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34-115-23436

Well Details

Well ID: 34-115-23436
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1984-10-26
Unconventional:
Horizontal:
Producing: No
Violations: 8
Latitude: 39.5969113942
Longitude: -81.6085840622

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1678809421 2013-04-25 Compliance Action Follow-Up 1353350156: Well is still sitting shut in. There has been no resolution to the well issues yet at this time.
-1788142147 2009-04-15 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2" casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery. 9-9-05(A)1
-1788142147 2009-04-15 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2" casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery. 9-9-05(A)8
-1788142147 2009-04-15 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2" casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery. 9-9-05(A)9
-1788142147 2009-04-15 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2" casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery. NONE E
-1815170689 2013-12-19 Compliance Action Follow-Up 1353350156: Alva Heiss called and asked me to inspect the well. Well is still shut in at location. There has been no resolution to the well issues yet at this time. John Schneider has been notified of this well.
-2137131345 2014-05-20 Compliance Action Follow-Up 1353350156: The well is still shut in and the equipment is still broken and disconnected in places. The nipple on the tank is starting to leak.
-502361126 2009-12-07 Follow-up on NOV, Non-Compliance. Well is still idle, no chart on meter. Appears well has H2S, production casing has corrosion. Took photos of well.
-902734341 2007-07-02 Well has been plugged back and placed back into production recently,well is equipped with tubing&rods and punpjack and 1-100 bbl tank.Resolving previous NOV and Chief's Order.
1005587516 2009-04-15 FOLLOW UP TO NOV # -1788142147 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2" casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva
1164405998 2006-11-22 Well has been plugged back to Oriskany Sand resolving previous NOV and Chiefs order.
1306912354 2009-04-15 FOLLOW UP TO NOV # -1788142147 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2" casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery.
1332332954 2012-03-15 My inspection this day is routine - I found well to be incapable of production. The well is equipped with pumping unit with all valves shut and polish rod rusty. The well is giving off slight H2S odor. The well and tank are both fenced. The tank has good identification, fair dike and a chart with no date - it is not moving and no marks are on it. This well was issued a violation in 4/09 - an inspection in 12/09 shows the well still idle yet company has turned in production for that year and 2010. Pictures taken.
1336155018 2012-05-04 I received a call from Alva Heiss, landowner, about idle wells with H2S. He says wells have not produced in years, that they have H2S on them, and he has NEVER received royalty payments. Having just inspected this well, I told him what I found. He says he just wants the wells plugged. I explained his options and suggested he have lawyer break the lease - that would be the quickest way to get the wells plugged. He agreed.
1353350156 2012-11-19 I received a call from Alva Heiss concerning H2S producing well. Upon inspection, I found well to be incapable of production. The well is equipped with pumping unit and all valves shut. The polish rod rusty. The well has H2S corrosion/scaling and is giving off slight H2S odor, however the gas meter did not pick up any H2S. The well and tank are both fenced, and the tank has no legible identification. There is a meter box with a chart dated Sept. 15 - it is not moving and no marks are on it. This well was issued a violation in 4/09 - an inspection in 12/09 shows the well still idle yet company has turned in production for 2009-2012. Landowner has stated the well has never produced gas during these years. Pictures taken. Stonebridge shall plug well. Failure to comply may result in forfeiture of bond. 9-1-03C
1353350156 2012-11-19 I received a call from Alva Heiss concerning H2S producing well. Upon inspection, I found well to be incapable of production. The well is equipped with pumping unit and all valves shut. The polish rod rusty. The well has H2S corrosion/scaling and is giving off slight H2S odor, however the gas meter did not pick up any H2S. The well and tank are both fenced, and the tank has no legible identification. There is a meter box with a chart dated Sept. 15 - it is not moving and no marks are on it. This well was issued a violation in 4/09 - an inspection in 12/09 shows the well still idle yet company has turned in production for 2009-2012. Landowner has stated the well has never produced gas during these years. Pictures taken. Stonebridge shall plug well. Failure to comply may result in forfeiture of bond. 9-9-05(A)1
