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Well ID: 34-115-23436 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Center Township | |
Operator Name: STONEBRIDGE OPERATING CO LLC | |
Well Pad ID: | |
Farm/Lease Name: HUPP G | |
License Status: Final Restoration | |
License Date: 2015-12-23 | |
Spud Date: 1984-10-26 | |
Spud Drilling Contractor: BURDETTE DRLG | |
Final Drill Date: 1984-10-31 | |
Well Total Depth: 5756.00 ft | |
Configuration: Vertical | |
Latitude: 39.590000 | |
Longitude: -81.600000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1983-12-16 | 631 BT ENERGY CORP GeoDate 12/16/83 |
Oil and Gas | 1983-12-16 | Issued Date 12/16/83 Expired Date 6/13/84 Acres 0040000 Tool Type CRAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1984-06-19 | 631 BT ENERGY CORP GeoDate 6/19/84 |
Oil and Gas | 1984-06-19 | Issued Date 6/19/84 Expired Date 12/16/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05756 Proposed Drill Depth 05756 |
Original Spud | 1984-10-26 | R.I. 6-23-84 |
Completed | 1984-10-31 | R.I. 6-23-84 |
Reached Total Depth | 1984-10-31 | R.I. 6-23-84 |
Completion Report Received | 1984-11-19 | R.I. 6-23-84 |
APP | 2006-09-18 | Proposed Formations:BEREA THRU BASS ISLAND, Issued Date:9/18/2006, Expired Date:9/18/2007 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:TAAD, Proposed Well Class:ENPW |
Plugged Back | 2006-11-22 | R.I. 6-23-84 |
Change of Owner | 2007-10-12 | Operator changed from 631, BT ENERGY CORP to 2070, STONEBRIDGE OPERATING CO |
Last Compliance Report | 2007-11-08 | R.I. 6-23-84 |
APP | 2015-12-23 | Proposed Formations:MEDINA, Issued Date:12/23/2015, Expired Date:12/22/2017 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class: |
Plugged/Abandoned | 2016-02-18 | R.I. 6-23-84 |
Record Last Modified | 2017-05-20 | R.I. 6-23-84 |
Construction Permit Expires | 2017-12-22 | R.I. 6-23-84 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5516 | 5578 | 0 |
5516 | 5578 | 0 | |
2006-09-11 | 5532 | 5642 | 12 |
5532 | 5642 | 12 | |
5516 | 5578 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 800 Bbl | 90000 | FRAC: H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BT ENERGY CORP | 0.00 | 0.00 | 365 |
1985 | BT ENERGY CORP | 5820.00 | 0.00 | 365 |
1986 | BT ENERGY CORP | 6201.00 | 0.00 | 365 |
1987 | BT ENERGY CORP | 7083.00 | 0.00 | 365 |
1988 | BT ENERGY CORP | 5751.00 | 0.00 | 365 |
1989 | BT ENERGY CORP | 3268.00 | 0.00 | 365 |
1990 | BT ENERGY CORP | 2819.00 | 0.00 | 365 |
1991 | BT ENERGY CORP | 1709.00 | 0.00 | 365 |
1993 | BT ENERGY CORP | 1679.00 | 0.00 | 365 |
1994 | BT ENERGY CORP | 1299.00 | 0.00 | 365 |
1995 | BT ENERGY CORP | 1193.00 | 0.00 | 56 |
1996 | BT ENERGY CORP | 363.00 | 0.00 | 70 |
1997 | BT ENERGY CORP | 0.00 | 0.00 | 70 |
1998 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 0 |
2000 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 364 |
2001 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 0 |
2002 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
2003 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
2004 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
2005 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
2006 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
2007 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 63 |
2008 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 336 |
2009 | STONEBRIDGE OPERATING CO LLC | 23.00 | 0.00 | 7 |
2010 | STONEBRIDGE OPERATING CO LLC | 50.00 | 0.00 | 287 |
2011 | STONEBRIDGE OPERATING CO LLC | 108.00 | 0.00 | 0 |
2012 | STONEBRIDGE OPERATING CO LLC | 80.00 | 0.00 | 0 |
2013 | STONEBRIDGE OPERATING CO LLC | 109.00 | 0.00 | 0 |
2014 | STONEBRIDGE OPERATING CO LLC | 41.00 | 0.00 | 112 |
2015 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 0 |
2016 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1036040580 | 2015-8-18 0:00: | PW | No Violations | 1.00 |
-1369846762 | 2015-7-20 0:00: | PW | No Violations | 1.50 |
-1678809421 | 2013-4-25 0:00: | PW | No Violations | 1.40 |
-1788142147 | 2009-4-15 0:00: | AD | No Violations | |
-1815170689 | 2013-12-19 0:00 | PW | No Violations | 0.30 |
-2037514489 | 2014-9-24 0:00: | AM | No Violations | |
