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Well ID: 34-103-22493 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: BLEACHTECH LLC | |
Well Pad ID: | |
Farm/Lease Name: AMHEISER (SMP #1) | |
License Status: Plugged and Abandoned | |
License Date: 2014-11-20 | |
Spud Date: 2006-03-27 | |
Spud Drilling Contractor: DAVIS DRLG | |
Final Drill Date: 1981-04-20 | |
Well Total Depth: 3315.00 ft | |
Configuration: Vertical | |
Latitude: 41.020000 | |
Longitude: -81.870000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-12-30 | 265 CSAPO FRANK A JR GeoDate 12/30/80 |
Oil and Gas | 1980-12-30 | Issued Date 12/30/80 Expired Date Acres 0020900 Tool Type CT Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1981-03-12 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
Completed | 1981-04-20 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
Reached Total Depth | 1981-04-20 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
Change of Owner | 2006-03-17 | Operator changed from 265, CSAPO FRANK to 7998, BLEACH TECH LLC |
APP | 2006-03-20 | Proposed Formations:NEWBURG, Issued Date:3/20/2006, Expired Date:3/20/2007 6:00:00 AM, Drilling unit acres:20.97, Proposed Well Type:ST, Proposed Well Class: |
Plugged Back | 2006-04-12 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
Completion Report Received | 2006-05-01 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
APP | 2006-07-28 | Proposed Formations:SALINA FI SALT, Issued Date:7/28/2006, Expired Date:7/28/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class:SMP |
Last Compliance Report | 2011-04-26 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
APP | 2014-11-20 | Proposed Formations:SALINA, Issued Date:11/20/2014, Expired Date:11/19/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SM, Proposed Well Class: |
Plugged/Abandoned | 2014-12-09 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
Record Last Modified | 2015-09-24 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
Construction Permit Expires | 2016-11-19 | OTD: 3315' PRODUCING OIL & GAS IN CLINTON. PLUG BACK TO TEST SALINA FOR SMP, CONVERTED TO SMP WELL |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3260 | 3280 | 0 |
3260 | 3280 | 0 | |
3260 | 3280 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 3000 Bbl | 40000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CSAPO LIMITED | 7908.00 | 0.00 | 0 |
1985 | CSAPO LIMITED | 24344.00 | 0.00 | 365 |
1986 | CSAPO LIMITED | 1329.00 | 122.00 | 365 |
1987 | CSAPO LIMITED | 1672.00 | 0.00 | 182 |
1988 | CSAPO LIMITED | 304.00 | 0.00 | 365 |
1989 | CSAPO LIMITED | 39.00 | 0.00 | 365 |
1990 | CSAPO LIMITED | 4.00 | 24.00 | 365 |
1991 | CSAPO LIMITED | 0.00 | 0.00 | 365 |
1992 | CSAPO LIMITED | 0.00 | 0.00 | 365 |
1993 | CSAPO LIMITED | 1150.00 | 0.00 | 365 |
1994 | CSAPO LIMITED | 1003.00 | 0.00 | 365 |
1995 | CSAPO LIMITED | 624.00 | 0.00 | 365 |
1996 | CSAPO LIMITED | 467.00 | 0.00 | 365 |
1997 | CSAPO LIMITED | 211.00 | 0.00 | 365 |
1998 | CSAPO LIMITED | 129.00 | 0.00 | 365 |
2000 | CSAPO LIMITED | 138.00 | 0.00 | 365 |
2001 | CSAPO LIMITED | 198.00 | 38.00 | 365 |
2002 | CSAPO LIMITED | 263.00 | 0.00 | 365 |
2003 | CSAPO LIMITED | 247.00 | 0.00 | 365 |
2004 | CSAPO LIMITED | 153.00 | 0.00 | 365 |
2005 | CSAPO LIMITED | 33.00 | 0.00 | 365 |
2006 | CSAPO LIMITED | 13.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CSAPO LIMITED | Brine | 0 | 0 |
1985 | CSAPO LIMITED | Brine | 115 | 365 |
1986 | CSAPO LIMITED | Brine | 50 | 365 |
1987 | CSAPO LIMITED | Brine | 0 | 182 |
1988 | CSAPO LIMITED | Brine | 23 | 365 |
