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Difference between revisions of "34-167-29719"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-167-29719
 
| Well ID: 34-167-29719
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.4072859071, -81.2230261079 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.40728591, -81.22302611 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Washington County, Ohio|Washington]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[OOGC DISPOSAL CO]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2013-02-13
 
| Spud Date: 2013-02-13
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Active Injection
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 39.4072859071
+
| Latitude: 39.40728591
 
|-
 
|-
| Longitude: -81.2230261079
+
| Longitude: -81.22302611
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 64: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -1550706580
 
| 2014-06-24
 
|
 
| Inspection revealed that service rig was still on site preparing to run tubing back into well and wash to bottom and once they have bottom of hole cleaned up they plan on running scraper in well and then place liner string in place.
 
|
 
|
 
|
 
|-
 
|-
 
| -1638383744
 
| 2013-12-02
 
|
 
| Inspection revealed that injection pump was in operation during my inspection and it was noted that temporary storage site has been decommissioned.
 
|
 
|
 
|
 
|-
 
|-
 
| -1727551462
 
| 2013-02-15
 
|
 
| On site for pre spud meeting with drilling contractor personnel and company reps to discuss drilling procedure and safety issues and answer questions regarding state regulations pertaining to drilling SWIW in Ohio.
 
|
 
|
 
|
 
|-
 
|-
 
| -1836284607
 
| 2013-12-13
 
|
 
| Inspection revealed that well is not in operation at this time.
 
|
 
|
 
|
 
|-
 
|-
 
| -1882999581
 
| 2014-06-17
 
|
 
| Inspection revealed that service rig on site mixing drill mud to kill said well and once killed they will release packer and pull from well and then they plan on running liner string into open hole section of well bore.
 
|
 
|
 
|
 
|-
 
|-
 
| -196296034
 
| 2014-05-05
 
|
 
| Inspection revealed that well is still down waiting on plan to correct equalization issues.
 
|
 
|
 
|
 
|-
 
|-
 
| -2095607429
 
| 2014-07-22
 
|
 
| Inspection revealed that site has been restored and well is back into active disposal mode.
 
|
 
|
 
|
 
|-
 
|-
 
| -2113170097
 
| 2013-12-30
 
|
 
| Inspection revealed that well is not in use at this time due to high injection pressures, owner is considering applying for deepening permit at this time.
 
|
 
|
 
|
 
|-
 
|-
 
| -413652614
 
| 2014-01-06
 
|
 
| Inspection revealed that well is down to high injection pressure issues in conversation with operator stating that owner may want to deepen well to find a more suitable injection zone.
 
|
 
|
 
|
 
|-
 
|-
 
| -484132147
 
| 2013-10-01
 
|
 
| Injection pump not running today and they were performing pressure testing of new 4" fiber spar flow line they pressured up to 3450 psi and will monitor pressure for eight hours.
 
|
 
|
 
|
 
|-
 
|-
 
| -544143039
 
| 2013-09-12
 
|
 
| Inspection revealed that injection pump was in operation during my inspection and it was noted that injection line to facility is nearly completed and should be ready for pressure testing in the near future.
 
|
 
|
 
|
 
|-
 
|-
 
| -61173572
 
| 2014-04-10
 
|
 
| Inspection revealed that well is still down waiting on company to submit workover plan or plug said well.
 
|
 
|
 
|
 
|-
 
|-
 
| -752604507
 
| 2014-07-30
 
|
 
| Inspection revealed that injection pump was not in operation during my inspection and it was noted that  temporary storage tanks at site are being cleaned and once clean they will return them to rental company.
 
|
 
|
 
|
 
|-
 
|-
 
| -868183927
 
| 2014-07-15
 
|
 
| On site to witness rig crew run 4.5" casing in well and pressure test annulus and owner is preparing to perform small frack on well later this week.
 
Note: Packer is set at 7020' and is set in compression and there is 131 bbl of water and 30 gallon of inhibitor in annular space.
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1093358842
 
| 1093358842
 
| 2013-11-06
 
| 2013-11-06
|
+
|  
 
| Inspection revealed that injection pump was in operation today and it was noted that storage tanks at temporary storage facility has been removed and liner and other materials still need to be removed from site.
 
| Inspection revealed that injection pump was in operation today and it was noted that storage tanks at temporary storage facility has been removed and liner and other materials still need to be removed from site.
 
