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Difference between revisions of "34-007-23888"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-007-23888
 
| Well ID: 34-007-23888
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.58430095, -80.77279886 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.584245673, -80.77299283 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Ashtabula County, Ohio|Ashtabula]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Ashtabula_County,_Ohio|Ashtabula]]
 +
|-
 +
| Municipality: [[New_Lyme_Township,_Ashtabula_County,_Ohio|New lyme Township]]
 
|-
 
|-
 
| Operator Name: [[PLATEAU ENERGY CORP]]
 
| Operator Name: [[PLATEAU ENERGY CORP]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: TANNER UNIT
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1989-10-12
 
|-
 
|-
 
| Spud Date: 1989-10-17
 
| Spud Date: 1989-10-17
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor: [[PEP DRLG]]
 +
|-
 +
| Final Drill Date: 1989-10-27
 +
|-
 +
| Well Total Depth: 6411 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 41.584245673
 +
|-
 +
| Longitude: -80.77299283
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Violations: 0
+
| CO
 +
| 1989-10-12
 +
| 3285  HALL IVAN & ASSOC INC  GeoDate  10/12/89
 
|-
 
|-
| Latitude: 41.58430095
+
| Oil and Gas
 +
| 1989-10-12
 +
| Issued Date 10/12/89 Expired Date 10/12/90 Acres 0053270 Tool Type RTAF Proposed Formation CLINTON/ROSE Proposed Depth 06411 Proposed Drill Depth 06411
 
|-
 
|-
| Longitude: -80.77279886
+
| Original Spud
 +
| 1989-10-18
 +
 +
|-
 +
| Plugged Back
 +
| 1989-10-26
 +
 +
|-
 +
| Completed
 +
| 1989-10-27
 +
 +
|-
 +
| Reached Total Depth
 +
| 1989-10-27
 +
 +
|-
 +
| Completion Report Received
 +
| 1989-12-05
 +
 +
|-
 +
| Construction Permit Expires
 +
| 1990-10-12
 +
 +
|-
 +
| CO
 +
| 1995-08-01
 +
| 5229  CUSTER A & DORIS J TANNER  GeoDate  10/12/89
 +
|-
 +
| Change of Owner
 +
| 1998-03-06
 +
| Operator changed from 5229, CUSTER A & DORIS J TANNER to 4415, PLATEAU ENERGY CORP
 +
|-
 +
| Record Last Modified
 +
| 2015-09-24
 +
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 1997-06-29
 +
| style="text-align: right;" | 3601
 +
| style="text-align: right;" | 3722
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2006-09-11
 +
| style="text-align: right;" | 3630
 +
| style="text-align: right;" | 3715
 +
| style="text-align: right;" | 18
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1990-0
 
| style="text-align:right;" | 3649.0
 
 
|  
 
|  
 +
| ACID
 +
| style="text-align: right;" | 15
 +
| style="text-align: right;" | 500 Gal
 +
| style="text-align: right;" | 0
 
|  
 
|  
|  
+
| FRAC:WATER/SAND
| style="text-align:right;" | 478.0
+
|-
|  
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1990
 +
| [[HALL IVAN & ASSOC INC]]
 +
| style="text-align: right;" | 3649
 +
| style="text-align: right;" | 478
 +
| style="text-align: right;" | 257
 +
|-
 +
| 1991
 +
| [[HALL IVAN & ASSOC INC]]
 +
| style="text-align: right;" | 1813
 +
| style="text-align: right;" | 287
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2002
 +
| [[PLATEAU ENERGY CORP]]
 +
| style="text-align: right;" | 598
 +
| style="text-align: right;" | 198
 +
| style="text-align: right;" | 365
 
|-
 
|-
 +
| 2011
 +
| [[PLATEAU ENERGY CORP]]
 +
| style="text-align: right;" | 506
 +
| style="text-align: right;" | 37
 +
| style="text-align: right;" | 155
 
|-
 
|-
| 1991-0
+
|}
| style="text-align:right;" | 1813.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 287.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1990
 +
| [[HALL IVAN & ASSOC INC]]
 +
| Brine
 +
| style="text-align: right;" | 806
 +
| style="text-align: right;" | 257
 