1989 | CSAPO LIMITED | Brine | 0 | 365 |
1990 | CSAPO LIMITED | Brine | 15 | 365 |
1991 | CSAPO LIMITED | Brine | 0 | 365 |
1992 | CSAPO LIMITED | Brine | 0 | 365 |
1993 | CSAPO LIMITED | Brine | 0 | 365 |
1994 | CSAPO LIMITED | Brine | 0 | 365 |
1995 | CSAPO LIMITED | Brine | 25 | 365 |
1996 | CSAPO LIMITED | Brine | 46 | 365 |
1997 | CSAPO LIMITED | Brine | 0 | 365 |
1998 | CSAPO LIMITED | Brine | 16 | 365 |
2000 | CSAPO LIMITED | Brine | 2 | 365 |
2001 | CSAPO LIMITED | Brine | 0 | 365 |
2002 | CSAPO LIMITED | Brine | 35 | 365 |
2003 | CSAPO LIMITED | Brine | 0 | 365 |
2004 | CSAPO LIMITED | Brine | 0 | 365 |
2005 | CSAPO LIMITED | Brine | 0 | 365 |
2006 | CSAPO LIMITED | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1033921200 | 2003-12-24 0:00 | PB | No Violations | 1.00 |
-1298685485 | 2006-3-23 0:00: | NW | No Violations | 1.70 |
-1368592765 | 2014-12-10 0:00 | PB | No Violations | |
-1467843878 | 2006-4-6 0:00:0 | PB | No Violations | 3.70 |
-170174271 | 2006-3-30 0:00: | PB | No Violations | 2.20 |
-1765309109 | 2014-12-4 0:00: | PB | No Violations | |
-1949862179 | 2006-3-22 0:00: | PB | No Violations | 1.50 |
-2065982930 | 2009-11-17 0:00 | SM | No Violations | 2.00 |
-2117268901 | 2009-11-16 0:00 | SM | No Violations | 3.00 |
-281823188 | 2006-8-15 0:00: | SM | No Violations | 1.00 |
-319521047 | 2011-4-1 0:00:0 | SM | No Violations | 9.70 |
-402136622 | 2012-1-24 0:00: | SM | No Violations | 1.50 |
-501429759 | 2008-4-7 0:00:0 | SM | No Violations | 3.00 |
-674469842 | 2008-4-10 0:00: | SM | No Violations | 3.00 |
-842042285 | 2006-4-12 0:00: | PB | No Violations | 5.50 |
000PL12185 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0097833637 | 2007-11-29 | Solution Mining Project | No Violations | Pits are closed and area is graded and seeded. |
0151435377 | 2014-12-05 | Plug / Plug Back | No Violations | Arrived on location to witness the start of plugging operations on the Bleachtech #1 well. Appalachian Wireline Services was onsite and rigged up. Ran in hole with wireline to set the bridge plug. Bridge plug set at 2,320, as the location appears to be in good cement, not in a collar, and within 50 of the top of the cavern. Set down on the plug - plug held. Rig down Appalachian Wireline. Shut down for the weekend. |
0170174271 | 2006-03-30 | Plug / Plug Back | No Violations | Arrive today and find that the service rig is trying to drill out the shoe and cement .They do not have enough weight . |
0281823188 | 2006-08-15 | Solution Mining Project | No Violations | This well has not been connected for production at this time . |
0319521047 | 2011-04-01 | Solution Mining Project | No Violations | Conduct an MIT on well today. During the last hour two fittings began to leak and when operator attempted to tighten fitting they began to leak 10 times as fast. Advised Ed Mack to repair leaks. Most likely repump interface and re-test well. During the repair there was too much fluid lost and interface will need repumped and well retested for MIT |
0338181829 | 2006-03-27 | Plug / Plug Back | No Violations | Glenn Davis service rig pulled rods and tubing and then set bottom plug at 3260 to 2540 ft. c/w 54 sks.Petrsoset Cementing John . |
0402136622 | 2012-01-24 | Solution Mining Project | No Violations | Bishop Well Service is working on well today because there has been a collapse of the roof and tubing has parted. They ran more tubing in and the well is now back in operation. |
0436981975 | 2006-04-03 | Plug / Plug Back | No Violations | Trip in hole with 4 1/2 casing and while going in hole hit obstruction and could not get past it . Trip out to drill out obstruction. |