Note: Annulus pressure is above pressure noted on last inspection it appears that annulus fluid is foaming up and creating pressure.
 
Note: Annulus pressure is above pressure noted on last inspection it appears that annulus fluid is foaming up and creating pressure.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 1263706718
 +
| 2015-06-08
 +
|
 +
| Inspection revealed that well is in operation but it appears that it is not used much at this time.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1328090560
 
| 1328090560
 
| 2014-08-14
 
| 2014-08-14
|
+
|  
 
| Inspection revealed that injection pressure has reached maximum level and there was three technicians on site plumbing valves on well head.
 
| Inspection revealed that injection pressure has reached maximum level and there was three technicians on site plumbing valves on well head.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1360620920
 
| 1360620920
 
| 2013-02-11
 
| 2013-02-11
|
+
|  
 
| On site with company rep to discuss casing program for well and inspect E&S plan as location is being built and they plan on having conductor rig on site by the end of week.
 
| On site with company rep to discuss casing program for well and inspect E&S plan as location is being built and they plan on having conductor rig on site by the end of week.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1361117002
 
| 1361117002
 
| 2013-02-16
 
| 2013-02-16
|
+
|  
| On site to witness casing job and cementing of casing,Precision Drilling ran 504' of 13.375" and Baker Hughes cemented it in place with 400 sacks of Class 1 cement with 20 bbls of good returns.
+
| On site to witness casing job and cementing of casing,Precision Drilling ran 504' of 13.375 and Baker Hughes cemented it in place with 400 sacks of Class 1 cement with 20 bbls of good returns.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1361823271
 
| 1361823271
 
| 2013-02-25
 
| 2013-02-25
|
+
|  
| Present depth@7252' coming out of hole to run wireline log and then run 7" casing and cement it in place.
+
| Present depth@7252' coming out of hole to run wireline log and then run 7 casing and cement it in place.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1361914534
 
| 1361914534
 
| 2013-02-26
 
| 2013-02-26
|
+
|  
| On site to witness running and cementing of 7" casing string Precision drilling ran 7222' of 26# casing and 1-cementing shoe and 10-centrilizers and 1-float collar  and 1-stage tool while landing 7" casing they plugged shoe and we had to get a set of 7" elevators and long bails to move pipe upward and once they established circulation decision was made to circulate hole with drilling mud be fore we cemented pipe in place.
+
| On site to witness running and cementing of 7 casing string Precision drilling ran 7222' of 26# casing and 1-cementing shoe and 10-centrilizers and 1-float collar  and 1-stage tool while landing 7 casing they plugged shoe and we had to get a set of 7 elevators and long bails to move pipe upward and once they established circulation decision was made to circulate hole with drilling mud be fore we cemented pipe in place.
 
Baker Hughes cemented first stage with 285 sacks of 50/50 POZ MIX.
 
Baker Hughes cemented first stage with 285 sacks of 50/50 POZ MIX.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1362089676
 
| 1362089676
 
| 2013-02-28
 
| 2013-02-28
|
+
|  
| On site to witness Baker Hughes wireline truck bond log 7" casing string .
+
| On site to witness Baker Hughes wireline truck bond log 7 casing string .
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1363216637
 
| 1363216637
 
| 2013-03-13
 
| 2013-03-13
|
+
|  
 
| Inspection revealed that well has been drilled and not completed at this time in conversation with company rep stating they plan on performing testing on well in early April.
 
| Inspection revealed that well has been drilled and not completed at this time in conversation with company rep stating they plan on performing testing on well in early April.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1366326217
 
| 1366326217
 
| 2013-04-18
 
| 2013-04-18
|
+
|  
 
| I went to the location today to witness the frac job.  Having too many technical difficulties prevented them from finishing the job by the time I left the location.  12 barrels of acid and 846 lbs. of sand had been pumped.  There was a total of 363.8 barrels of slurry that was pumped downhole.  Well was shut in at 1584 psi.
 
