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Well ID: 34-153-20558 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1977-03-04 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 2 | |
Latitude: 41.0422741342 | |
Longitude: -81.5378775791 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-616827636 | 2006-04-13 | The last reported production from this well was in 1995. The well must either be placed back in production or properly plugged and abandoned. Common tank battery with the Firestone #3 (P/N 824) and the Firestone #5 (P/N 826). | NONE | |||
-832407546 | 2007-07-21 | Arvilla attempted to unseat the packer and pull the tubing. The packer would not release and the tubing parted at 2485'. Arvilla ran another R-4 packer 30' into the hole to shut off the brine flow. Plugging activity will begin on Monday morning. | ||||
1185813528 | 2007-07-19 | I received a call from Richard Jones (330-697-3818) reporting an active brine spill behind the Firestone Polymer complex at 381 Wilbeth Road. The leak occurred in the 4-1/2" casing just above the 8-5/8" casing head. Plant employees noticed the leak earlier this morning. J&M Water Service and Kenmore Construction were on site to recover brine and dig a containment pit respectively. An Arvilla service rig should be on site Friday or Saturday. Plugging operations will commence as soon as the 2-3/8" tubing is removed. Brine continues to flow to surface and there appears to be communication with an abandoned Cargill salt solution mine cavern. | ||||
1439641202 | 2007-08-01 | The containment pit and the well have been closed and graded. Several trees have lost leaves and will checked later in the year to see if they refoliate. | ||||
1621563449 | 2007-07-20 | Arvilla will be on site late today and is planning on unseating the packer and recovering the 2-3/8" tubing on Saturday. The brine flow continues and is contained in the recovery pit. J&M will continue to haul water as necessary. | ||||
1680523426 | 2006-07-18 | Firestone is reported to be obtaining a plugging permit for this well. The plug or produce NOV is still open. | NONE | |||
1840488831 | 2013-07-23 | No indication of well equipment, access road, or tank battery. | ||||
211854467 | 2007-07-30 | Arvilla was on site to cut off the surface casing and place the ID plate on top. There was a small natural gas leak between the 4-1/2 and the 8-5/8 which will be monitored. The gas probably originates from the Ohio shale. Communication with the Cargill salt cavern has been controlled. The outstanding violation has been corrected. |