0501429759 | 2008-04-07 | Solution Mining Project | No Violations | Arrive for possible shoot off and or plug job.Tubing is leaking and is stuck in well and may have to be shot off .Rig is going to try and work tubing and will contack if plugging is needed. |
0581230689 | 2009-08-17 | Solution Mining Project | No Violations | Ed Mack contacted me and advised they had problem with NO brine during solution .Hole in tubing or break off. |
0649786304 | 2006-03-29 | Plug / Plug Back | No Violations | Ran in hole with 534 ft. of 17 lb 7 inch casing and circulate cement back to surface.C/w 100 Sks class A 4 % C.C. Cement remained at surface after job was complete. |
0674469842 | 2008-04-10 | Solution Mining Project | No Violations | Arrive and met with rig crew .Still working to free tubing and have made good progress.Next tubing came free and may be parted.They will try to fish out and if not plug well.Found tubing connected and need to clean out well and run in with new string of t |
0784938373 | 2008-09-10 | Preliminary Restoration | No Violations | Area needs more seed and vegetation .Has some just not enough.They have had a rig on location and t have not had good weather to seed and establish vegetation.Met with their field man in charge of the wells and advise on more cover. |
0842042285 | 2006-04-12 | Plug / Plug Back | No Violations | Cement top of annulus between 7 inch and 41/2 casing. Placed 9 sk grout in well with Orrville Trucking by gravity.The mix had to be very wet in order to go in between casing strings and took forever because of restriction due to size.Did get well to fill up with correct volume. |
1033921200 | 2003-12-24 | Plug / Plug Back | No Violations | Cement remains at surface and pipe should be cut off soon. |
1044358390 | 2011-04-04 | Solution Mining Project | No Violations | Arrive for possible test today and found that interface has not been re-spotted . Test on # 3 well not ready either. |
1082074303 | 2014-12-11 | Plug / Plug Back | No Violations | Visited location on 12/11/2014. Pit has been closed. Permanent monument with permit number has been installed at the well. |
1119708437 | 2014-12-02 | Plug / Plug Back | No Violations | Visited location on 12/02/2014 to check on the rigs progress at preparing for plugging operations. Bishop Well Service was still pulling rods and did not expect to be ready to plug until Thursday or Friday. Will monitor progress and be back to witness plugging operations. |
1133173133 | 2014-12-09 | Plug / Plug Back | No Violations | Arrived on location on 12/09/2014 to finish plugging out the well. Rigged up Petroset and thawed out equipment. Finished plugging out well, completely filling the casing with cement. Circulation was established prior to setting each plug. Good cement was seen at surface. Top of cement stayed at surface even after all tubing was removed. |
1144690772 | 2006-04-10 | Plug / Plug Back | No Violations | Pressure up 4 1/2 casing today for M.I.T.- Had a lot of air in system and first and second tests failed.Bled air from line and test again and the 3rd test passed. Test at 560 P.S.I. And after 5 minutes it had dropped to 555 P.S.I. And remained there until the test was complete.15 minutes with only a 5 LB. P.S.I. Decline. |
1144946971 | 2006-03-28 | Plug / Plug Back | No Violations | Ran 1 1/2 tubing to 2700 ft and set plug from 2700 to 2500 ft. c/w 15 sks. Then pull up to 2500 ft. and circulate any leftover cement out of well.Next ran in hole to 2450 ft and shot off casing. |
