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34-089-23256

Well Details

Well ID: 34-089-23256
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Country: United States
State: Ohio
County: Licking
Municipality: Hopewell Township
Operator Name: NATIONAL ENERGY EXP INC
Well Pad ID:
Farm/Lease Name: SFORZA LARRY L
License Status: Plugged and Abandoned
License Date: 2016-11-14
Spud Date: 1975-11-15
Spud Drilling Contractor:
Final Drill Date: 1975-12-19
Well Total Depth: 2897.00 ft
Configuration: Vertical
Latitude: 40.020000
Longitude: -82.230000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1975-11-14 627 KENOIL GeoDate 11/14/75
Original Spud 1975-11-15
Completed 1975-12-19
Reached Total Depth 1975-12-19
CO 1990-12-04 627 KENOIL GeoDate 12/4/90
COMBINATION WELL 1990-12-04 Issued Date 12/4/90 Expired Date 12/4/91 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date 1/7/91
APP 2010-05-28 Proposed Formations:CLINTON, Issued Date:5/28/2010, Expired Date:5/28/2011 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Completion Report Received 2016-11-03
APP 2016-11-14 Proposed Formations:CLINTON SAND, Issued Date:11/14/2016, Expired Date:11/14/2017 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-12-20
Record Last Modified 2017-05-25
Construction Permit Expires 2017-11-14

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2200 Bbl 20000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 JADOIL INC D VERNAU 258.00 202.00 0
1985 JADOIL INC D VERNAU 270.00 286.00 365
1986 JADOIL INC D VERNAU 567.00 380.00 365
1987 JADOIL INC D VERNAU 343.00 312.00 145
1989 JADOIL INC D VERNAU 0.00 150.00 125
1990 KENOIL LLC 0.00 69.00 365
1991 KENOIL LLC 0.00 138.00 365
2014 NATIONAL ENERGY EXP INC 0.00 0.00 180
2016 NATIONAL ENERGY EXP INC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 JADOIL INC D VERNAU Brine 0 0
1985 JADOIL INC D VERNAU Brine 649 365
1986 JADOIL INC D VERNAU Brine 130 365
1987 JADOIL INC D VERNAU Brine 235 145
1989 JADOIL INC D VERNAU Brine 160 125
1990 KENOIL LLC Brine 160 365
1991 KENOIL LLC Brine 40 365
2014 NATIONAL ENERGY EXP INC Brine 400 180
2016 NATIONAL ENERGY EXP INC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1057334830 2016-12-20 0:00 PB No Violations 0.50
-1264736847 2017-1-4 0:00:0 PB No Violations 0.50
-159165400 2011-8-17 0:00: DD No Violations
-1623770479 2011-8-11 0:00: DD No Violations
-1707871797 2011-5-31 0:00: PW No Violations 0.50
-543510843 2011-5-4 0:00:0 DD No Violations 0.50
0000001772 Final Restoration No Violations PASSED WITNESSED INSPECTOR DATE 00/0019/00 DATA FROM OLD VAX INFO
0002694491 2011-05-31 Drill / Deepen / Reopen No Violations An inspection of drilling rig status revealed no activity or personnel at well location.
0125006685 2011-10-17 Drill / Deepen / Reopen No Violations An inspection of drilling operation revealed no activity or personnel.
0159165400 2011-08-17 Drill / Deepen / Reopen No Violations An inspection of drilling operations revealed H&D Drilling attempting to run 6 (OD)/5.63 (ID) casing, but encountering an obstruction in the wellbore 80 off bottom. Joints have been welded together then placed in wellbore. Note: Records attached to the permit do not match well. The current well owner has obtained a well record from original well owner (Everett Oil). The well contains the following: 108 of 8 drive pipe; 660 of 7 casing; 2654 of 5.19 casing. Iron ball had been encountered at 160. The 7 casing had parted years ago when the well was plugged. A spear has been utilized but unable to retrieve 7 casing with iron ball. H&D will run bailer to compare depth of obstruction inside casing. The cement job scheduled for today has been cancelled.
0293286070 2011-09-10 Drill / Deepen / Reopen No Violations Reopen well. H&D Drilling ran 6 casing ran inside of old 7 casing. Cemenco cemented casing. Well circulated during cement job. Records show that 660 of 7 casing set in well when it was drilled. During plugging 400 was left in hole.
0543510843 2011-05-04 Drill / Deepen / Reopen No Violations An inspection revealed no activity or personnel at location.
1057334830 2016-12-20 Plug / Plug Back No Violations I witnessed plugging operations on this well today. Berry Well Service was contracted to plug well with cement. Refer to plug report for details. Time of inspection: 8:00 AM.
125006685 2011-10-17 0:00 DD No Violations
1264736847 2017-01-04 Plug / Plug Back No Violations Inspect location as a status check. The well has been plugged. The casing has been cut down and covered with soil. Location has been graded.
1324329600 2011-12-19 Drill / Deepen / Reopen No Violations An inspection of drilling operation revealed no activity or personnel.
1623770479 2011-08-11 Drill / Deepen / Reopen No Violations An inspection revealed no activity or personnel at the well location.
1690400862 2011-10-28 Drill / Deepen / Reopen No Violations An inspection of drilling operation revealed no activity or personnel.
1707871797 2011-05-31 Production Wells No Violations Accompanied Brent Bear on inspection.
1772 FR No Violations
2694491 2011-5-31 0:00: DD No Violations 0.50
293286070 2011-9-10 0:00: DD No Violations

For data sources see[8]

References