If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-089-23256 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.02,"lon":-82.23,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Hopewell Township | |
Operator Name: NATIONAL ENERGY EXP INC | |
Well Pad ID: | |
Farm/Lease Name: SFORZA LARRY L | |
License Status: Plugged and Abandoned | |
License Date: 2016-11-14 | |
Spud Date: 1975-11-15 | |
Spud Drilling Contractor: | |
Final Drill Date: 1975-12-19 | |
Well Total Depth: 2897.00 ft | |
Configuration: Vertical | |
Latitude: 40.020000 | |
Longitude: -82.230000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1975-11-14 | 627 KENOIL GeoDate 11/14/75 |
Original Spud | 1975-11-15 | |
Completed | 1975-12-19 | |
Reached Total Depth | 1975-12-19 | |
CO | 1990-12-04 | 627 KENOIL GeoDate 12/4/90 |
COMBINATION WELL | 1990-12-04 | Issued Date 12/4/90 Expired Date 12/4/91 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date 1/7/91 |
APP | 2010-05-28 | Proposed Formations:CLINTON, Issued Date:5/28/2010, Expired Date:5/28/2011 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Completion Report Received | 2016-11-03 | |
APP | 2016-11-14 | Proposed Formations:CLINTON SAND, Issued Date:11/14/2016, Expired Date:11/14/2017 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-12-20 | |
Record Last Modified | 2017-05-25 | |
Construction Permit Expires | 2017-11-14 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2200 Bbl | 20000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | JADOIL INC D VERNAU | 258.00 | 202.00 | 0 |
1985 | JADOIL INC D VERNAU | 270.00 | 286.00 | 365 |
1986 | JADOIL INC D VERNAU | 567.00 | 380.00 | 365 |
1987 | JADOIL INC D VERNAU | 343.00 | 312.00 | 145 |
1989 | JADOIL INC D VERNAU | 0.00 | 150.00 | 125 |
1990 | KENOIL LLC | 0.00 | 69.00 | 365 |
1991 | KENOIL LLC | 0.00 | 138.00 | 365 |
2014 | NATIONAL ENERGY EXP INC | 0.00 | 0.00 | 180 |
2016 | NATIONAL ENERGY EXP INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | JADOIL INC D VERNAU | Brine | 0 | 0 |
1985 | JADOIL INC D VERNAU | Brine | 649 | 365 |
1986 | JADOIL INC D VERNAU | Brine | 130 | 365 |
1987 | JADOIL INC D VERNAU | Brine | 235 | 145 |
1989 | JADOIL INC D VERNAU | Brine | 160 | 125 |
1990 | KENOIL LLC | Brine | 160 | 365 |
1991 | KENOIL LLC | Brine | 40 | 365 |
2014 | NATIONAL ENERGY EXP INC | Brine | 400 | 180 |
2016 | NATIONAL ENERGY EXP INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1057334830 | 2016-12-20 0:00 | PB | No Violations | 0.50 |
-1264736847 | 2017-1-4 0:00:0 | PB | No Violations | 0.50 |
-159165400 | 2011-8-17 0:00: | DD | No Violations | |
-1623770479 | 2011-8-11 0:00: | DD | No Violations | |
-1707871797 | 2011-5-31 0:00: | PW | No Violations | 0.50 |
-543510843 | 2011-5-4 0:00:0 | DD | No Violations | 0.50 |
0000001772 | Final Restoration | No Violations | PASSED WITNESSED INSPECTOR DATE 00/0019/00 DATA FROM OLD VAX INFO | |
0002694491 | 2011-05-31 | Drill / Deepen / Reopen | No Violations | An inspection of drilling rig status revealed no activity or personnel at well location. |
0125006685 | 2011-10-17 | Drill / Deepen / Reopen | No Violations | An inspection of drilling operation revealed no activity or personnel. |
0159165400 | 2011-08-17 | Drill / Deepen / Reopen | No Violations | An inspection of drilling operations revealed H&D Drilling attempting to run 6 (OD)/5.63 (ID) casing, but encountering an obstruction in the wellbore 80 off bottom. Joints have been welded together then placed in wellbore. Note: Records attached to the permit do not match well. The current well owner has obtained a well record from original well owner (Everett Oil). The well contains the following: 108 of 8 drive pipe; 660 of 7 casing; 2654 of 5.19 casing. Iron ball had been encountered at 160. The 7 casing had parted years ago when the well was plugged. A spear has been utilized but unable to retrieve 7 casing with iron ball. H&D will run bailer to compare depth of obstruction inside casing. The cement job scheduled for today has been cancelled. |
0293286070 | 2011-09-10 | Drill / Deepen / Reopen | No Violations | Reopen well. H&D Drilling ran 6 casing ran inside of old 7 casing. Cemenco cemented casing. Well circulated during cement job. Records show that 660 of 7 casing set in well when it was drilled. During plugging 400 was left in hole. |
0543510843 | 2011-05-04 | Drill / Deepen / Reopen | No Violations | An inspection revealed no activity or personnel at location. |
1057334830 | 2016-12-20 | Plug / Plug Back | No Violations | I witnessed plugging operations on this well today. Berry Well Service was contracted to plug well with cement. Refer to plug report for details. Time of inspection: 8:00 AM. |
125006685 | 2011-10-17 0:00 | DD | No Violations | |
1264736847 | 2017-01-04 | Plug / Plug Back | No Violations | Inspect location as a status check. The well has been plugged. The casing has been cut down and covered with soil. Location has been graded. |
1324329600 | 2011-12-19 | Drill / Deepen / Reopen | No Violations | An inspection of drilling operation revealed no activity or personnel. |
1623770479 | 2011-08-11 | Drill / Deepen / Reopen | No Violations | An inspection revealed no activity or personnel at the well location. |
1690400862 | 2011-10-28 | Drill / Deepen / Reopen | No Violations | An inspection of drilling operation revealed no activity or personnel. |
1707871797 | 2011-05-31 | Production Wells | No Violations | Accompanied Brent Bear on inspection. |
1772 | FR | No Violations | ||
2694491 | 2011-5-31 0:00: | DD | No Violations | 0.50 |
293286070 | 2011-9-10 0:00: | DD | No Violations |
For data sources see[8]