1353350156 2012-11-19 I received a call from Alva Heiss concerning H2S producing well. Upon inspection, I found well to be incapable of production. The well is equipped with pumping unit and all valves shut. The polish rod rusty. The well has H2S corrosion/scaling and is giving off slight H2S odor, however the gas meter did not pick up any H2S. The well and tank are both fenced, and the tank has no legible identification. There is a meter box with a chart dated Sept. 15 - it is not moving and no marks are on it. This well was issued a violation in 4/09 - an inspection in 12/09 shows the well still idle yet company has turned in production for 2009-2012. Landowner has stated the well has never produced gas during these years. Pictures taken. Stonebridge shall plug well. Failure to comply may result in forfeiture of bond. 9-9-05(A)10
1353350156 2012-11-19 I received a call from Alva Heiss concerning H2S producing well. Upon inspection, I found well to be incapable of production. The well is equipped with pumping unit and all valves shut. The polish rod rusty. The well has H2S corrosion/scaling and is giving off slight H2S odor, however the gas meter did not pick up any H2S. The well and tank are both fenced, and the tank has no legible identification. There is a meter box with a chart dated Sept. 15 - it is not moving and no marks are on it. This well was issued a violation in 4/09 - an inspection in 12/09 shows the well still idle yet company has turned in production for 2009-2012. Landowner has stated the well has never produced gas during these years. Pictures taken. Stonebridge shall plug well. Failure to comply may result in forfeiture of bond. NONE
1353424677 2012-11-19 I accompanied Jake Glascock on a request for inspection of a possible H2S well. We met with the landowner Alva Heiss, he showed us this well, using our gas meters, no H2S was found. Mr. Heiss had us look at 4 other wells on his property, Jake has written reports on these wells.
1366900023 2013-04-25 Compliance Action Follow-Up 1353350156: I received another call from Landowner Alva Heiss and he wants resolution of the compliance actions. I called and left another message with John Schneider of Stonebridge. I also called the well tender Dave Crippen and he stated he would let his superiors know of the issues.
1392048797 2014-02-10 Compliance Action Follow-Up 1353350156: The well is still idle and equipment is still disconnected and shut off at various points. The separator is not functional and the flow line to the tank is rusted off at the top. The tank is almost full, and there is still an old chart in meter box. The well location is equipped with pumpjack and there was a strong odor of sour gas. There has been no resolution to any of the issues.
1395326800 2014-03-20 Compliance Action Follow-Up 1353350156: The well is still idle and equipment is still disconnected and shut off at various points. There has been no resolution to any of the issues.
1403719604 2014-06-25 Rob Nutter of Stonebridge called and stated that they went over and drained the entire tank with a brine truck.
1999462834 2006-11-09 On site to witness setting of bottom hole plug set through 2" tubing set at 5550' cemented with 30 sk. Estimated top of plug@5150'
2037205897 2006-07-27 A.D. not hooked up well is still idle,called and left messages on pumpers cell phone with no reply.Recommend that a CHIEF'S ORDER TO PLUG said well be issued.
673625031 2006-04-27 Upon receiving complaint from landowner Alva Heiss found well to be idle no I.D. posted all valves at wellhead are shut old tubing head&misc fitting strung about site,well is equipped with 8" surface casing 4.5" production casing&2.375 tubing well has not produced for quite sometime,1-100 bbl tank (no dike) suspect hole in bottom of tank!
769928190 2014-01-23 Compliance Action Follow-Up 1353350156: Alva Heiss called me and stated he has just received a document from Morgan County stating he needs to pay taxes on received oil and gas royalties for the two Stonebridge wells on his property. He said this was the first time he has ever received a tax statement and that he has never received royalties for these wells from Stonebridge.
854698054 2014-04-04 Compliance Action Follow-Up 1353350156: The well is still idle and equipment is still disconnected and shut off at various points. There has been no resolution to any of the issues.
967255302 2013-11-04 Compliance Action Follow-Up 1353350156: Well is still sitting shut in. There has been no resolution to the well issues yet at this time. John Schneider has been notified of this well.
PL9592 Preliminary Restoration done information from Data Point