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34-119-25737

Well Details

Well ID: 34-119-25737
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-12-15
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.087080375
Longitude: -82.1744740543

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1179186610 2011-07-18 Phil Moran called and stated that they placed a 350' clay plug in and then ripped the 4.5" casing at 2450'. I did not witness this activity. The clay plug would have been from 2786'-2436'.
-1790408168 2011-07-22 Stopped at the well site and found cement level down 15'. Moran will let set and top off.
-504133228 2011-07-19 Moran had set 350' clay plug at 2786'-2436' in 4.5' casing and then ripped 4.5" casing at 2450'. Pulled up to 900.8'. Cemenco set cement plug at 900'-700'. Pulled 4.5" casing out. The 8 5/8" head was loose. Will spear casing tomorrow.
-59479903 2011-07-15 Moran Drilling called and said that packer would not come out. The 2 3/8" tubing is good, so placed the cement plug thru it and spotted a 200' plug on bottom. Then Jet Wireline shot the tubing off at 2786'.
-703266861 2011-07-21 Rig is pulling 8 5/8" casing. Will check back tomorrow.
1822713130 2008-04-18 Honda engine on well now. Producing.
35623379 2003-09-15
788698638 2011-12-28 Final Restoration passed on 12-28-11 by Patrick Shreve.
PL8700 Preliminary Restoration done information from Data Point