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Well ID: 37-113-20102 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Sullivan | |
Municipality: Fox Township | |
Operator Name: CHIEF OIL & GAS LLC | |
Well Pad ID: 150919 | |
Farm/Lease Name: KUZIAK UNIT 1H | |
License Status: | |
Spud Date: 2011-08-04 | |
Permit Date: 2011-04-15 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.559722 | |
Longitude: -76.705917 |
Date | Event |
---|---|
2011-04-15 | New Permit Application |
2011-08-04 | Performed Spud Operation |
2011-09-17 | Drilling Completion |
2011-11-07 | Perforation |
2012-04-27 | DEVIATED |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2011-11-14 | 2011-11-14 | 7,185 | 979,062 | |
2 | 2012-12-12 | 2012-12-12 | 7,185 | 4,143,300 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | KR-153SL | Superior Well Services | Biocide | |||||
Diethylene glycol | 111-46-6 | |||||||
Polyethylene glycol | 25322-68-3 | 5000.00 | ||||||
2,2-Dibromo-3-nitrilopropionamide | 10222-01-2 | 20.00 | 0.02 | |||||
Ethylene glycol | 107-21-1 | 100.00 | ||||||
WFR-3B | Superior Well Services | Friction Reducer | Ethoxylated C12-16 alcohols | 68551-12-2 | 4.00 | |||
1,2-Propylene glycol | 57-55-6 | 25.00 | ||||||
Distillates, petroleum, hydrotreated light | 64742-47-8 | 0.14 | ||||||
Stoddard solvent | 8052-41-3 | 10.00 | ||||||
Super Scale Control TSC | Superior Well Services | Scale Inhibitor | 1,2,4-Butanetricarboxylic acid, 2-phosphono- | 37971-36-1 | ||||
Anionic Polymer | ||||||||
Anionic Copolymer | ||||||||
1,2-Propylene glycol | 57-55-6 | 0.04 | ||||||
Water | Base Fluid | Fresh Water | 100.00 | 84.87 | ||||
Sand (Proppant) | Superior Well Services | Propping Agent | Quartz | 14808-60-7 | 99.90 | 14.92 | ||
2 | FRW-66 | Halliburton Energy Services | Friction Reducer | Hydrotreated Light Distillate 64742-47-8 |
0.08 | |||
Sand (Proppant) | Halliburton Energy Services | Propping Agent | Quartz | 14808-60-7 | 99.90 | 38.00 | ||
Hydrochloric Acid 28 | Halliburton Energy Services | Acid | ||||||
Hydrochloric acid | 7647-01-0 | 0.54 | ||||||
Water 7732-18-5 85 |
||||||||
Biocide - Bactron K 139 | Champion Technologies | Biocide | Quaternary ammonium compounds, benzyl-C12-16-alkyldimethyl, chlorides |
68424-85-1 | 10.00 | |||
Ethanol | 64-17-5 | 5.00 | ||||||
Glutaraldehyde | 111-30-8 | 5.00 | 0.04 | |||||
Water | Base Fluid | Fresh Water | 100.00 | 62.00 | ||||
Gyptron T-390 Champion Technologies | Scale Inhibitor | |||||||
Gyptron T-390 Champion Technologies | Halliburton Energy Services | Scale Inhibitor | ||||||
Methanol 67-56-1 10.00 |
0.01 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2011 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | CHIEF OIL & GAS LLC | 880,140.00 | 172 | 0.00 | 0 | 0.00 | 0 |
2015 | CHIEF OIL & GAS LLC | 384,833.09 | 309 | 0.00 | 0 | 0.00 | 0 |
2016 | CHIEF OIL & GAS LLC | 262,565.45 | 325 | 0.00 | 0 | 0.00 | 0 |
2017 | CHIEF OIL & GAS LLC | 128,909.85 | 287 | 0.00 | 0 | 0.00 | 0 |
2018 | CHIEF OIL & GAS LLC | 82,886.71 | 313 | 0.00 | 0 | 0.00 | 0 |
2019 | CHIEF OIL & GAS LLC | 6,641.78 | 52 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2011 | CHIEF OIL & GAS LLC | Drill Cuttings | 1,949.77 Tons | LANDFILL | 301626 |
2013 | CHIEF OIL & GAS LLC | Fracing Fluid Waste | 350.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123 |
2013 | CHIEF OIL & GAS LLC | Fracing Fluid Waste | 43.38 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NC006 |
2013 | CHIEF OIL & GAS LLC | Fracing Fluid Waste | 4,192.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2014 | CHIEF OIL & GAS LLC | Fracturing Fluid Waste | 60.00 Tons | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2014 | CHIEF OIL & GAS LLC | Produced Fluid | 5,736.43 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2015 | CHIEF OIL & GAS LLC | Produced Fluid | 45.67 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2015 | CHIEF OIL & GAS LLC | Produced Fluid | 3,238.28 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | CHIEF OIL & GAS LLC | Produced Fluid | 3,015.61 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2017 | CHIEF OIL & GAS LLC | Produced Fluid | 0.40 Bbl | STORAGE PENDING DISPOSAL OR REUSE | |
2017 | CHIEF OIL & GAS LLC | Produced Fluid | 1,005.88 Bbl | REUSE (AT WELL PAD) | |
2018 | CHIEF OIL & GAS LLC | Produced Fluid | 238.61 Bbl | REUSE (AT WELL PAD) | |
2019 | CHIEF OIL & GAS LLC | Produced Fluid | 17.40 Bbl | REUSE (AT WELL PAD) |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1994972 | Primary Facility | 2011-08-09 | Drilling/Alteration | No Violations Noted | UDI 207. rig moved in on location. Plan on running and cementing 13 3/8 Aug 12, 2011 AM. |
1996013 | Primary Facility | 2011-08-15 | Drilling/Alteration | No Violations Noted | Currently at 1421' UDI Rig 207. running dev survey. |
1999112 | Primary Facility | 2011-08-19 | Follow-up Inspection | Viol(s) Noted & Immediately Corrected | |
2032961 | Primary Facility | 2012-01-10 | Routine/Complete Inspection | No Violations Noted | |
2045070 | Primary Facility | 2012-02-23 | Routine/Complete Inspection | No Violations Noted | |
2161466 | Primary Facility | 2013-04-25 | Routine/Complete Inspection | No Violations Noted | |
2363210 | Primary Facility | 2015-04-13 | Routine/Complete Inspection | No Violations Noted | Arrived @ 11:50. There were two wells on the pad. The 1H was in production. At the 13-3/8” x 9-5/8” annulus there was 5% methane. I could not obtain a separate fiend reading at the 9-5/8” x 5-1/2” annulus. There was some staining immediately around the well cellar. The other well, the 7V, was capped. The cellar was partly water-filled with an oily-looking scum on top. Field readings were 0% methane for both the 13-3/8” x 8-5/8” annulus and 9-5/8” vent. Met Kevin Hadlock towards the end of my inspection. Left @12:30 |
2481105 | Primary Facility | 2016-05-04 | Routine/Complete Inspection | No Violations Noted | The site currently has >70% coverage of perennial vegetation; temporary erosion and sediment control BMPs are still in place. No evidence of accelerated erosion or sedimentation was observed.
