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Difference between revisions of "34-175-60946"

m
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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-175-60946
 
| Well ID: 34-175-60946
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.95002408, -83.25177959 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.950078862, -83.25170115 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Wyandot County, Ohio|Wyandot]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Wyandot_County,_Ohio|Wyandot]]
 +
|-
 +
| Municipality: [[Tymochtee_Township,_Wyandot_County,_Ohio|Tymochtee Township]]
 
|-
 
|-
 
| Operator Name: [[HISTORIC OWNER]]
 
| Operator Name: [[HISTORIC OWNER]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: WALTON
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date:  
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 40.950078862
 +
|-
 +
| Longitude: -83.25170115
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Oil and Gas
 +
| 2005-04-25
 +
| INPSECTED BY TOM BENKO ON 4/13/05. ORPHAN WELL, CASE # 1998-07-099.
 
|-
 
|-
| Violations: 0
+
| Plugged by Orphan Well Program
 +
| 2014-11-11
 +
| Plugged by Orphan Well Program
 
|-
 
|-
| Latitude: 40.95002408
+
| Plugged/Abandoned
 +
| 2014-11-11
 +
| INPSECTED BY TOM BENKO ON 4/13/05. ORPHAN WELL, CASE # 1998-07-099.
 
|-
 
|-
| Longitude: -83.25177959
+
| Record Last Modified
 +
| 2015-05-19
 +
| INPSECTED BY TOM BENKO ON 4/13/05. ORPHAN WELL, CASE # 1998-07-099.
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0232555660
 +
| 2014-11-04
 +
| Orphan
 +
| No Violations
 +
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the crew started drilling with the 4 cable tool bit at 9 am. The fresh water flow was diverted to the existing drain tile. The water flow could be moved to the half tank in the event anything other than the existing fresh water in encountered. An obstruction was hit at 60 and again at 151. These obstructions were broken through and a total depth of 1462 was reached. The crew then ran 1430 of 1.5 tubing with a 5 mud anchor in preparation for plugging on 11-5-14. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 55 ppm Hydrogen Sulfide at the wellhead during the cleanout. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide.
 
|-
 
|-
| -1196437190
+
| 0565158973
| 2005-04-13
+
| 2014-11-11
|  
+
| Plug / Plug Back
| orphan well case number 1998-07-099. Add well to system.
+
| No Violations
|  
+
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the flow of water from the well had slowed even more overnight. The flow continued to slow as the brush and stone plug set on 11-10-14 at about 60 was added to over the next 4 hours. The final length of this plug was from 60 to 45 and 35 of 1.5 tubing was set above that. A heavy mix of 50/50 Pozmix with 4% calcium added was pumped down the well until returns were observed at the surface. A total of 60 sacks was used and the cement was weighed by the inspector at 15.1 lb./gal. The level inside the well settled at about 6 below grade with no sign of gas or water. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 4 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 2 ppm of Hydrogen Sulfide throughout the plugging.
|  
+
|-
|  
+
| 0758914789
 +
| 2014-03-05
 +
| Orphan
 +
| No Violations
 +
| At the time of the inspection there was a steady flow of water coming from the casing of the suspected well. This water tested at a 2 on a low range quantab and flowed into a drainage tile in the middle of a 10 x 12 depression. The path of this drainage tile is unknown but slow flowing puddles of water were evident to the north stretching an undetermined distance. The temperature at the time was below freezing but these puddle had not frozen over. A low range quantab reading of 4 was obtained from one of the puddles approximately 50 north of the well. A follow-up inspection will be needed to determine the extent of the flowing water due to heavy snow still on the ground.
 
|-
 
|-
 +
| 0936752812
 +
| 2014-11-10
 +
| Plug / Plug Back
 +
| No Violations
 +
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection there was no sign of the surface plug set on 11-7-14 was tagged and fresh water was still flowing from the well at about half the rate as before plugging. The decision was made to set a brush and stone plug at about 60 to slow the water even more before setting a final plug. The plugging crew spent 4 hours on this plug with little effect on the flow of water from the well. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 21 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 5 ppm of Hydrogen Sulfide throughout the plugging.
 
|-
 
|-
| -1.19644E+15
+
| 1196437190
 
| 2005-04-13
 
| 2005-04-13
|  
+
| Orphan
 +
| No Violations
 
| orphan well case number 1998-07-099. Add well to system.
 