-2137131345 | 2014-5-20 0:00: | PW | No Violations | |
-22038369 | 2014-9-23 0:00: | AM | No Violations | |
-502361126 | 2009-12-7 0:00: | AD | No Violations | |
-902734341 | 2007-7-2 0:00:0 | AD | No Violations | |
0000PL9592 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0022038369 | 2014-09-23 | Administrative Inspection | No Violations | The landowner has expressed concern over the smell of H2S. At the time of inspection the well casing was found to have H2S corrosion/scaling. There has been a strong smell of H2S during previous inspections. The landowner was present and stated that noone has been out to the well. |
0445217890 | 2009-04-15 | Annular Disposal | No Violations | FOLLOW UP TO NOV # 1306912354 FOLLOW UP TO NOV # -1788142147 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2 casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery. |
0502361126 | 2009-12-07 | Annular Disposal | No Violations | Follow-up on NOV, Non-Compliance. Well is still idle, no chart on meter. Appears well has H2S, production casing has corrosion. Took photos of well. |
0673625031 | 2006-04-27 | Annular Disposal | No Violations | Upon receiving complaint from landowner Alva Heiss found well to be idle no I.D. posted all valves at wellhead are shut old tubing head&misc fitting strung about site,well is equipped with 8 surface casing 4.5 production casing&2.375 tubing well has not produced for quite sometime,1-100 bbl tank (no dike) suspect hole in bottom of tank! |
0769928190 | 2014-01-23 | Administrative Inspection | No Violations | Compliance Action Follow-Up 1353350156: Alva Heiss called me and stated he has just received a document from Morgan County stating he needs to pay taxes on received oil and gas royalties for the two Stonebridge wells on his property. He said this was the first time he has ever received a tax statement and that he has never received royalties for these wells from Stonebridge. |
0854698054 | 2014-04-04 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: The well is still idle and equipment is still disconnected and shut off at various points. There has been no resolution to any of the issues. |
0898262074 | 2014-09-16 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: The well is still shut in and the equipment is still broken and disconnected in places. |
0902734341 | 2007-07-02 | Annular Disposal | No Violations | Well has been plugged back and placed back into production recently,well is equipped with tubing&rods and punpjack and 1-100 bbl tank.Resolving previous NOV and Chiefs Order. |
0967255302 | 2013-11-04 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: Well is still sitting shut in. There has been no resolution to the well issues yet at this time. John Schneider has been notified of this well. |
1005587516 | 2009-04-15 | Annular Disposal | No Violations | FOLLOW UP TO NOV # -1788142147 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2 casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva |
1036040580 | 2015-08-18 | Production Wells | No Violations | I was on location to do a follow-up inspection on the well. There has been no change to the well. The well is still incapable of production and is still in violation. I took updated photos of the well during my inspection. |
1164405998 | 2006-11-22 | Plug / Plug Back | No Violations | Well has been plugged back to Oriskany Sand resolving previous NOV and Chiefs order. |
1306912354 | 2009-04-15 | Annular Disposal | No Violations | FOLLOW UP TO NOV # -1788142147 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2 casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery. |
1332332954 | 2012-03-15 | Production Wells | No Violations | My inspection this day is routine - I found well to be incapable of production. The well is equipped with pumping unit with all valves shut and polish rod rusty. The well is giving off slight H2S odor. The well and tank are both fenced. The tank has good identification, fair dike and a chart with no date - it is not moving and no marks are on it. This well was issued a violation in 4/09 - an inspection in 12/09 shows the well still idle yet company has turned in production for that year and 2010. Pictures taken. |
