X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-113-20102

Well Details

Well ID: 37-113-20102
Loading map...
County: Sullivan
Municipality: Fox Township
Operator Name: CHIEF OIL & GAS LLC
Well Pad ID: 150919
Farm/Lease Name: KUZIAK UNIT 1H
First Permit Date: 2011-04-15
Last Permit Date: 2011-04-15
Spud Date: 2011-08-04
Unconventional: Yes
Horizontal: Yes
Well Status: ACTIVE
Violations: 1
Latitude: 41.559722
Longitude: -76.705916

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2012-2 0.0 0.0 0.0 0.0 0.0 0.0
2013-1 0.0 0.0 0.0 0.0 0.0 0.0
2013-2 0.0 0.0 0.0 0.0 0.0 0.0
2014-1 32339.0 3.0 0.0 0.0 0.0 0.0
2014-2 847801.0 169.0 0.0 0.0 0.0 0.0
2015-02 45593.01 21.0 0.0 0.0 0.0 0.0
2015-01 36231.0 27.0 0.0 0.0 0.0 0.0
2015-03 53854.77 31.0 0.0 0.0 0.0 0.0

For data sources see[1]

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2011-2 DRILL CUTTINGS 1.0 Tons LANDFILL 301626 WHITE PINES LANDFILL MILLVILLE PA
2013-1 FRACING FLUID WASTE 43.38 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR123NC006 CLEAN STREAMS LLC WILLIAMSPORT FACILITY WILLIAMSPORT PA
2013-1 FRACING FLUID WASTE 350.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR0123 HYDRO RECOVERY LP BLOSSBURG FACILITY BLOSSBURG PA
2013-1 FRACING FLUID WASTE 4.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2014-2 FLOWBACK FRACTURING SAND 60.0 Tons RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR0123 HYDRO RECOVERY LP BLOSSBURG FACILITY BLOSSBURG PA
2014-2 PRODUCED FLUID 5.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY

For data sources see[2]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1994972 2011-08-09 No Violations Noted UDI 207. rig moved in on location. Plan on running and cementing 13 3/8 Aug 12, 2011 AM.

Cond set at 80'

1996013 2011-08-15 No Violations Noted Currently at 1421' UDI Rig 207. running dev survey.

20 set at 78 13 3/8 set at 586 (540 sakcs) 15.6# 20 bbls returned 9 5/8 paln on setting at 1809'

Tested BOPs on 8 /14/11

Planned KO 6897' ETD 18019'

1999112 2011-08-19 Viol(s) Noted & Immediately Corrected 618861 78.56(1) - Pit and tanks not constructed with sufficient capacity to contain pollutional substances.
2032961 2012-01-10 No Violations Noted
2045070 2012-02-23 No Violations Noted
2161466 2013-04-25 No Violations Noted
2363210 2015-04-13 No Violations Noted Arrived @ 11:50. There were two wells on the pad. The 1H was in production. At the 13-3/8 x 9-5/8 annulus there was 5% methane. I could not obtain a separate fiend reading at the 9-5/8 x 5-1/2 annulus. There was some staining immediately around the well cellar. The other well

For data sources see[3]

References