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34-119-25737

Well Details

Well ID: 34-119-25737
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Country: United States
State: Ohio
County: Muskingum
Municipality: Licking Township
Operator Name: KING PETROLEUM 2
Well Pad ID:
Farm/Lease Name: TURNER
License Status: Final Restoration
License Date: 2010-10-28
Spud Date: 1982-12-15
Spud Drilling Contractor: CO TOOLS
Final Drill Date:
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 40.080000
Longitude: -82.170000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1982-06-24 368 K-B OIL CO GeoDate 6/24/82
Oil and Gas 1982-06-24 Issued Date 6/24/82 Expired Date 12/15/82 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1982-12-15 RI CHG IN OWNER 6/26/1982 PERMIT EXPIRED
Change of Owner 1999-08-13 Operator changed from 368, K-B OIL CO to 5425, GINGERICH MIKE
Change of Owner 2002-10-28 Operator changed from 5425, GINGERICH MIKE to 1493, KING PETROLEUM
APP 2010-10-28 Proposed Formations:CLINTON, Issued Date:10/28/2010, Expired Date:10/27/2012 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2011-07-22 RI CHG IN OWNER 6/26/1982 PERMIT EXPIRED
Construction Permit Expires 2012-10-27 RI CHG IN OWNER 6/26/1982 PERMIT EXPIRED
Record Last Modified 2015-09-24 RI CHG IN OWNER 6/26/1982 PERMIT EXPIRED

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1999 GINGERICH MIKE 0.00 416.00 365
2000 GINGERICH MIKE 0.00 159.00 365
2003 KING PETROLEUM 2 0.00 0.00 0
2004 KING PETROLEUM 2 0.00 0.00 0
2005 KING PETROLEUM 2 0.00 0.00 0
2006 KING PETROLEUM 1 0.00 0.00 52
2007 KING PETROLEUM 2 0.00 0.00 0
2008 KING PETROLEUM 2 0.00 0.00 0
2009 KING PETROLEUM 2 0.00 0.00 60
2010 KING PETROLEUM 2 0.00 87.00 204
2011 KING PETROLEUM 2 0.00 42.00 160

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1999 GINGERICH MIKE Brine 0 365
2000 GINGERICH MIKE Brine 100 365
2003 KING PETROLEUM 2 Brine 0 0
2004 KING PETROLEUM 2 Brine 0 0
2005 KING PETROLEUM 2 Brine 0 0
2006 KING PETROLEUM 1 Brine 40 52
2007 KING PETROLEUM 2 Brine 0 0
2008 KING PETROLEUM 2 Brine 0 0
2009 KING PETROLEUM 2 Brine 60 60
2010 KING PETROLEUM 2 Brine 160 204
2011 KING PETROLEUM 2 Brine 160 160

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1179186610 2011-7-18 0:00: PB No Violations
-1790408168 2011-7-22 0:00: PB No Violations 2.00
-504133228 2011-7-19 0:00: PB No Violations 3.00
-59479903 2011-7-15 0:00: PB No Violations 4.00
-703266861 2011-7-21 0:00: PB No Violations 1.00
0000PL8700 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0035623379 2003-09-15 Production Wells No Violations
0059479903 2011-07-15 Plug / Plug Back No Violations Moran Drilling called and said that packer would not come out. The 2 3/8 tubing is good, so placed the cement plug thru it and spotted a 200 plug on bottom. Then Jet Wireline shot the tubing off at 2786.
0504133228 2011-07-19 Plug / Plug Back No Violations Moran had set 350 clay plug at 2786-2436 in 4.5 casing and then ripped 4.5 casing at 2450. Pulled up to 900.8. Cemenco set cement plug at 900-700. Pulled 4.5 casing out. The 8 5/8 head was loose. Will spear casing tomorrow.
0703266861 2011-07-21 Plug / Plug Back No Violations Rig is pulling 8 5/8 casing. Will check back tomorrow.
0788698638 2011-12-28 Final Restoration No Violations Final Restoration passed on 12-28-11 by Patrick Shreve.
1179186610 2011-07-18 Plug / Plug Back No Violations Phil Moran called and stated that they placed a 350 clay plug in and then ripped the 4.5 casing at 2450. I did not witness this activity. The clay plug would have been from 2786-2436.
1790408168 2011-07-22 Plug / Plug Back No Violations Stopped at the well site and found cement level down 15. Moran will let set and top off.
1822713130 2008-04-18 Production Wells No Violations Honda engine on well now. Producing.
35623379 2003-9-15 0:00: PW No Violations
788698638 2011-12-28 0:00 FR No Violations 1.00
PL8700 PL No Violations

For data sources see[7]

References