1336155018 | 2012-05-04 | Administrative Inspection | No Violations | I received a call from Alva Heiss, landowner, about idle wells with H2S. He says wells have not produced in years, that they have H2S on them, and he has NEVER received royalty payments. Having just inspected this well, I told him what I found. He says he just wants the wells plugged. I explained his options and suggested he have lawyer break the lease - that would be the quickest way to get the wells plugged. He agreed. |
1349979003 | 2009-04-15 | Annular Disposal | No Violations | FOLLOW UP TO NOV # 1005587516 FOLLOW UP TO NOV # -1788142147 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2 casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva |
1353350156 | 2012-11-19 | Production Wells | Violations Noted | I received a call from Alva Heiss concerning H2S producing well. Upon inspection, I found well to be incapable of production. The well is equipped with pumping unit and all valves shut. The polish rod rusty. The well has H2S corrosion/scaling and is giving off slight H2S odor, however the gas meter did not pick up any H2S. The well and tank are both fenced, and the tank has no legible identification. There is a meter box with a chart dated Sept. 15 - it is not moving and no marks are on it. This well was issued a violation in 4/09 - an inspection in 12/09 shows the well still idle yet company has turned in production for 2009-2012. Landowner has stated the well has never produced gas during these years. Pictures taken. Stonebridge shall plug well. Failure to comply may result in forfeiture of bond. |
1353424677 | 2012-11-19 | Production Wells | No Violations | I accompanied Jake Glascock on a request for inspection of a possible H2S well. We met with the landowner Alva Heiss, he showed us this well, using our gas meters, no H2S was found. Mr. Heiss had us look at 4 other wells on his property, Jake has written reports on these wells. |
1366900023 | 2013-04-25 | Administrative Inspection | No Violations | Compliance Action Follow-Up 1353350156: I received another call from Landowner Alva Heiss and he wants resolution of the compliance actions. I called and left another message with John Schneider of Stonebridge. I also called the well tender Dave Crippen and he stated he would let his superiors know of the issues. |
1369846762 | 2015-07-20 | Production Wells | No Violations | I went out to this well to do a follow-up inspection on it. The well still appears to be idle at this time. The valves are shut at the wellhead and and the tank pad making it incapable of selling any production. The pumping unit does not look like it is in operation. At the production tank the ladder is laying on its side on the ground. It is not hooked up to the production tank. There has been no change on putting the well back in production. I have taken pictures of my findings today for my records. |
1392048797 | 2014-02-10 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: The well is still idle and equipment is still disconnected and shut off at various points. The separator is not functional and the flow line to the tank is rusted off at the top. The tank is almost full, and there is still an old chart in meter box. The well location is equipped with pumpjack and there was a strong odor of sour gas. There has been no resolution to any of the issues. |
1395326800 | 2014-03-20 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: The well is still idle and equipment is still disconnected and shut off at various points. There has been no resolution to any of the issues. |
1403719604 | 2014-06-25 | Administrative Inspection | No Violations | Rob Nutter of Stonebridge called and stated that they went over and drained the entire tank with a brine truck. |
1427207613 | 2015-03-24 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: There has been no resolution to any of the issues. The well is still not in production. |
