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Well ID: 34-121-22794 |
County: |
Municipality: |
Operator Name: |
Well Pad ID: |
Farm/Lease Name: |
First Permit Date: |
Last Permit Date: |
Spud Date: |
Unconventional: |
Horizontal: |
Producing: |
Violations: |
Latitude: |
Longitude: |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1938540912 | 2012-05-29 | Inspection of the well found the following equipment -8.625 surface casing -4.5 production casing -1.5 tubing with the production valves open . A single 100 barrel tank -separator and gas meter are present in an established dike .Inspector will note well leaking gas from tubing slips and ID needs refreshed, will call company and ask for corrective action. | ||||
1340882571 | 2012-06-28 | Follow up on verbal request to properly identify well and repair gas leak at well head. Proper identification has been erected and attempt has been made to stop gas leak. | ||||
2085155387 | 2014-02-24 | My inspection finds the well appears to be shut in. The well is equipped to be produced by a plunger lift system. The tank battery is comprised of one 100 bbl tank, a separator, and a meter. | ||||
PL7765 | Preliminary Restoration done information from Data Point |