| I went to the location today to witness the frac job.  Having too many technical difficulties prevented them from finishing the job by the time I left the location.  12 barrels of acid and 846 lbs. of sand had been pumped.  There was a total of 363.8 barrels of slurry that was pumped downhole.  Well was shut in at 1584 psi.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1366828136
 
| 1366828136
 
| 2013-04-23
 
| 2013-04-23
|
+
|  
 
| On site to witness acid job being preformed on said well Baker Hughes pumped 1000 gal of 28% acid at 5 bpm at 1930 psi and ISIP was 1750 psi and 5 min was 1700 psi and 15 min was 1690 and still falling we will start packer and tubing in well tomorrow.
 
| On site to witness acid job being preformed on said well Baker Hughes pumped 1000 gal of 28% acid at 5 bpm at 1930 psi and ISIP was 1750 psi and 5 min was 1700 psi and 15 min was 1690 and still falling we will start packer and tubing in well tomorrow.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1366894658
 
| 1366894658
 
| 2013-04-24
 
| 2013-04-24
|
+
|  
 
| On site to witness Packer and tubing run in well Key Energy service rig preformed work they ran 2100' of pipe today and will resume operations at daylight in the morning.
 
| On site to witness Packer and tubing run in well Key Energy service rig preformed work they ran 2100' of pipe today and will resume operations at daylight in the morning.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1367067230
 
| 1367067230
 
| 2013-04-25
 
| 2013-04-25
|
+
|  
| On site to witness running of 4.5" tubing and packer in hole and pressure tested.
+
| On site to witness running of 4.5 tubing and packer in hole and pressure tested.
 
Key Energy Services preformed work at site, they ran 7175' of casing and we pressure tested @2020psi and it held(TEST PASSED),Baker Hughes pumped 134 bbl of inhibitor laden fluid in annulus of well.
 
Key Energy Services preformed work at site, they ran 7175' of casing and we pressure tested @2020psi and it held(TEST PASSED),Baker Hughes pumped 134 bbl of inhibitor laden fluid in annulus of well.
 
Note: Kline packer stainless steel and it was set under 32K compression.
 
Note: Kline packer stainless steel and it was set under 32K compression.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1367882907
 
| 1367882907
 
| 2013-05-06
 
| 2013-05-06
|
+
|  
 
| Key Energy Services back on site to repair mandrel type wellhead and Baker Hughes was on site with pump truck to retest annulus of tubing once we fixed wellhead,packer is set under 32K compression and string weight of tubing is 83K.
 
| Key Energy Services back on site to repair mandrel type wellhead and Baker Hughes was on site with pump truck to retest annulus of tubing once we fixed wellhead,packer is set under 32K compression and string weight of tubing is 83K.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1372106345
 
| 1372106345
 
| 2013-06-24
 
| 2013-06-24
|
+
|  
 
| On site to witness start up of injection well, owner has placed 10-500 bbl tanks in temporary containment and placed injection pump and generator at site to perform testing on injection zone they hope to perform pressure falloff test by weeks end.
 
| On site to witness start up of injection well, owner has placed 10-500 bbl tanks in temporary containment and placed injection pump and generator at site to perform testing on injection zone they hope to perform pressure falloff test by weeks end.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1372712983
 
| 1372712983
 
| 2013-06-28
 
| 2013-06-28
|
+
|  
 
| On site to witness Blue Dot Services set down hole digital pressure gauges inside of injection string@7160' and pressure on tubing prior to setting gauges was 1790 psi.
 
| On site to witness Blue Dot Services set down hole digital pressure gauges inside of injection string@7160' and pressure on tubing prior to setting gauges was 1790 psi.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1373590724
 
| 1373590724
 
| 2013-07-10
 
| 2013-07-10
|
+
|  
 
| Inspection revealed that injection pump was in operation today and it was noted that two company owned tankers were unloading at the site during my inspection.
 
| Inspection revealed that injection pump was in operation today and it was noted that two company owned tankers were unloading at the site during my inspection.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1393016224
 
| 1393016224
 
| 2014-02-20
 
| 2014-02-20
|
+
|  
 
| On site to witness Blue Dot Wire line run tools in well to check total depth and try and determine if tubing or packer has failed integrity.
 
| On site to witness Blue Dot Wire line run tools in well to check total depth and try and determine if tubing or packer has failed integrity.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1395356262
 
| 1395356262
 
| 2014-03-20
 
| 2014-03-20
|
+
|  
 
| Inspection revealed that Key Energy Services has a coil tubing unit on well trying to clean out fill up in bottom of hole and once cleaned out they will hire service rig to release packer and pull from well to check for leakage in tubing or packer.
 