1486507241 | 2016-02-17 | Plug / Plug Back | No Violations | On location to witness plugging operations for this well. Matheny Well Services tagged the Big Lime plug at 3780, indicating a successful plug. 2.375 tubing was set to 1917 to set the bottom of surface casing plug. Formation Cementing pumped 60 bbls of freshwater and was unable to establish circulation. It was decided to set the 200 bottom of surface plug with 60 sks class A cement with 2% CaCl and 20 lbs LCM. Circulation was established briefly during the displacement of the plug, but was lost quickly. After waiting on cement for 2 hours, fluid level was gauged and found to be approximately 700 down, indicating the plug may have slid downhole or was absorbed by the Ohio Shale. The job was shut down for the day and the top of plug will be tagged on 2/18/16. |
1493728122 | 2017-05-02 | Final Restoration | No Violations | The final restoration meets 1509.072 (B) requirements. |
1678809421 | 2013-04-25 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: Well is still sitting shut in. There has been no resolution to the well issues yet at this time. |
1687640917 | 2009-04-15 | Annular Disposal | No Violations | FOLLOW UP TO NOV # -1788142147 An inspection of the well revealed H2S leaking from the well head packing. 4 1/2 casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery. |
1788142147 | 2009-04-15 | Annular Disposal | Violations Noted | An inspection of the well revealed H2S leaking from the well head packing. 4 1/2 casing has scaling & corrosion from the H2S. Well is capable of producing, no production reported to State since 1996. No house gas being used according to landowner (Alva Heiss 740-983-4747). No chart on gas meter, all equipment on well and tank battery. Need to rebuild dike around tank battery. |
1815170689 | 2013-12-19 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: Alva Heiss called and asked me to inspect the well. Well is still shut in at location. There has been no resolution to the well issues yet at this time. John Schneider has been notified of this well. |
1999462834 | 2006-11-09 | Annular Disposal | No Violations | On site to witness setting of bottom hole plug set through 2 tubing set at 5550 cemented with 30 sk. Estimated top of plug@5150 |
2037205897 | 2006-07-27 | Annular Disposal | No Violations | A.D. not hooked up well is still idle,called and left messages on pumpers cell phone with no reply.Recommend that a CHIEFS ORDER TO PLUG said well be issued. |
2037514489 | 2014-09-24 | Administrative Inspection | No Violations | Compliance Action Follow-Up 1353350156: Rob Nutter with Stonebridge called and stated they they are in the process of finalizing a deal with the landowern, Alva Heiss. Once they have come to an agreement then they can begin to service the wells. |
2049937731 | 2015-11-17 | Production Wells | No Violations | I returned to this well to do a follow-up inspection on it. The well is still currently sitting idle with no change in it being capable of production. The well is in violation. |
2137131345 | 2014-05-20 | Production Wells | No Violations | Compliance Action Follow-Up 1353350156: The well is still shut in and the equipment is still broken and disconnected in places. The nipple on the tank is starting to leak. |
445217890 | 2009-4-15 0:00: | AD | No Violations | |
673625031 | 2006-4-27 0:00: | AD | No Violations | |
769928190 | 2014-1-23 0:00: | AM | No Violations | |
854698054 | 2014-4-4 0:00:0 | PW | No Violations | 2.70 |
898262074 | 2014-9-16 0:00: | PW | No Violations | |
967255302 | 2013-11-4 0:00: | PW | No Violations | 0.20 |
PL9592 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1353350156 | US-OH-110221 | 2012-12-10 | Forfeiture of bond | |
1353350156 | US-OH-110222 | 2012-12-10 | Well insufficiently equipped to prevent escape of oil and gas | |
1353350156 | US-OH-110223 | 2012-12-10 | Failure to legibly identify well | |
1353350156 | US-OH-110224 | 2012-12-10 | Well shall be plugged | |
1788142147 | US-OH-117824 | 2009-04-17 | Well not equipped to prevent escape of oil and/or gas | |
1788142147 | US-OH-117825 | 2009-04-17 | Equipment pressure rated below operating pressure | |
1788142147 | US-OH-117826 | 2009-04-17 | No SPCC dike/or failure to keep dike free of water or oil | |
1788142147 | US-OH-117827 | 2009-04-17 | Well shall be plugged |
For data sources see[9]