| orphan well case number 1998-07-099. Add well to system.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1362422707
 
| 1362422707
 
| 2013-03-04
 
| 2013-03-04
|  
+
| Orphan
 +
| No Violations
 
| Inspected the Walton #1 (#60946) as a standard orphan well status check. This well is a active flowing artesian water well with associated sulfur smell. Location is croplands.
 
| Inspected the Walton #1 (#60946) as a standard orphan well status check. This well is a active flowing artesian water well with associated sulfur smell. Location is croplands.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1375974318
 
| 1375974318
 
| 2013-07-31
 
| 2013-07-31
|  
+
| Orphan
| An inspection of this orphan well revealed a strong and consistent flow of artesian water and the release of H2S from the inside of an approximate 6.5 inside diameter casing (ID).  The flow rate was not measured (Refer to video clip for details) but amount of water released was discharged just as quickly into a second casing.  The immediate area surrounding the well consisted of a depression in the ground surface (i.e. resembled a pit approx 5'x 5') with pooled water and a layer of white film.  A second casing was also observed within this depression approximately 5' away and contained a yellow filter style device for debris on the top that is often seen for drain tile.  The fluid that was being released from the approx 6.5 (ID) casing drained into this casing.  A measurement of this casing could not be obtained due to the fluid level and presence of H2S.  The immediate area also contained a concrete monument likely from a standard rig that measured 10' x 5' x 2.5'.  The well was monitored with a gas meter equipped with an automatic pump, a probe and filter.  A strong rotten egg odor was encountered and the H2S reading from this well reached a maximum of 36 ppm.  The well was situated on property designated as agricultural field with no crops planted at this time, no residential dwellings within approximately 500', and located off a state route.  A GPS reading was obtained and recorded for the potential entry off state route.  Central Office will be notified of H2S status for this county and township.
+
| No Violations
|
+
| An inspection of this orphan well revealed a strong and consistent flow of artesian water and the release of H2S from the inside of an approximate 6.5 inside diameter casing (ID).  The flow rate was not measured (Refer to video clip for details) but amount of water released was discharged just as quickly into a second casing.  The immediate area surrounding the well consisted of a depression in the ground surface (i.e. resembled a pit approx 5x 5) with pooled water and a layer of white film.  A second casing was also observed within this depression approximately 5 away and contained a yellow filter style device for debris on the top that is often seen for drain tile.  The fluid that was being released from the approx 6.5 (ID) casing drained into this casing.  A measurement of this casing could not be obtained due to the fluid level and presence of H2S.  The immediate area also contained a concrete monument likely from a standard rig that measured 10 x 5 x 2.5.  The well was monitored with a gas meter equipped with an automatic pump, a probe and filter.  A strong rotten egg odor was encountered and the H2S reading from this well reached a maximum of 36 ppm.  The well was situated on property designated as agricultural field with no crops planted at this time, no residential dwellings within approximately 500, and located off a state route.  A GPS reading was obtained and recorded for the potential entry off state route.  Central Office will be notified of H2S status for this county and township.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1415733988
 
| 1415733988
 
| 2014-10-30
 
| 2014-10-30
|  
+
| Orphan
 +
| No Violations
 
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the rig and half tank were moved to the location. The current farmer for the property, Corey Bills, was on location to represent the landowner. The well was still flowing water from the top of the casing. The plugging process is scheduled to start on Monday, 11-3-14.
 
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the rig and half tank were moved to the location. The current farmer for the property, Corey Bills, was on location to represent the landowner. The well was still flowing water from the top of the casing. The plugging process is scheduled to start on Monday, 11-3-14.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1415905459
 
| 1415905459
 
| 2014-11-06
 
| 2014-11-06
|  
+
| Orphan
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the bottom plug set on 11-5-14 was tagged at 980'. Fresh water was still flowing from the well at about the same rate as before plugging. The plugging crew set 952' of 1.5 tubing and ran 300 sacks of 50/50 Pozmix in two stages. Good circulation was maintained throughout the cementing. A crew from O'Brien's Safety Services was on location to monitor gas levels. There were readings as high as 24 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide throughout the plugging.
+
| No Violations
|
+
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the bottom plug set on 11-5-14 was tagged at 980. Fresh water was still flowing from the well at about the same rate as before plugging. The plugging crew set 952 of 1.5 tubing and ran 300 sacks of 50/50 Pozmix in two stages. Good circulation was maintained throughout the cementing. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 24 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide throughout the plugging.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1416245047
 