| Inspection revealed that Key Energy Services has a coil tubing unit on well trying to clean out fill up in bottom of hole and once cleaned out they will hire service rig to release packer and pull from well to check for leakage in tubing or packer.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1405716944
 
| 1405716944
 
| 2014-07-18
 
| 2014-07-18
|
+
|  
 
| On site to pressure test annulus of tubing and to witness mini frack operation on said well.
 
| On site to pressure test annulus of tubing and to witness mini frack operation on said well.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1542838378
 
| 1542838378
 
| 2013-10-16
 
| 2013-10-16
|
+
|  
 
| Inspection revealed that well was in operation today and it was noted that company owned vacuum trucks were emptying storage tanks at the site of approved temporary storage facility.
 
| Inspection revealed that well was in operation today and it was noted that company owned vacuum trucks were emptying storage tanks at the site of approved temporary storage facility.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1550706580
 +
| 2014-06-24
 +
|
 +
| Inspection revealed that service rig was still on site preparing to run tubing back into well and wash to bottom and once they have bottom of hole cleaned up they plan on running scraper in well and then place liner string in place.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1638383744
 +
| 2013-12-02
 +
|
 +
| Inspection revealed that injection pump was in operation during my inspection and it was noted that temporary storage site has been decommissioned.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1727551462
 +
| 2013-02-15
 +
|
 +
| On site for pre spud meeting with drilling contractor personnel and company reps to discuss drilling procedure and safety issues and answer questions regarding state regulations pertaining to drilling SWIW in Ohio.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1836284607
 +
| 2013-12-13
 +
|
 +
| Inspection revealed that well is not in operation at this time.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1882999581
 +
| 2014-06-17
 +
|
 +
| Inspection revealed that service rig on site mixing drill mud to kill said well and once killed they will release packer and pull from well and then they plan on running liner string into open hole section of well bore.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1890958709
 
| 1890958709
 
| 2013-02-20
 
| 2013-02-20
|
+
|  
 
| On site to witness testing of Blowout Prevent or, Greene's Energy Group tested  blind rams at 250 psi on low side and 2500 psi on high side with no decline in pressures and also tested annular section with 250 psi on low side and 1500 psi on high side with no pressure loss and kill lines were tested and choke manifold was also tested and pipe rams also passed testing levels approved by inspector.
 
| On site to witness testing of Blowout Prevent or, Greene's Energy Group tested  blind rams at 250 psi on low side and 2500 psi on high side with no decline in pressures and also tested annular section with 250 psi on low side and 1500 psi on high side with no pressure loss and kill lines were tested and choke manifold was also tested and pipe rams also passed testing levels approved by inspector.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -196296034
 +
| 2014-05-05
 +
|
 +
| Inspection revealed that well is still down waiting on plan to correct equalization issues.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1974930350
 +
| 2015-03-18
 +
|
 +
| On site to witness mini test on annulus of injection string they pressured up to 680 psi and we monitored pressure for 15 minutes with no decline in pressure and it appears that well is not used much at this time due to high pressure issues.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 2061546145
 
| 2061546145
 
| 2014-01-28
 
| 2014-01-28
|
+
|  
 
| Inspection revealed that well is down waiting on company to deepen well or possibly plug due to fact that current injection zone won't take fluid.
 
| Inspection revealed that well is down waiting on company to deepen well or possibly plug due to fact that current injection zone won't take fluid.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -2095607429
 +
| 2014-07-22
 +
|
 +
| Inspection revealed that site has been restored and well is back into active disposal mode.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -2113170097
 +
| 2013-12-30
 +
|
 +
| Inspection revealed that well is not in use at this time due to high injection pressures, owner is considering applying for deepening permit at this time.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2134671361
 +
| 2014-12-11
 +
|
 +
| Inspection revealed that well was not in operation during my inspection and it was noted that owner has winterized wellhead and associated plumbing going to well.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 269218046
 
| 269218046
 
| 2014-06-16
 
| 2014-06-16
|
+
|  
 
| Inspection revealed that service rig was on site and mixing kill fluid in preparation to release packer and remove it from well bore and once this task is completed they plan on placing liner string in open hole section of well bore.
 