|-
 
|-
| 2002-0
+
| 1991
| style="text-align:right;" | 598.0
+
| [[HALL IVAN & ASSOC INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 466
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 198.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[PLATEAU ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2011-0
+
| 2011
| style="text-align:right;" | 506.0
+
| [[PLATEAU ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 75
|
+
| style="text-align: right;" | 155
| style="text-align:right;" | 37.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 11121664
+
| 0011121664
|
 
|
 
| PASSED Y WITNESSED 4/8/92 INSPECTOR JERRY KOHL DATE 04/0819/92 DATA FROM OLD VAX INFO
 
|
 
|
 
 
|  
 
|  
 +
| Preliminary Restoration
 +
| No Violations
 +
|  PASSED Y WITNESSED 4/8/92 INSPECTOR JERRY KOHL DATE 04/0819/92 DATA FROM OLD VAX INFO
 
|-
 
|-
 +
| 0048678403
 +
| 2019-01-08
 +
| Production Wells
 +
| No Violations
 +
| I conducted a compliance notice follow-up inspection for compliance notice 1444155947, regarding the cleanup of the tank battery oil spill.  During this inspection, efforts to mitigate the free oil inside the tank battery had not been conducted.  The tank battery was diked but free oil was still present within the tank battery.  The 100 BBL tank heater tube had not been repaired.  The area approximately 9X27 feet outside of the diked tank battery had been previously impacted from the oil overflowing the dike on the west side.  The impacted area outside of the dike was nonvegetated and stained.  Previous cleanup efforts had been conducted by Charles Moisio.  Identification has not been installed at the tank or well location.
 
