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34-103-22493

Well Details

Well ID: 34-103-22493
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2006-03-27
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 41.0297759967
Longitude: -81.8755352708

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1033921200 2003-12-24 Cement remains at surface and pipe should be cut off soon.
-1298685485 2006-03-23 Met with Inspector Moravy about the new Solution Mine being installed in Medina Co. needed permit and info .
-1467843878 2006-04-06 Ran 11.6 lb 4 1/2 casing to 2387 ft and cement with 500 sks. Cement did not circulate.Well did circulate but not cement.
-170174271 2006-03-30 Arrive today and find that the service rig is trying to drill out the shoe and cement .They do not have enough weight .
-1949862179 2006-03-22 Met with Ed Mack on well plugging and conversion for Solution Mine.
-2065982930 2009-11-17 Davis well is running new tubing in well today.They are using a new micro coated tubing to solve the iron problem.
-2117268901 2009-11-16 Glenn Davis is trying to knock out rubble pile but does not have enough weight.Tools are too small and most likely will need collars and rotary drill stem.
-281823188 2006-08-15 This well has not been connected for production at this time .
-319521047 2011-04-01 Conduct an MIT on well today. During the last hour two fittings began to leak and when operator attempted to tighten fitting they began to leak 10 times as fast. Advised Ed Mack to repair leaks. Most likely repump interface and re-test well. During the repair there was too much fluid lost and interface will need repumped and well retested for MIT
-402136622 2012-01-24 Bishop Well Service is working on well today because there has been a collapse of the roof and tubing has parted. They ran more tubing in and the well is now back in operation.
-501429759 2008-04-07 Arrive for possible shoot off and or plug job.Tubing is leaking and is stuck in well and may have to be shot off .Rig is going to try and work tubing and will contack if plugging is needed.
-674469842 2008-04-10 Arrive and met with rig crew .Still working to free tubing and have made good progress.Next tubing came free and may be parted.They will try to fish out and if not plug well.Found tubing connected and need to clean out well and run in with new string of t
-842042285 2006-04-12 Cement top of annulus between 7 inch and 41/2 casing. Placed 9 sk grout in well with Orrville Trucking by gravity.The mix had to be very wet in order to go in between casing strings and took forever because of restriction due to size.Did get well to fill up with correct volume.
1044358390 2011-04-04 Arrive for possible test today and found that interface has not been re-spotted . Test on # 3 well not ready either.
1144690772 2006-04-10 Pressure up 4 1/2 casing today for M.I.T.- Had a lot of air in system and first and second tests failed.Bled air from line and test again and the 3rd test passed. Test at 560 P.S.I. And after 5 minutes it had dropped to 555 P.S.I. And remained there until the test was complete.15 minutes with only a 5 LB. P.S.I. Decline.
1144946971 2006-03-28 Ran 1 1/2 tubing to 2700 ft and set plug from 2700 to 2500 ft. c/w 15 sks. Then pull up to 2500 ft. and circulate any leftover cement out of well.Next ran in hole to 2450 ft and shot off casing.
1206100712 2008-03-21 Inspect well and location. Advised securety at plant. Well is in operation.
1593559409 2012-10-04 Made an attempt to pull the fiberglass tubing but it is hung in the hole. Rigged down and moved off. The well was put back to injecting.
1650994935 2011-04-08 Conduct MIT on well today which passed. It had leaks around several fittings at surface and still passed .
1889312477 2006-04-05 Return and wait on cement trucks and found that they can't make job before dark so job was cancelled.
1953816524 2006-04-05 Arrive today and found service rig pulling tubing and will run 4 1/2 in and cement this afternoon.
1955332078 2006-03-31 Drill out plug and job will be cancelled today ,cement trucks not available.\Schedule for Monday.
338181829 2006-03-27 Glenn Davis service rig pulled rods and tubing and then set bottom plug at 3260 to 2540 ft. c/w 54 sks.Petrsoset Cementing John .
436981975 2006-04-03 Trip in hole with 4 1/2 casing and while going in hole hit obstruction and could not get past it . Trip out to drill out obstruction.
581230689 2009-08-17 Ed Mack contacted me and advised they had problem with NO brine during solution .Hole in tubing or break off.
649786304 2006-03-29 Ran in hole with 534 ft. of 17 lb 7 inch casing and circulate cement back to surface.C/w 100 Sks class A 4 % C.C. Cement remained at surface after job was complete.
784938373 2008-09-10 Area needs more seed and vegetation .Has some just not enough.They have had a rig on location and t have not had good weather to seed and establish vegetation.Met with their field man in charge of the wells and advise on more cover.
97833637 2007-11-29 Pits are closed and area is graded and seeded.
PL12185 Preliminary Restoration done information from Data Point