| Inspection revealed that service rig was on site and mixing kill fluid in preparation to release packer and remove it from well bore and once this task is completed they plan on placing liner string in open hole section of well bore.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 368935874
 
| 368935874
 
| 2013-03-01
 
| 2013-03-01
|
+
|  
| Inspection revealed that Precision Drilling was at a depth of 7330' and were preparing to trip drill bit and install new 6.250" tri-cone bit to finish drilling well with.
+
| Inspection revealed that Precision Drilling was at a depth of 7330' and were preparing to trip drill bit and install new 6.250 tri-cone bit to finish drilling well with.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -413652614
 +
| 2014-01-06
 +
|
 +
| Inspection revealed that well is down to high injection pressure issues in conversation with operator stating that owner may want to deepen well to find a more suitable injection zone.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -484132147
 +
| 2013-10-01
 +
|
 +
| Injection pump not running today and they were performing pressure testing of new 4 fiber spar flow line they pressured up to 3450 psi and will monitor pressure for eight hours.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -544143039
 +
| 2013-09-12
 +
|
 +
| Inspection revealed that injection pump was in operation during my inspection and it was noted that injection line to facility is nearly completed and should be ready for pressure testing in the near future.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -61173572
 +
| 2014-04-10
 +
|
 +
| Inspection revealed that well is still down waiting on company to submit workover plan or plug said well.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 74355347
 
| 74355347
 
| 2013-08-21
 
| 2013-08-21
|
+
|  
 
| Inspection revealed that injection pump was in operation today and it was noted that two Ohio Oil Gathering trucks were unloading at temporary storage facility during my inspection.
 
| Inspection revealed that injection pump was in operation today and it was noted that two Ohio Oil Gathering trucks were unloading at temporary storage facility during my inspection.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 747030739
 
| 747030739
 
| 2014-06-26
 
| 2014-06-26
|
+
|  
 
| Inspection revealed that Forbes Service rig was on site washing fill up in open hole section of well to bottom and once well bore is clean they will attempt to run liner string to bottom.
 
| Inspection revealed that Forbes Service rig was on site washing fill up in open hole section of well to bottom and once well bore is clean they will attempt to run liner string to bottom.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -752604507
 +
| 2014-07-30
 +
|
 +
| Inspection revealed that injection pump was not in operation during my inspection and it was noted that  temporary storage tanks at site are being cleaned and once clean they will return them to rental company.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 766412508
 
| 766412508
 
| 2013-02-22
 
| 2013-02-22
|
+
|  
| Stopped by drilling rig for update they were drill@4750' with 8.750" bit and were planning on drilling to 7200' and run 7" casing  in this section of well.
+
| Stopped by drilling rig for update they were drill@4750' with 8.750 bit and were planning on drilling to 7200' and run 7 casing  in this section of well.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -868183927
 +
| 2014-07-15
 +
|
 +
| On site to witness rig crew run 4.5 casing in well and pressure test annulus and owner is preparing to perform small frack on well later this week.
 +
Note: Packer is set at 7020' and is set in compression and there is 131 bbl of water and 30 gallon of inhibitor in annular space.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 904552061
 
| 904552061
 
| 2013-08-21
 
| 2013-08-21
|
+
|  
 
| Injection pump in operation at the time of inspection.  There was some fluid inside the dike during my visit.  I told a truck driver about it and he dipped it out with a bucket and put it in a tank.  Everything is in good working order.
 
| Injection pump in operation at the time of inspection.  There was some fluid inside the dike during my visit.  I told a truck driver about it and he dipped it out with a bucket and put it in a tank.  Everything is in good working order.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 96115455
 
| 96115455
 
| 2013-11-20
 
| 2013-11-20
|
+
|  
 
| Inspection revealed that injection pump was in operation and it was noted that liner from temporary storage site is being removed and hauled to a approved landfill.
 
| Inspection revealed that injection pump was in operation and it was noted that liner from temporary storage site is being removed and hauled to a approved landfill.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 16:00, 15 July 2015

Well Details

Well ID: 34-167-29719
Loading map...
County: Washington
Municipality:
Operator Name: OOGC DISPOSAL CO
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-02-13
Unconventional: No
Configuration: Vertical
Well Status: Active Injection
Violations: 0
Latitude: 39.40728591
Longitude: -81.22302611

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1093358842 2013-11-06 Inspection revealed that injection pump was in operation today and it was noted that storage tanks at temporary storage facility has been removed and liner and other materials still need to be removed from site.

