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37-015-21341

Well Details

Well ID: 37-015-21341
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County: Bradford
Municipality: Asylum Township
Operator Name: CHIEF OIL & GAS LLC
Well Pad ID: 147714
Farm/Lease Name: ALLEN UNIT 1H
First Permit Date: 2010-11-22
Last Permit Date: 2010-11-22
Spud Date: 2011-01-02
Unconventional: Yes
Horizontal: Yes
Well Status: ACTIVE
Violations: 4
Latitude: 41.730263
Longitude: -76.330425

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 501035.7 90.0 0.0 0.0 0.0 0.0
2012-2 1266403.0 184.0 0.0 0.0 0.0 0.0
2013-1 1321279.0 165.0 0.0 0.0 0.0 0.0
2013-2 1123882.0 180.0 0.0 0.0 0.0 0.0
2014-1 877878.0 181.0 0.0 0.0 0.0 0.0
2014-2 370809.0 183.0 0.0 0.0 0.0 0.0
2015-02 15421.0 10.0 0.0 0.0 0.0 0.0
2015-01 58840.0 31.0 0.0 0.0 0.0 0.0
2015-03 50563.0 31.0 0.0 0.0 0.0 0.0

For data sources see[1]

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2010-2 FRACING FLUID WASTE 2.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472 TUNNELTON LIQUIDS TREATMENT FACILITY SALTSBURG PA
2011-2 FRACING FLUID WASTE 5.0 Bbl REUSE OTHER THAN ROAD SPREADING FRAC WATER REUSE PA
2012-1 FRACING FLUID WASTE 3.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-1 PRODUCED FLUID 1.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-2 PRODUCED FLUID 657.5 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2013-1 PRODUCED FLUID 4.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2013-2 PRODUCED FLUID 792.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
2014-1 PRODUCED FLUID 489.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
2014-2 PRODUCED FLUID 181.44 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY

For data sources see[2]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1952183 2011-02-11 No Violations Noted Brandon. Set conductor with Zigenfus to 40'. Drilling with air to 5000' closed loop system. Drilled wells 1 and 2 with Zigenfus. Well #1 - no shows. Well #2 - showed 80 bbls of water that dried right up.

20' set to 40' 13 3/8 set at 465' 9 5/8 set at 1762' - cementing at 12:30pm on 2/11

Small oil spill on liner and housekeeping needs some work. will followup in 5 days.

1965593 2011-04-14 Violation(s) Noted Bubbling between the 9 5/8 and 13 3/8 annuli. 8-10% combustible gas reading utilizing the MSA Model 60 gas meter. Uncontrolled release of gas. No well tag on wellhead. Iotopic sample obtained. 608861 78.86 - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days
1965593 2011-04-14 Violation(s) Noted Bubbling between the 9 5/8 and 13 3/8 annuli. 8-10% combustible gas reading utilizing the MSA Model 60 gas meter. Uncontrolled release of gas. No well tag on wellhead. Iotopic sample obtained. 608863 201TAG - Failure to install, in a permanent manner, the permit number on a completed well
1976892 2011-05-10 Outstanding Violations - No Viols Req'd Methane vented to tank. No visible bubbling in cellar
1983982 2011-06-28 Violation(s) Noted 614410 78.66A - Failure to report release of substance threatening or causing pollution
1983982 2011-06-28 Violation(s) Noted 614414 402CSL - Failure to adopt pollution prevention measures required or prescribed by DEP by handling materials that create a danger of pollution.
1985326 2011-06-28 Outstanding Violations - No Viols Req'd Cellars filled with gravel. Condensate (methane) coming up thru gravel.
1985800 2011-07-04 Outstanding Violations - No Viols Req'd
1987034 2011-07-12 No Violations Noted
1994975 2011-08-09 No Violations Noted Faulty pressure gauge replaced. gauge now reads 0 psi on 9 5/8.
2134260 2013-01-29 No Violations Noted Neighbor filed new water supply complaint, pad is closest and upgradient.

For data sources see[3]

References