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Well ID: 34-055-20407 | Loading map...
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County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1982-12-05 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 1 | |
Latitude: 41.5120396695 | |
Longitude: -81.1275488758 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
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PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
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INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
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-1614515483 | 2013-11-21 | My inspection found the pump jack and rods have been removed from the well. The rock pad and electric service for the pump jack still remain. The well still has the tubing in it. The valves on the wellhead are closed. The tank battery is over grown with weeds and tree saplings. The tank battery consists of two 100 BBL production tanks and a buried concrete brine tank. The separator appears to have been removed from the location. There is no identification on location. Production records show the well has not had production reported since 1996. I will contact the company about the well. The well shall be placed back into production in 90 days. If the well is not producible a plugging permit shall be obtained within 90 days and the well shall be plugged within 180 days of this compliance action. | NONE | |||
326221819 | 2014-08-18 | My inspection found no chsanges since my last inspection. The landowner wants the well to be put back into operation. The company has the service scheduled to get the well back into production. |