Note: Annulus pressure is above pressure noted on last inspection it appears that annulus fluid is foaming up and creating pressure.

1263706718 2015-06-08 Inspection revealed that well is in operation but it appears that it is not used much at this time.
1328090560 2014-08-14 Inspection revealed that injection pressure has reached maximum level and there was three technicians on site plumbing valves on well head.
1360620920 2013-02-11 On site with company rep to discuss casing program for well and inspect E&S plan as location is being built and they plan on having conductor rig on site by the end of week.
1361117002 2013-02-16 On site to witness casing job and cementing of casing,Precision Drilling ran 504' of 13.375 and Baker Hughes cemented it in place with 400 sacks of Class 1 cement with 20 bbls of good returns.
1361823271 2013-02-25 Present depth@7252' coming out of hole to run wireline log and then run 7 casing and cement it in place.
1361914534 2013-02-26 On site to witness running and cementing of 7 casing string Precision drilling ran 7222' of 26# casing and 1-cementing shoe and 10-centrilizers and 1-float collar and 1-stage tool while landing 7 casing they plugged shoe and we had to get a set of 7 elevators and long bails to move pipe upward and once they established circulation decision was made to circulate hole with drilling mud be fore we cemented pipe in place.

Baker Hughes cemented first stage with 285 sacks of 50/50 POZ MIX.

1362089676 2013-02-28 On site to witness Baker Hughes wireline truck bond log 7 casing string .
1363216637 2013-03-13 Inspection revealed that well has been drilled and not completed at this time in conversation with company rep stating they plan on performing testing on well in early April.
1366326217 2013-04-18 I went to the location today to witness the frac job. Having too many technical difficulties prevented them from finishing the job by the time I left the location. 12 barrels of acid and 846 lbs. of sand had been pumped. There was a total of 363.8 barrels of slurry that was pumped downhole. Well was shut in at 1584 psi.
1366828136 2013-04-23 On site to witness acid job being preformed on said well Baker Hughes pumped 1000 gal of 28% acid at 5 bpm at 1930 psi and ISIP was 1750 psi and 5 min was 1700 psi and 15 min was 1690 and still falling we will start packer and tubing in well tomorrow.
1366894658 2013-04-24 On site to witness Packer and tubing run in well Key Energy service rig preformed work they ran 2100' of pipe today and will resume operations at daylight in the morning.
1367067230 2013-04-25 On site to witness running of 4.5 tubing and packer in hole and pressure tested.

Key Energy Services preformed work at site, they ran 7175' of casing and we pressure tested @2020psi and it held(TEST PASSED),Baker Hughes pumped 134 bbl of inhibitor laden fluid in annulus of well. Note: Kline packer stainless steel and it was set under 32K compression.