| 1416245047
 
| 2014-11-07
 
| 2014-11-07
|  
+
| Plug / Plug Back
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the second plug set on 11-6-14 was tagged at 110'. Fresh water was still flowing from the well at about the same rate as before plugging. The next plug was pumped down the well through the wellhead at a maximum pressure of 280 psi with 75 sacks of 50/50 Pozmix. Immediately after pumping the level inside the well remained static with no signs of any gas or water. The well was then shut in. A crew from O'Brien's Safety Services was on location to monitor gas levels. There were readings as high as 14 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 5 ppm of Hydrogen Sulfide throughout the plugging.
+
| No Violations
|
+
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the second plug set on 11-6-14 was tagged at 110. Fresh water was still flowing from the well at about the same rate as before plugging. The next plug was pumped down the well through the wellhead at a maximum pressure of 280 psi with 75 sacks of 50/50 Pozmix. Immediately after pumping the level inside the well remained static with no signs of any gas or water. The well was then shut in. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 14 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 5 ppm of Hydrogen Sulfide throughout the plugging.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1432047954
 
| 1432047954
 
| 2015-05-19
 
| 2015-05-19
|  
+
| Final Restoration
 +
| No Violations
 
| At the time of the inspection the area was graded and all other equipment and debris has been removed. The small pit surrounding the existing drainage tile that was put in by the landowner remains next to the well. Final Restoration Passed.
 
| At the time of the inspection the area was graded and all other equipment and debris has been removed. The small pit surrounding the existing drainage tile that was put in by the landowner remains next to the well. Final Restoration Passed.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1471065274
 
| 1471065274
 
| 2014-11-12
 
| 2014-11-12
|  
+
| Plug / Plug Back
| This well was plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the cement level inside the well was at 6' below grade and there was no sign of  any gas or water. The restoration work on the location was underway and the well was cut off below grade. The identification plate was then attached to the well and the remaining hole was filled in. The concrete water basin will be removed but the existing drainage tile will be left in place.
+
| No Violations
|
+
| This well was plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the cement level inside the well was at 6 below grade and there was no sign of  any gas or water. The restoration work on the location was underway and the well was cut off below grade. The identification plate was then attached to the well and the remaining hole was filled in. The concrete water basin will be removed but the existing drainage tile will be left in place.
|
 
|
 
|-
 
 
|-
 
|-
 
| 2133080597
 
| 2133080597
 
| 2014-11-03
 
| 2014-11-03
|  
+
| Orphan
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the water flow from the well was diverted by pumping it from the well to the half tank. This allowed a collar to be welded to the 10 casing for attaching a wellhead. A crew from O'Brien's Safety Services was on location to monitor gas levels. There were readings as high as 73 ppm Hydrogen Sulfide at the wellhead during the cleanout. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide.
+
| No Violations
|
+
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the water flow from the well was diverted by pumping it from the well to the half tank. This allowed a collar to be welded to the 10 casing for attaching a wellhead. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 73 ppm Hydrogen Sulfide at the wellhead during the cleanout. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide.
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -232555660
+
|}-->
| 2014-11-04
 
|
 
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the crew started drilling with the 4 cable tool bit at 9 am. The fresh water flow was diverted to the existing drain tile. The water flow could be moved to the half tank in the event anything other than the existing fresh water in encountered. An obstruction was hit at 60' and again at 151'. These obstructions were broken through and a total depth of 1462' was reached. The crew then ran 1430' of 1.5 tubing with a 5' mud anchor in preparation for plugging on 11-5-14. A crew from O'Brien's Safety Services was on location to monitor gas levels. There were readings as high as 55 ppm Hydrogen Sulfide at the wellhead during the cleanout. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide.
 