|-
 
|-
| 69438179
+
| 0069438179
 
| 2005-06-08
 
| 2005-06-08
 +
| Production Wells
 +
| No Violations
 +
| no violations .
 +
|-
 +
| 0095140078
 +
| 2019-03-28
 +
| Production Wells
 +
| No Violations
 +
| I conducted a compliance notice follow-- inch casing with a drip bottle and regulator.  The tank battery consisted of one 100-barrel tank, one 50-barrel tank and a mechanical separator. An earthen dike surrounded the tank battery. The entire diked area was covered with oil and water due to a leaking heater tube on the 100-barrel tank. There was an area outside of dike approximately 10 foot by 10 foot that had oil on it due to the overflow of tank battery. There is a stream approximately 200 feet from the tank battery, in which the oil could possibly reach from the overflow of tank battery.  Identification was posted at the tank battery. The lease road was in stable condition. I contacted Charles Moisio about the clean-up. He informed me the he does not own the well and landowner will not let him on the property.
 +
|-
 +
| 1008683885
 +
| 2016-01-15
 +
| Production Wells
 +
| No Violations
 +
| I was on site to conduct an inspection of this well.  Oil around the wellhead and tank battery had still not been cleaned up at the time this inspection.  Please see previous report dated 11/19/2015.
 +
|-
 +
| 1289950447
 +
| 2017-08-14
 +
| Production Wells
 +
| No Violations
 +
| I conducted a compliance notice follow-up inspection for this well. The well was equipped with a pumpjack and the valve off of the domestic line was open.  The tank battery consisted of one 100 BBL production tank, one 35 BBL steel brine tank and a mechanical separator.  Valves on the separator were open.  The tank battery was full of water and oil and was contained within the dike.  No changes have been made since the last inspection report dated 1/15/2016.  Signage has not been posted on the well site.  The lease access was stable.  I contacted Charles Moisio of Plateau Energy about cleaning up the tank battery and removing all of the oil/water and impacted medium from inside the dike.
 +
|-
 +
| 1427249788
 +
| 2016-02-09
 +
| Production Wells
 +
| No Violations
 +
| I conducted a compliance notice follow-up inspection on this well.  The stuffing box was still coated with oil and paraffin.  The tank battery was still full of water and oil.  The dike was heavily eroded and there were areas of the dike which had been breached and still not repaired.  Oil and water were present outside of the dike and the area adjacent to the dike was devoid of vegetation.  Signage on the production tank was not legible and still needs replaced.
 +
|-
 +
| 1432085773
 +
| 2015-11-19
 +
| Production Wells
 +
| No Violations
 +
| I was on site to conduct an inspection of this well.  Oil around the wellhead and tank battery had still not been cleaned up at the time this inspection.  Please see previous report dated 11/06/2015.
 +
|-
 +
| 1444155947
 +
| 2015-09-22
 +
| Production Wells
 +
| Violations Noted
 +
| I was on site to conduct an order follow-up inspection of this well.  The well has a pump jack on it and is not in production.  There is a domestic gas line.  The stuffing box was coated with oil and paraffin.  The tank battery consisted of  one, 100 BBL production tank, a 1500 gallon steel brine tank, and a mechanical separator.  The tank battery was full of water and oil.  The dike was heavily eroded and there were areas of the dike which had been breached.  Oil and water were present outside of the dike and the area adjacent to the dike was devoid of vegetation.  I took a high range Quantab sample and the reading on the Quantab was 5.  The signage on the production tank was not legible.  The lease access was stable.  The following needs completed by: 
 +
1)  Clean-up all spilled oil/brine in tank battery and repair the dike (10-20-15)
 +
2)  Clean-up the parrafin around the wellhead and stuffing box (10-20-15)
 +
3) A new identification sign needs posted (10-20-15)
 +
|-
 +
| 1476062804
 +
| 2018-08-22
 +
| Production Wells
 +
| No Violations
 +
| I conducted a compliance notice follow-up inspection for compliance notice 1444155947.  The well was equipped with a pumping unit and the valves on the tubing and flow line were closed.  There was an active domestic line plumbed off of the 4.5 inch casing with a drip bottle and regulator.  The tank battery consisted of one 100 BBL tank, one 50 BBL tank and a mechanical separator.  The tank battery was diked but free oil was still present within the tank battery.  The entire diked area was covered with oil and water due to a leaking heater tube on the 100 BBL tank.  An area approximately 9X27 feet outside of the diked tank battery had been previously impacted from the oil overflowing the dike on the west side.  The impacted area outside of the dike was nonvegetated and stained.  Previous cleanup efforts had been conducted by Charles Moisio, but the heater tube on the 100 BBL tank has never been repaired.  Signage was illegible at the tank battery location and lease access stable.  Efforts to contact Charles Moisio about removing the oil and water from the dike and repairing the leaking tank were unsuccessful.
 +
|-
 +
| 1501128706
 +
| 2017-08-15
 +
| Production Wells
 +
| No Violations
 +
| I conducted a compliance notice follow-up on this site for the previous inspection dated 8/14/2017.  Met Charles Moisio of Plateau Energy on site to conduct the cleanup of the tank battery.  Mr. Moisio was on site with a pump truck to begin the removal of the oil/water from the tank battery.  Approximately 3 BBLs of fluid was removed from the tank battery.  Mr. Moisio indicated that he would return to the site to remove the rest of the fluid and repair the leaking heater tube on the 100 BBL tank that had caused the release.
 +
|-
 +
| 1631335236
 +
| 2015-11-06
 +
| Production Wells
 +
| No Violations
 +
| I was on site for a follow-up inspection to the compliance notice issued on 9/22/2015 for this well.  No changes have occurred since the last inspection.  I spoke with Charlie Moseo owner of Plateau Energy Corp about when the well and tank battery clean-up efforts would begin.  He indicated that he would be on site the following week to begin addressing the compliance issues.
 +
|-
 +
| 1658658260
 +
| 2018-02-14
 +
| Production Wells
 +
| No Violations
 +
| I inspected this well as a follow-up to Chiefs Order  #2014-202 for failure to maintain liability insurance. At the time of this inspection, the well was being reported to be utilized by the landowner for domestic gas, but the well was not being produced commercially based on the closed flow-line connections. The was a pump jack unit and associated tank battery (comprised of one 100-barrel steel production tank, 50-barrel brine tank, with mechanical separator)  Elements of the system appeared to be in disrepair and the flow-line connections were closed. There was remnants of visible oil in the tank battery containment from a prior release that had not been remediated. There remained no active liability insurance on file for Plateau Energy Corp.
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 1444155947
 +
| US-OH-112920
 +
| 2018-08-23
 
|  
 
|  
| no violations .
+
| Well operation causing pollution and contamination
 +
|-
 +
| 1444155947
 +
| US-OH-112921
 +
| 2018-08-23
 
|  
 
|  
 +
| Failure to legibly identify well
 +
|-
 +
| 1444155947
 +
| US-OH-112922
 +
| 2018-08-23
 
|  
 
|  
 +
| No SPCC dike/or failure to keep dike free of water or oil
 +
|-
 +
| 1444155947
 +
| US-OH-112923
 +
| 2018-08-23
 
|  
 
|  
 +
| Dike or pit not able to prevent escape of brine or other wastes
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 19:29, 24 July 2019