1367882907 2013-05-06 Key Energy Services back on site to repair mandrel type wellhead and Baker Hughes was on site with pump truck to retest annulus of tubing once we fixed wellhead,packer is set under 32K compression and string weight of tubing is 83K.
1372106345 2013-06-24 On site to witness start up of injection well, owner has placed 10-500 bbl tanks in temporary containment and placed injection pump and generator at site to perform testing on injection zone they hope to perform pressure falloff test by weeks end.
1372712983 2013-06-28 On site to witness Blue Dot Services set down hole digital pressure gauges inside of injection string@7160' and pressure on tubing prior to setting gauges was 1790 psi.
1373590724 2013-07-10 Inspection revealed that injection pump was in operation today and it was noted that two company owned tankers were unloading at the site during my inspection.
1393016224 2014-02-20 On site to witness Blue Dot Wire line run tools in well to check total depth and try and determine if tubing or packer has failed integrity.
1395356262 2014-03-20 Inspection revealed that Key Energy Services has a coil tubing unit on well trying to clean out fill up in bottom of hole and once cleaned out they will hire service rig to release packer and pull from well to check for leakage in tubing or packer.
1405716944 2014-07-18 On site to pressure test annulus of tubing and to witness mini frack operation on said well.
1542838378 2013-10-16 Inspection revealed that well was in operation today and it was noted that company owned vacuum trucks were emptying storage tanks at the site of approved temporary storage facility.
-1550706580 2014-06-24 Inspection revealed that service rig was still on site preparing to run tubing back into well and wash to bottom and once they have bottom of hole cleaned up they plan on running scraper in well and then place liner string in place.
-1638383744 2013-12-02 Inspection revealed that injection pump was in operation during my inspection and it was noted that temporary storage site has been decommissioned.
-1727551462 2013-02-15 On site for pre spud meeting with drilling contractor personnel and company reps to discuss drilling procedure and safety issues and answer questions regarding state regulations pertaining to drilling SWIW in Ohio.
-1836284607 2013-12-13 Inspection revealed that well is not in operation at this time.
-1882999581 2014-06-17 Inspection revealed that service rig on site mixing drill mud to kill said well and once killed they will release packer and pull from well and then they plan on running liner string into open hole section of well bore.
1890958709 2013-02-20 On site to witness testing of Blowout Prevent or, Greene's Energy Group tested blind rams at 250 psi on low side and 2500 psi on high side with no decline in pressures and also tested annular section with 250 psi on low side and 1500 psi on high side with no pressure loss and kill lines were tested and choke manifold was also tested and pipe rams also passed testing levels approved by inspector.
-196296034 2014-05-05 Inspection revealed that well is still down waiting on plan to correct equalization issues.
-1974930350 2015-03-18 On site to witness mini test on annulus of injection string they pressured up to 680 psi and we monitored pressure for 15 minutes with no decline in pressure and it appears that well is not used much at this time due to high pressure issues.
2061546145 2014-01-28 Inspection revealed that well is down waiting on company to deepen well or possibly plug due to fact that current injection zone won't take fluid.
-2095607429 2014-07-22 Inspection revealed that site has been restored and well is back into active disposal mode.
-2113170097 2013-12-30 Inspection revealed that well is not in use at this time due to high injection pressures, owner is considering applying for deepening permit at this time.
2134671361 2014-12-11 Inspection revealed that well was not in operation during my inspection and it was noted that owner has winterized wellhead and associated plumbing going to well.
269218046 2014-06-16 Inspection revealed that service rig was on site and mixing kill fluid in preparation to release packer and remove it from well bore and once this task is completed they plan on placing liner string in open hole section of well bore.
368935874 2013-03-01 Inspection revealed that Precision Drilling was at a depth of 7330' and were preparing to trip drill bit and install new 6.250 tri-cone bit to finish drilling well with.
-413652614 2014-01-06 Inspection revealed that well is down to high injection pressure issues in conversation with operator stating that owner may want to deepen well to find a more suitable injection zone.
-484132147 2013-10-01 Injection pump not running today and they were performing pressure testing of new 4 fiber spar flow line they pressured up to 3450 psi and will monitor pressure for eight hours.
-544143039 2013-09-12 Inspection revealed that injection pump was in operation during my inspection and it was noted that injection line to facility is nearly completed and should be ready for pressure testing in the near future.
-61173572 2014-04-10 Inspection revealed that well is still down waiting on company to submit workover plan or plug said well.
74355347 2013-08-21 Inspection revealed that injection pump was in operation today and it was noted that two Ohio Oil Gathering trucks were unloading at temporary storage facility during my inspection.
747030739 2014-06-26 Inspection revealed that Forbes Service rig was on site washing fill up in open hole section of well to bottom and once well bore is clean they will attempt to run liner string to bottom.
-752604507 2014-07-30 Inspection revealed that injection pump was not in operation during my inspection and it was noted that temporary storage tanks at site are being cleaned and once clean they will return them to rental company.
766412508 2013-02-22 Stopped by drilling rig for update they were drill@4750' with 8.750 bit and were planning on drilling to 7200' and run 7 casing in this section of well.
-868183927 2014-07-15 On site to witness rig crew run 4.5 casing in well and pressure test annulus and owner is preparing to perform small frack on well later this week.

Note: Packer is set at 7020' and is set in compression and there is 131 bbl of water and 30 gallon of inhibitor in annular space.

904552061 2013-08-21 Injection pump in operation at the time of inspection. There was some fluid inside the dike during my visit. I told a truck driver about it and he dipped it out with a bucket and put it in a tank. Everything is in good working order.
96115455 2013-11-20 Inspection revealed that injection pump was in operation and it was noted that liner from temporary storage site is being removed and hauled to a approved landfill.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.