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34-031-27213

Well Details

Well ID: 34-031-27213
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-04-23
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.1914865699
Longitude: -82.1743487321

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1042728460 2013-05-22 On the day of my inspection Wheeler Drilling was drilling at a depth of 2570' with a 6.5" bit. The permit was on location, the pit liner was in good shape and there were no leaks or spills.
-1346138494 2013-08-19 On the day of my inspection I found that the location had been graded out and seeded, but there was no grass growth. All drilling equipment and debris had been removed from the site. The well head was equipped with a pumping unit. There were no leaks or spills and there were some signs of erosion. This site does not pass preliminary restoration.
-1461789560 2013-06-05 On the day of my inspection Wheeler Drilling was drilling at a depth of 2900' with a 6.5" bit. The permit was on location, the pit liner was in good shape and there were no leaks or spills.
-1535961641 2013-05-16 On the day of my inspection I found that Wheeler Drilling was drilling at a depth of 2150' on a 6.5" bit. The permit was on display, the pit liner was in good shape and there were no leaks or spills.
-2055248991 2013-10-29 On the day of my inspection I found that all drilling equipment and materials had been removed from the location. The drill site was graded out and approximately 90% covered with well established short grass vegetation. This site passes preliminary restoration.
-755566374 2013-04-30 On the day of my inspection Jet Wireline Services ran a bond log on the surface casing. The log showed that the cement top was at approximately 58'. Wheeler Drilling filled the annular space to surface with 700 lbs of sack cement. They were approved to continue drilling operations.
1239829635 2013-04-15 On the day of my inspection I found that Mike Wheeler was excavating the location. There was no drilling equipment on location. The drilling pit was not constructed.
1366739047 2013-04-23 On the day of my inspection I found that Wheeler Drilling had just set 61' of 11.75" drive pipe. They were drilling at a depth of 70' on a 10.875" bit. The permit was on display, the pit liner was in good shape and there were no leaks or spills.
1367277091 2013-04-29 On the day of my inspection Wheeler Drilling ran used, tested 8.625" casing to 515'. Cemenco pumped 40 barrels of water, 500 lbs of gel and 166 sacks of class A cement. Circulation was never established. Upon landing the plug Cemenco pressured up to 500 psi and held for 5 minutes with less than 10% bleed off. Mackenco will be required to run a bond log before resuming drilling operations.
1367277091 2013-04-29 On the day of my inspection Wheeler Drilling ran used, tested 8.625" casing to 515'. Cemenco pumped 40 barrels of water, 500 lbs of gel and 166 sacks of class A cement. Circulation was never established. Upon landing the plug Cemenco pressured up to 500 psi and held for 5 minutes with less than 10% bleed off. Mackenco will be required to run a bond log before resuming drilling operations.
1367868249 2013-05-06 On the day of my inspection I found that Wheeler Drilling had set 7" intermediate casing at 983'. They were drilling at a depth of 1000' on a 6.5" bit. The permit was on display, the pit liner was in good shape and there were no leaks or spills.
1371652842 2013-06-19 On the day of my inspection I found that Wheeler Drilling lost the tools and 1700' of drilling line down hole. The 4.5" casing had been set at 3123' and the open hole had been drilled to 3165'. The drilling crew was in the process of equipping the rig with new drilling cable to begin fishing for the lost tools.
816977276 2013-06-25 On the day of my inspection I found that Wheeler Drilling was successful at recovering their lost tools. Producers was on location to frac the well. There were no significant pressure changes and I observed no leaks or spills.