|
 
|
 
|
 
|-
 
|-
 
| 565158973
 
| 2014-11-11
 
|
 
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the flow of water from the well had slowed even more overnight. The flow continued to slow as the brush and stone plug set on 11-10-14 at about 60' was added to over the next 4 hours. The final length of this plug was from 60' to 45' and 35' of 1.5 tubing was set above that. A heavy mix of 50/50 Pozmix with 4% calcium added was pumped down the well until returns were observed at the surface. A total of 60 sacks was used and the cement was weighed by the inspector at 15.1 lb./gal. The level inside the well settled at about 6' below grade with no sign of gas or water. A crew from O'Brien's Safety Services was on location to monitor gas levels. There were readings as high as 4 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 2 ppm of Hydrogen Sulfide throughout the plugging.
 
|
 
|
 
|
 
|-
 
|-
 
| 758914789
 
| 2014-03-05
 
|
 
| At the time of the inspection there was a steady flow of water coming from the casing of the suspected well. This water tested at a 2 on a low range quantab and flowed into a drainage tile in the middle of a 10' x 12' depression. The path of this drainage tile is unknown but slow flowing puddles of water were evident to the north stretching an undetermined distance. The temperature at the time was below freezing but these puddle had not frozen over. A low range quantab reading of 4 was obtained from one of the puddles approximately 50' north of the well. A follow-up inspection will be needed to determine the extent of the flowing water due to heavy snow still on the ground.
 
|
 
|
 
|
 
|-
 
|-
 
| 936752812
 
| 2014-11-10
 
|
 
| This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection there was no sign of the surface plug set on 11-7-14 was tagged and fresh water was still flowing from the well at about half the rate as before plugging. The decision was made to set a brush and stone plug at about 60' to slow the water even more before setting a final plug. The plugging crew spent 4 hours on this plug with little effect on the flow of water from the well. A crew from O'Brien's Safety Services was on location to monitor gas levels. There were readings as high as 21 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 5 ppm of Hydrogen Sulfide throughout the plugging.
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 19:00, 30 July 2019

Well Details

Well ID: 34-175-60946
Loading map...
Country: United States
State: Ohio
County: Wyandot
Municipality: Tymochtee Township
Operator Name: HISTORIC OWNER
Well Pad ID:
Farm/Lease Name: WALTON
License Status: Final Restoration
License Date:
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 40.950078862
Longitude: -83.25170115