Well Details

Well ID: 34-007-23888
Loading map...
Country: United States
State: Ohio
County: Ashtabula
Municipality: New lyme Township
Operator Name: PLATEAU ENERGY CORP
Well Pad ID:
Farm/Lease Name: TANNER UNIT
License Status: Producing
License Date: 1989-10-12
Spud Date: 1989-10-17
Spud Drilling Contractor: PEP DRLG
Final Drill Date: 1989-10-27
Well Total Depth: 6411 ft
Configuration: Vertical
Latitude: 41.584245673
Longitude: -80.77299283

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1989-10-12 3285 HALL IVAN & ASSOC INC GeoDate 10/12/89
Oil and Gas 1989-10-12 Issued Date 10/12/89 Expired Date 10/12/90 Acres 0053270 Tool Type RTAF Proposed Formation CLINTON/ROSE Proposed Depth 06411 Proposed Drill Depth 06411
Original Spud 1989-10-18
Plugged Back 1989-10-26
Completed 1989-10-27
Reached Total Depth 1989-10-27
Completion Report Received 1989-12-05
Construction Permit Expires 1990-10-12
CO 1995-08-01 5229 CUSTER A & DORIS J TANNER GeoDate 10/12/89
Change of Owner 1998-03-06 Operator changed from 5229, CUSTER A & DORIS J TANNER to 4415, PLATEAU ENERGY CORP
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3601 3722 0
2006-09-11 3630 3715 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 500 Gal 0 FRAC:WATER/SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1990 HALL IVAN & ASSOC INC 3649 478 257
1991 HALL IVAN & ASSOC INC 1813 287 365
2002 PLATEAU ENERGY CORP 598 198 365
2011 PLATEAU ENERGY CORP 506 37 155

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1990 HALL IVAN & ASSOC INC Brine 806 257
1991 HALL IVAN & ASSOC INC Brine 466 365
2002 PLATEAU ENERGY CORP Brine 0 365
2011 PLATEAU ENERGY CORP Brine 75 155

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0011121664 Preliminary Restoration No Violations PASSED Y WITNESSED 4/8/92 INSPECTOR JERRY KOHL DATE 04/0819/92 DATA FROM OLD VAX INFO
0048678403 2019-01-08 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice 1444155947, regarding the cleanup of the tank battery oil spill. During this inspection, efforts to mitigate the free oil inside the tank battery had not been conducted. The tank battery was diked but free oil was still present within the tank battery. The 100 BBL tank heater tube had not been repaired. The area approximately 9X27 feet outside of the diked tank battery had been previously impacted from the oil overflowing the dike on the west side. The impacted area outside of the dike was nonvegetated and stained. Previous cleanup efforts had been conducted by Charles Moisio. Identification has not been installed at the tank or well location.
0069438179 2005-06-08 Production Wells No Violations no violations .
0095140078 2019-03-28 Production Wells No Violations I conducted a compliance notice follow-- inch casing with a drip bottle and regulator. The tank battery consisted of one 100-barrel tank, one 50-barrel tank and a mechanical separator. An earthen dike surrounded the tank battery. The entire diked area was covered with oil and water due to a leaking heater tube on the 100-barrel tank. There was an area outside of dike approximately 10 foot by 10 foot that had oil on it due to the overflow of tank battery. There is a stream approximately 200 feet from the tank battery, in which the oil could possibly reach from the overflow of tank battery. Identification was posted at the tank battery. The lease road was in stable condition. I contacted Charles Moisio about the clean-up. He informed me the he does not own the well and landowner will not let him on the property.
1008683885 2016-01-15 Production Wells No Violations I was on site to conduct an inspection of this well. Oil around the wellhead and tank battery had still not been cleaned up at the time this inspection. Please see previous report dated 11/19/2015.
1289950447 2017-08-14 Production Wells No Violations I conducted a compliance notice follow-up inspection for this well. The well was equipped with a pumpjack and the valve off of the domestic line was open. The tank battery consisted of one 100 BBL production tank, one 35 BBL steel brine tank and a mechanical separator. Valves on the separator were open. The tank battery was full of water and oil and was contained within the dike. No changes have been made since the last inspection report dated 1/15/2016. Signage has not been posted on the well site. The lease access was stable. I contacted Charles Moisio of Plateau Energy about cleaning up the tank battery and removing all of the oil/water and impacted medium from inside the dike.
1427249788 2016-02-09 Production Wells No Violations I conducted a compliance notice follow-up inspection on this well. The stuffing box was still coated with oil and paraffin. The tank battery was still full of water and oil. The dike was heavily eroded and there were areas of the dike which had been breached and still not repaired. Oil and water were present outside of the dike and the area adjacent to the dike was devoid of vegetation. Signage on the production tank was not legible and still needs replaced.
1432085773 2015-11-19 Production Wells No Violations I was on site to conduct an inspection of this well. Oil around the wellhead and tank battery had still not been cleaned up at the time this inspection. Please see previous report dated 11/06/2015.
1444155947 2015-09-22 Production Wells Violations Noted I was on site to conduct an order follow-up inspection of this well. The well has a pump jack on it and is not in production. There is a domestic gas line. The stuffing box was coated with oil and paraffin. The tank battery consisted of one, 100 BBL production tank, a 1500 gallon steel brine tank, and a mechanical separator. The tank battery was full of water and oil. The dike was heavily eroded and there were areas of the dike which had been breached. Oil and water were present outside of the dike and the area adjacent to the dike was devoid of vegetation. I took a high range Quantab sample and the reading on the Quantab was 5. The signage on the production tank was not legible. The lease access was stable. The following needs completed by:

