If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-121-24507 |
County: |
Municipality: |
Operator Name: |
Well Pad ID: |
Farm/Lease Name: |
First Permit Date: |
Last Permit Date: |
Spud Date: |
Unconventional: |
Horizontal: |
Producing: |
Violations: |
Latitude: |
Longitude: |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-1287043149 | 2014-07-14 | I am onsite to witness the cementing operations of the conductor casing string. Express energy ran 100' of twenty-six inch weld casing. Express also cemented the casing in place with 330 sacks of class A cement. I witnessed twenty barrels of cement return to surface. | ||||
1164043278 | 2014-07-15 | My inspection to day finds Express Energy Services has drilled a 32' hole to a depth of 100'. They then ran 100' of 26" 98 pound casing. Allied Oil and Gas Services cemented the casing in place with 330 sacks of class A cement. I witnessed good cement returns to surface. | ||||
1408578897 | 2014-08-20 | I am onsite to witness the surface casing cementing operations. I tested the mix water with a low range Quantab which indicated the total chlorides were at 37 ppm. Dallas Morris 24 ran 371' of 18.625" casing. Allied Oil and Gas Services circulated 730 sacks of class A cement into place. The casing was pressured up to 800 pounds and lost only five percent. |