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 2005-04-25 INPSECTED BY TOM BENKO ON 4/13/05. ORPHAN WELL, CASE # 1998-07-099.
Plugged by Orphan Well Program 2014-11-11 Plugged by Orphan Well Program
Plugged/Abandoned 2014-11-11 INPSECTED BY TOM BENKO ON 4/13/05. ORPHAN WELL, CASE # 1998-07-099.
Record Last Modified 2015-05-19 INPSECTED BY TOM BENKO ON 4/13/05. ORPHAN WELL, CASE # 1998-07-099.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0232555660 2014-11-04 Orphan No Violations This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the crew started drilling with the 4 cable tool bit at 9 am. The fresh water flow was diverted to the existing drain tile. The water flow could be moved to the half tank in the event anything other than the existing fresh water in encountered. An obstruction was hit at 60 and again at 151. These obstructions were broken through and a total depth of 1462 was reached. The crew then ran 1430 of 1.5 tubing with a 5 mud anchor in preparation for plugging on 11-5-14. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 55 ppm Hydrogen Sulfide at the wellhead during the cleanout. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide.
0565158973 2014-11-11 Plug / Plug Back No Violations This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the flow of water from the well had slowed even more overnight. The flow continued to slow as the brush and stone plug set on 11-10-14 at about 60 was added to over the next 4 hours. The final length of this plug was from 60 to 45 and 35 of 1.5 tubing was set above that. A heavy mix of 50/50 Pozmix with 4% calcium added was pumped down the well until returns were observed at the surface. A total of 60 sacks was used and the cement was weighed by the inspector at 15.1 lb./gal. The level inside the well settled at about 6 below grade with no sign of gas or water. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 4 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 2 ppm of Hydrogen Sulfide throughout the plugging.
0758914789 2014-03-05 Orphan No Violations At the time of the inspection there was a steady flow of water coming from the casing of the suspected well. This water tested at a 2 on a low range quantab and flowed into a drainage tile in the middle of a 10 x 12 depression. The path of this drainage tile is unknown but slow flowing puddles of water were evident to the north stretching an undetermined distance. The temperature at the time was below freezing but these puddle had not frozen over. A low range quantab reading of 4 was obtained from one of the puddles approximately 50 north of the well. A follow-up inspection will be needed to determine the extent of the flowing water due to heavy snow still on the ground.
0936752812 2014-11-10 Plug / Plug Back No Violations This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection there was no sign of the surface plug set on 11-7-14 was tagged and fresh water was still flowing from the well at about half the rate as before plugging. The decision was made to set a brush and stone plug at about 60 to slow the water even more before setting a final plug. The plugging crew spent 4 hours on this plug with little effect on the flow of water from the well. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 21 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 5 ppm of Hydrogen Sulfide throughout the plugging.
1196437190 2005-04-13 Orphan No Violations orphan well case number 1998-07-099. Add well to system.
1362422707 2013-03-04 Orphan No Violations Inspected the Walton #1 (#60946) as a standard orphan well status check. This well is a active flowing artesian water well with associated sulfur smell. Location is croplands.
1375974318 2013-07-31 Orphan No Violations An inspection of this orphan well revealed a strong and consistent flow of artesian water and the release of H2S from the inside of an approximate 6.5 inside diameter casing (ID). The flow rate was not measured (Refer to video clip for details) but amount of water released was discharged just as quickly into a second casing. The immediate area surrounding the well consisted of a depression in the ground surface (i.e. resembled a pit approx 5x 5) with pooled water and a layer of white film. A second casing was also observed within this depression approximately 5 away and contained a yellow filter style device for debris on the top that is often seen for drain tile. The fluid that was being released from the approx 6.5 (ID) casing drained into this casing. A measurement of this casing could not be obtained due to the fluid level and presence of H2S. The immediate area also contained a concrete monument likely from a standard rig that measured 10 x 5 x 2.5. The well was monitored with a gas meter equipped with an automatic pump, a probe and filter. A strong rotten egg odor was encountered and the H2S reading from this well reached a maximum of 36 ppm. The well was situated on property designated as agricultural field with no crops planted at this time, no residential dwellings within approximately 500, and located off a state route. A GPS reading was obtained and recorded for the potential entry off state route. Central Office will be notified of H2S status for this county and township.
1415733988 2014-10-30 Orphan No Violations This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the rig and half tank were moved to the location. The current farmer for the property, Corey Bills, was on location to represent the landowner. The well was still flowing water from the top of the casing. The plugging process is scheduled to start on Monday, 11-3-14.
1415905459 2014-11-06 Orphan No Violations This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the bottom plug set on 11-5-14 was tagged at 980. Fresh water was still flowing from the well at about the same rate as before plugging. The plugging crew set 952 of 1.5 tubing and ran 300 sacks of 50/50 Pozmix in two stages. Good circulation was maintained throughout the cementing. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 24 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide throughout the plugging.
1416245047 2014-11-07 Plug / Plug Back No Violations This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the second plug set on 11-6-14 was tagged at 110. Fresh water was still flowing from the well at about the same rate as before plugging. The next plug was pumped down the well through the wellhead at a maximum pressure of 280 psi with 75 sacks of 50/50 Pozmix. Immediately after pumping the level inside the well remained static with no signs of any gas or water. The well was then shut in. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 14 ppm Hydrogen Sulfide at the wellhead when the well was opened that morning. Levels around the well and work area stayed between zero and 5 ppm of Hydrogen Sulfide throughout the plugging.
1432047954 2015-05-19 Final Restoration No Violations At the time of the inspection the area was graded and all other equipment and debris has been removed. The small pit surrounding the existing drainage tile that was put in by the landowner remains next to the well. Final Restoration Passed.
1471065274 2014-11-12 Plug / Plug Back No Violations This well was plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the cement level inside the well was at 6 below grade and there was no sign of any gas or water. The restoration work on the location was underway and the well was cut off below grade. The identification plate was then attached to the well and the remaining hole was filled in. The concrete water basin will be removed but the existing drainage tile will be left in place.
2133080597 2014-11-03 Orphan No Violations This well is under contract to be plugged for the Orphan Well Program by Davis Well Service. At the time of the inspection the water flow from the well was diverted by pumping it from the well to the half tank. This allowed a collar to be welded to the 10 casing for attaching a wellhead. A crew from OBriens Safety Services was on location to monitor gas levels. There were readings as high as 73 ppm Hydrogen Sulfide at the wellhead during the cleanout. Levels around the well and work area stayed between zero and 15 ppm of Hydrogen Sulfide.

For data sources see[3]

References