1) Clean-up all spilled oil/brine in tank battery and repair the dike (10-20-15) 2) Clean-up the parrafin around the wellhead and stuffing box (10-20-15) 3) A new identification sign needs posted (10-20-15)

1476062804 2018-08-22 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice 1444155947. The well was equipped with a pumping unit and the valves on the tubing and flow line were closed. There was an active domestic line plumbed off of the 4.5 inch casing with a drip bottle and regulator. The tank battery consisted of one 100 BBL tank, one 50 BBL tank and a mechanical separator. The tank battery was diked but free oil was still present within the tank battery. The entire diked area was covered with oil and water due to a leaking heater tube on the 100 BBL tank. An area approximately 9X27 feet outside of the diked tank battery had been previously impacted from the oil overflowing the dike on the west side. The impacted area outside of the dike was nonvegetated and stained. Previous cleanup efforts had been conducted by Charles Moisio, but the heater tube on the 100 BBL tank has never been repaired. Signage was illegible at the tank battery location and lease access stable. Efforts to contact Charles Moisio about removing the oil and water from the dike and repairing the leaking tank were unsuccessful.
1501128706 2017-08-15 Production Wells No Violations I conducted a compliance notice follow-up on this site for the previous inspection dated 8/14/2017. Met Charles Moisio of Plateau Energy on site to conduct the cleanup of the tank battery. Mr. Moisio was on site with a pump truck to begin the removal of the oil/water from the tank battery. Approximately 3 BBLs of fluid was removed from the tank battery. Mr. Moisio indicated that he would return to the site to remove the rest of the fluid and repair the leaking heater tube on the 100 BBL tank that had caused the release.
1631335236 2015-11-06 Production Wells No Violations I was on site for a follow-up inspection to the compliance notice issued on 9/22/2015 for this well. No changes have occurred since the last inspection. I spoke with Charlie Moseo owner of Plateau Energy Corp about when the well and tank battery clean-up efforts would begin. He indicated that he would be on site the following week to begin addressing the compliance issues.
1658658260 2018-02-14 Production Wells No Violations I inspected this well as a follow-up to Chiefs Order #2014-202 for failure to maintain liability insurance. At the time of this inspection, the well was being reported to be utilized by the landowner for domestic gas, but the well was not being produced commercially based on the closed flow-line connections. The was a pump jack unit and associated tank battery (comprised of one 100-barrel steel production tank, 50-barrel brine tank, with mechanical separator) Elements of the system appeared to be in disrepair and the flow-line connections were closed. There was remnants of visible oil in the tank battery containment from a prior release that had not been remediated. There remained no active liability insurance on file for Plateau Energy Corp.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1444155947 US-OH-112920 2018-08-23 Well operation causing pollution and contamination
1444155947 US-OH-112921 2018-08-23 Failure to legibly identify well
1444155947 US-OH-112922 2018-08-23 No SPCC dike/or failure to keep dike free of water or oil
1444155947 US-OH-112923 2018-08-23 Dike or pit not able to prevent escape of brine or other wastes

For data sources see[9]

References