1193538014 | 2014-12-08 | Plug / Plug Back | No Violations | Arrived on location to witness MIT. Bishop Well Service was still running in the hole with tubing upon arrival. Ran in hole to one joint above the bridge plug. Pressured well up to 650# and held it for 15 minutes. No pressure was lost. MIT passed. Will be back on location once tubing has been tripped out and tripped back in to set bottom plug. |
1206100712 | 2008-03-21 | Solution Mining Project | No Violations | Inspect well and location. Advised securety at plant. Well is in operation. |
1292362556 | 2014-12-08 | Plug / Plug Back | No Violations | Arrived on location on 12/08/2014 to witness plugging operations. Petroset arrived and rigged up. Established circulation with freshwater prior to pumping cement. Set bottom plug through tubing with no problems. Shut down for the day. |
1298685485 | 2006-03-23 | Non Well | No Violations | Met with Inspector Moravy about the new Solution Mine being installed in Medina Co. needed permit and info . |
1368592765 | 2014-12-10 | Plug / Plug Back | No Violations | Visited location on 12/10/2014 to check on cement top. Top of cement stayed at ground level. Permanent monuments will be installed later today. Pits will also be worked on later in the day. |
1467843878 | 2006-04-06 | Plug / Plug Back | No Violations | Ran 11.6 lb 4 1/2 casing to 2387 ft and cement with 500 sks. Cement did not circulate.Well did circulate but not cement. |
151435377 | 2014-12-5 0:00: | PB | No Violations | |
1593559409 | 2012-10-04 | Solution Mining Project | No Violations | Made an attempt to pull the fiberglass tubing but it is hung in the hole. Rigged down and moved off. The well was put back to injecting. |
1650994935 | 2011-04-08 | Solution Mining Project | No Violations | Conduct MIT on well today which passed. It had leaks around several fittings at surface and still passed . |
1765309109 | 2014-12-04 | Plug / Plug Back | No Violations | Visited location on 12/04/2014 to check on status of plugging operations. Bishop Well Service was still scraping out production casing, and would not be ready until Friday. |
1889312477 | 2006-04-05 | Plug / Plug Back | No Violations | Return and wait on cement trucks and found that they cant make job before dark so job was cancelled. |
1949862179 | 2006-03-22 | Plug / Plug Back | No Violations | Met with Ed Mack on well plugging and conversion for Solution Mine. |
1953816524 | 2006-04-05 | Plug / Plug Back | No Violations | Arrive today and found service rig pulling tubing and will run 4 1/2 in and cement this afternoon. |
1955332078 | 2006-03-31 | Plug / Plug Back | No Violations | Drill out plug and job will be cancelled today ,cement trucks not available.Schedule for Monday. |
2065982930 | 2009-11-17 | Solution Mining Project | No Violations | Davis well is running new tubing in well today.They are using a new micro coated tubing to solve the iron problem. |
2117268901 | 2009-11-16 | Solution Mining Project | No Violations | Glenn Davis is trying to knock out rubble pile but does not have enough weight.Tools are too small and most likely will need collars and rotary drill stem. |
338181829 | 2006-3-27 0:00: | PB | No Violations | 4.70 |
436981975 | 2006-4-3 0:00:0 | PB | No Violations | 2.70 |
581230689 | 2009-8-17 0:00: | SM | No Violations | 1.00 |
649786304 | 2006-3-29 0:00: | PB | No Violations | 4.50 |
784938373 | 2008-9-10 0:00: | PL | No Violations | 2.00 |
97833637 | 2007-11-29 0:00 | SM | No Violations | 1.00 |
PL12185 | PL | No Violations |
For data sources see[9]