The electrical conductance of puddles was not screened due to the absence of puddles. The Erosion and Sediment Control General Permit for this site expires on 06/17/2016. No current well permits exist. Chief has indicated that it plans to partially restore the well pad sometime in 2016. In order to remain in compliance with the Department's regulations regarding site restoration (Title 58 Pa. C.S. § 3216), Chief should obtain a new drilling permit or request a 2-year extension of time for site restoration. No violations were cited during this inspection. |
2499035 | Primary Facility | 2016-06-30 | Routine/Complete Inspection | Pending | Well in production, compressor on site undergoing routine maintanence. Cellar water filled.
top gauge: 600 psi (0-2000 psi analog) 5-1/2": 600 psi 13" x 9": 74% methane. |
2513652 | Primary Facility | 2016-08-04 | Routine/Complete Inspection | Violation(s) Noted | Arrived @ 10:30. Weather: sunny, warm. No company representatives were present during the inspection. There were 2wells and a small compressor on the site. The Kuziak 1H was in production with artificial lift. This follow-up inspection was prompted by an Inactive Well Status application for Kuziak Unit 7V. Previously on 6/30/16, combustible gas was detected on the Kuziak Unit 1H well at the 13-3/8” x 9-5/8” annulus. Typically, the 1” , 13-3/8” x 9-5/8” annular vent T’s into the 2” 13-3/8” x 9-5/8” annular vent, allowing for cross-contamination. To eliminate that possibility in this follow-up inspection, the annuli were open and isolated from each other prior to my arrival on site. Monitoring was conducted with Altair 5X gas meter (calibrated: 7/26/16).
Kuziak 1H .13-3/8” x 9-5/8”: 17%/volume combustible gas, 9-5/8” x 5-1/2”: 9%/volume combustible gas. The combustible gas detected at the 13-3/8” x 9-5/8” annuli of the Kuziak 1H well is evidence of defective cement which is a violation of Title 25 §78.8 |
2556777 | Primary Facility | 2016-01-30 | Routine/Complete Inspection | No Violations Noted | Routine inspection conducted to assess general conditions on site. No Chief representatives were present.
This site has been partially restored. The pad has been reduced in size, and much of the remaining area has been de-compacted and vegetated. Temporary erosion and sediment controls were in place around the perimeter of the site. No evidence of accelerated erosion or sedimentation was observed. No violations were cited during this inspection. |
2685693 | Primary Facility | 2018-01-23 | Routine/Complete Inspection | No Violations Noted | One well staged for production phase. One well not staged for production. Two each sand and water separators. No leaks detected from production equipment. No violations noted. |
2736447 | Primary Facility | 2018-06-01 | Routine/Complete Inspection | No Violations Noted | One well staged for production phase. One water separator. No leaks detected from production equipment. No violations noted. |
2788176 | Primary Facility | 2018-10-11 | Routine/Complete Inspection | No Violations Noted | Chief Oil & Gas submitted a Notice of Termination (NOT) for the Kuziak pad covered under ESG29-113-18-0001. The NOT was received by the Department on 10/5/18.
It had rained throughout the day and during part of the inspections. Some small puddles had formed on the pad and had a conductivity below 100 µS/cm. The pad has been reduced in size and the majority is now vegetation. The areas of vegetation around the site were >70% cover. No E&S issues were observed. There is 1 active well and 1 inactive well onsite. The well cellars were filled with water; no bubbling was observed. There is also 1 GPU, 1 compressor, and 2 steel produced water tanks onsite and in secondary containment. All containment appeared to be in good condition. The PCSM measures consist of 1 infiltration berm near the southwest corner of the pad. The berm appeared to be installed and functioning as designed. No violations noted. The Department recommends acknowledging termination of coverage under ESG29-113-18-0001. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
1999112 | 618861 | 08/19/2011 | 2011-08-19 | 78.56(1) - Pit and tanks not constructed with sufficient capacity to contain pollutional substances. | Administrative | |
2513652 | 766750 | 2016-08-04 | 78.86 | Environmental Health & Safety | see description in admin. |
For data sources see[8]