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Well ID: 34-059-24395 | Loading map...
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Spud Date: 2014-07-03 | |
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Producing: No | |
Violations: 0 | |
Latitude: 40.0435999585 | |
Longitude: -81.3810879386 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1650802951 | 2014-07-29 | On the day of my inspection accompanied by ODNR Southeast Regional Supervisor Rocky King, I met with Company Man Randall Downen and discussed upcoming surface string and cementing. First Class Drilling Rig #6 was drilling a 24 inch diameter hole on air at 103 feet with a planned td of 544 feet. | ||||
-1853968162 | 2014-07-30 | I accompanied Doug Bennett on the inspection of this well today. | ||||
1779677126 | 2014-07-30 | On the day of my inspection accompanied by ODNR Inspector Justin Smith, I witnessed that First Class Drilling Rig #6 had drilled a 24 inch diameter surface hole to the depth of 544 feet and ran 544 feet of 20 inch 94#/ft. casing and had to wash down the last 5 feet . Universal Well Services was on site and gained circulation with 25bbls of gel, 5bbls of fresh water and cemented casing with 706 sacks of Type 1 cement with 3% CaCl and .25#/sk. of cello flake. While dropping the plug they believed it kicked sideways so the cement was displaced with 183bbls of fresh water. Had good cement returns of 35bbls to surface and no pressure test was performed. Cement head was shut in and they were instructed to leave shut in for 8 hours and complete pressure test. |