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34-127-27298

Well Details

Well ID: 34-127-27298
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Country: United States
State: Ohio
County: Perry
Municipality: Bearfield Township
Operator Name: R C POLING CO INC
Well Pad ID:
Farm/Lease Name: MILLIGAN
License Status: Final Restoration
License Date: 2014-07-28
Spud Date: 2005-09-09
Spud Drilling Contractor: PROFESSIONAL WELL SVC-PWS
Final Drill Date: 2005-09-15
Well Total Depth: 4017.00 ft
Configuration: Vertical
Latitude: 39.710000
Longitude: -82.050000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2005-08-16 Proposed Formations:CLINTON, Issued Date:8/16/2005, Expired Date:8/16/2006 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
Original Spud 2005-09-09 RBDMS Rec
Completed 2005-09-15 RBDMS Rec
Reached Total Depth 2005-09-15 RBDMS Rec
Completion Report Received 2006-01-31 RBDMS Rec
APP 2008-09-02 Proposed Formations:BEREA, Issued Date:9/2/2008, Expired Date:9/2/2009 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
APP 2014-07-28 Proposed Formations:CLINTON, Issued Date:7/28/2014, Expired Date:7/27/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-10-07 RBDMS Rec
Construction Permit Expires 2016-07-27 RBDMS Rec
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-04-05 3844 3950 42
3844 3950 42
3844 3950 42

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 65000 Gal 25000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2006 R C POLING CO INC 2529.00 0.00 365
2007 R C POLING CO INC 1300.00 51.00 365
2008 R C POLING CO INC 0.00 0.00 365
2009 R C POLING CO INC 0.00 0.00 365
2010 R C POLING CO INC 0.00 0.00 365
2011 R C POLING CO INC 0.00 0.00 365
2012 R C POLING CO INC 0.00 0.00 366
2013 R C POLING CO INC 0.00 0.00 365
2014 R C POLING CO INC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2006 R C POLING CO INC Brine 736 365
2007 R C POLING CO INC Brine 315 365
2008 R C POLING CO INC Brine 0 365
2009 R C POLING CO INC Brine 0 365
2010 R C POLING CO INC Brine 0 365
2011 R C POLING CO INC Brine 0 365
2012 R C POLING CO INC Brine 0 366
2013 R C POLING CO INC Brine 0 365
2014 R C POLING CO INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2038267826 2007-9-14 0:00: PW No Violations
-276588928 2014-9-30 0:00: PB No Violations 3.00
-5206456 2014-10-7 0:00: PB No Violations 5.00
0005206456 2014-10-07 Plug / Plug Back No Violations I was onsite to witness the plugging of this well. The tubing was set at 1550ft for the first plug. We were unable to get the tubing back down to the Lime formation. After the pipe was shot off the hole caved in down the 5.5. We tried to wash the tubing down for 2days but only gained 120ft. We set a 250ft plug at 1550 then pulled out 250ft of pipe and set another 200ft plug to cover the Berea. The tubing was then pulled up to the bottom of the surface casing and a 200ft plug was set. The tubing was then pulled up to set the 200ft surface plug. The cement stayed at the surface with no signs of settling. The well is now plug.
0141107473 2007-07-20 Drill / Deepen / Reopen No Violations Follow-up on NOV, Non-Compliance, will issue the company a letter explaining the violation and failure to comply with NOV.
0276588928 2014-09-30 Plug / Plug Back No Violations Kenny Wright has moved in on this well to plug it. They have pulled out the rods and tubing from the well. The tubing was tallied then ran back in to a depth of 3960ft to set the bottom plug. The tubing was then pulled back out so they could get set up to rip the 5.5
1127134624 2005-09-12 Drill / Deepen / Reopen No Violations Checked drlg rig
1153857737 2015-06-11 Plug / Plug Back No Violations I returned to this well to do the final restoration on it. I was not able to pass the final restoration because the wellhead has not been cut off. I called Dick Poling and left a message for him to call me back. I will let him know this still needs to be done.
141107473 2007-7-20 0:00: DD No Violations
1412339824 2014-10-03 Plug / Plug Back No Violations I was onsite to witness the plugging of this well. The rig crew had to run the tubing back down to the Lime to set the plug. They were unable to get the tubing down to the lime so they had Formation Cementing hook up to the tubing and try to wash the pipe down. The tubing would not wash down. They are shutting down for the day and will try to clean up the hole on Monday. We talked about possibly bringing out a mud pump and power swivel.
1412774879 2014-10-07 Plug / Plug Back No Violations I received a request from inspector Justin Smith. I was asked to cover this plug job. Formation Cementing on location setting the plugs. I witnessed the lime/isolation plug and the bottom of surface plugs. Inspector Smith will fill out the plugging report.
1442094995 2007-05-31 Drill / Deepen / Reopen Violations Noted An inspection of the well revealed the Preliminary Restoration does not meet the 1509.072 requirements, lease road and well site need restored.
1521582996 2015-10-21 Final Restoration No Violations The final restoration meets 1509.072B.
1800714726 2007-10-19 Preliminary Restoration No Violations Restoration meets 1509.072(A) requirements.
2038267826 2007-09-14 Production Wells No Violations Follow-up on NOV, In-Compliance.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1442094995 US-OH-112850 2007-05-31 Failure to restore land surface within 9 mos. (CHANGE) (REPLACE)

For data sources see[9]

References