK | Brine | 0 | 366 |
2013 | ENCZI FRANK | Brine | 0 | 365 |
2014 | ENCZI FRANK | Brine | 1 | 365 |
2015 | ENCZI FRANK | Brine | 0 | 365 |
2016 | ENCZI FRANK | Brine | 0 | 365 |
2017 | PETRO QUEST INC | Brine | 0 | 0 |
2018 | PETRO QUEST INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1978202221 | 2017-12-15 0:00 | PW | No Violations | 0.50 |
-498747729 | 2018-6-4 0:00:0 | PW | No Violations | 0.50 |
0498747729 | 2018-06-04 | Production Wells | No Violations | My inspection revealed that the pumping tee has been repaired. The violation has been resolved. Time of inspection: 9:25 AM. Weather: 65 degrees F, Cloudy |
1525265018 | 2018-05-02 | Production Wells | No Violations | My inspection revealed that the pumping tee has not been replaced. I contacted well owner Larry Baringer and advised him that the pumping tee needs replaced to bring well into compliance. Mr. Baringer said he will look at it tomorrow and should be able to fix it by next week. Time of inspection: 8:00 AM. Weather: 67 degrees F, Sunny |
1978202221 | 2017-12-15 | Production Wells | Violations Noted | My inspection revealed that the well was equipped with a pumping unit and motor. The pumping tee was broke in half and would not prevent the escape of fluids. It was not leaking during inspection. Identification was not observed at the well. The tank battery consists of (1) 100 barrel tank and a plastic brine tank. Identification was not observed at the tank battery. Petro Quest Inc. took ownership of this well on 11/16/2017 and will have 30 more days to post identification. A phone call was placed to Petro Quest Inc. (Larry Baringer) regarding the pumping tee. Mr. Baringer was advised that the pumping tee shall be fixed in order to prevent the escape of fluids. Mr. Baringer agreed to have it fixed. Time of inspection: 9:05 AM. Weather: 19*F, Partly cloudy |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1978202221 | US-OH-120002 | 2018-06-11 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[8]