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Well ID: 34-153-20558 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: BRIDGESTONE/FIRESTONE INC | |
Well Pad ID: | |
Farm/Lease Name: FIRESTONE | |
License Status: Final Restoration | |
License Date: 2006-10-25 | |
Spud Date: 1977-03-04 | |
Spud Drilling Contractor: | |
Final Drill Date: 1977-03-15 | |
Well Total Depth: 3999.00 ft | |
Configuration: Vertical | |
Latitude: 41.040000 | |
Longitude: -81.530000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1977-01-05 | 1024 FIRESTONE TIRE & RUBBER GeoDate 1/5/77 |
Original Spud | 1977-03-04 | |
Completed | 1977-03-15 | |
Reached Total Depth | 1977-03-15 | |
CO | 1993-02-09 | 3745 BRIDGESTONE/FIRESTONE INC GeoDate 1/5/77 |
APP | 2006-10-25 | Proposed Formations:CLINTON, Issued Date:10/25/2006, Expired Date:10/25/2007 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2007-07-27 | |
Construction Permit Expires | 2007-10-25 | |
Record Last Modified | 2013-08-06 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3731 | 3801 | 12 |
3731 | 3801 | 12 | |
3731 | 3801 | 12 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 56000 Gal | 49000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | FIRESTONE TIRE & RUBBER | 2363.00 | 14.00 | 0 |
1985 | FIRESTONE TIRE & RUBBER | 1605.00 | 12.00 | 0 |
1986 | FIRESTONE TIRE & RUBBER | 1459.00 | 11.00 | 365 |
1987 | FIRESTONE TIRE & RUBBER | 1065.00 | 13.00 | 365 |
1988 | FIRESTONE TIRE & RUBBER | 917.00 | 10.00 | 365 |
1989 | FIRESTONE TIRE & RUBBER | 762.00 | 10.00 | 365 |
1990 | BRIDGESTONE/FIRESTONE INC | 903.00 | 9.00 | 365 |
1991 | BRIDGESTONE/FIRESTONE INC | 1190.00 | 7.00 | 365 |
1992 | BRIDGESTONE/FIRESTONE INC | 1505.00 | 3.00 | 365 |
1993 | BRIDGESTONE/FIRESTONE INC | 834.00 | 2.00 | 365 |
1994 | BRIDGESTONE/FIRESTONE INC | 818.00 | 0.00 | 365 |
1995 | BRIDGESTONE/FIRESTONE INC | 232.00 | 0.00 | 0 |
1997 | BRIDGESTONE/FIRESTONE INC | 0.00 | 0.00 | 0 |
1998 | BRIDGESTONE/FIRESTONE INC | 0.00 | 0.00 | 365 |
2003 | BRIDGESTONE/FIRESTONE INC | 0.00 | 0.00 | 365 |
2004 | BRIDGESTONE/FIRESTONE INC | 0.00 | 0.00 | 365 |
2005 | BRIDGESTONE/FIRESTONE INC | 0.00 | 0.00 | 365 |
2006 | BRIDGESTONE/FIRESTONE INC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | FIRESTONE TIRE & RUBBER | Brine | 86 | 0 |
1985 | FIRESTONE TIRE & RUBBER | Brine | 46 | 0 |
1986 | FIRESTONE TIRE & RUBBER | Brine | 40 | 365 |
1987 | FIRESTONE TIRE & RUBBER | Brine | 42 | 365 |
1988 | FIRESTONE TIRE & RUBBER | Brine | 28 | 365 |
1989 | FIRESTONE TIRE & RUBBER | Brine | 36 | 365 |
1990 | BRIDGESTONE/FIRESTONE INC | Brine | 37 | 365 |
1991 | BRIDGESTONE/FIRESTONE INC | Brine | 13 | 365 |
1992 | BRIDGESTONE/FIRESTONE INC | Brine | 3 | 365 |
1993 | BRIDGESTONE/FIRESTONE INC | Brine | 1 | 365 |
1994 | BRIDGESTONE/FIRESTONE INC | Brine | 1 | 365 |
1995 | BRIDGESTONE/FIRESTONE INC | Brine | 3 | 0 |
1997 | BRIDGESTONE/FIRESTONE INC | Brine | 0 | |
1998 | BRIDGESTONE/FIRESTONE INC | Brine | 0 | 365 |
2003 | BRIDGESTONE/FIRESTONE INC | Brine | 0 | 365 |
2004 | BRIDGESTONE/FIRESTONE INC | Brine | 0 | 365 |
2005 | BRIDGESTONE/FIRESTONE INC | Brine | 0 | 365 |
2006 | BRIDGESTONE/FIRESTONE INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-616827636 | 2006-4-13 0:00: | PW | No Violations | |
-832407546 | 2007-7-21 0:00: | PW | No Violations | |
0211854467 | 2007-07-30 | Plug / Plug Back | No Violations | Arvilla was on site to cut off the surface casing and place the ID plate on top. There was a small natural gas leak between the 4-1/2 and the 8-5/8 which will be monitored. The gas probably originates from the Ohio shale. Communication with the Cargill salt cavern has been controlled. The outstanding violation has been corrected. |
0616827636 | 2006-04-13 | Production Wells | Violations Noted | The last reported production from this well was in 1995. The well must either be placed back in production or properly plugged and abandoned. Common tank battery with the Firestone #3 (P/N 824) and the Firestone #5 (P/N 826). |
0832407546 | 2007-07-21 | Production Wells | No Violations | Arvilla attempted to unseat the packer and pull the tubing. The packer would not release and the tubing parted at 2485. Arvilla ran another R-4 packer 30 into the hole to shut off the brine flow. Plugging activity will begin on Monday morning. |
1185813528 | 2007-07-19 | Production Wells | No Violations | I received a call from Richard Jones (330-697-3818) reporting an active brine spill behind the Firestone Polymer complex at 381 Wilbeth Road. The leak occurred in the 4-1/2 casing just above the 8-5/8 casing head. Plant employees noticed the leak earlier this morning. J&M Water Service and Kenmore Construction were on site to recover brine and dig a containment pit respectively. An Arvilla service rig should be on site Friday or Saturday. Plugging operations will commence as soon as the 2-3/8 tubing is removed. Brine continues to flow to surface and there appears to be communication with an abandoned Cargill salt solution mine cavern. |
1439641202 | 2007-08-01 | Plug / Plug Back | No Violations | The containment pit and the well have been closed and graded. Several trees have lost leaves and will checked later in the year to see if they refoliate. |
1621563449 | 2007-07-20 | Production Wells | No Violations | Arvilla will be on site late today and is planning on unseating the packer and recovering the 2-3/8 tubing on Saturday. The brine flow continues and is contained in the recovery pit. J&M will continue to haul water as necessary. |
1680523426 | 2006-07-18 | Production Wells | Violations Noted | Firestone is reported to be obtaining a plugging permit for this well. The plug or produce NOV is still open. |
1840488831 | 2013-07-23 | Final Restoration | No Violations | No indication of well equipment, access road, or tank battery. |
211854467 | 2007-7-30 0:00: | PB | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0616827636 | US-OH-126902 | 2006-04-14 | Well shall be plugged | |
1680523426 | US-OH-116633 | 2006-04-14 | Well shall be plugged |
For data sources see[9]