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34-067-21324

Well Details

Well ID: 34-067-21324
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County: Harrison
Municipality:
Operator Name: CHESAPEAKE EXPLORATION LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-05-15
Unconventional: No
Configuration: Vertical
Well Status: Well Drilled
Violations: 0
Latitude: 40.3599835
Longitude: -81.05945778

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1341306860 2014-10-31 At 10766' and tripping back into the hole after a bottom hole assembly change. No problems were noted at the time of the inspection.
1414391804 2014-10-25 The rig ran 591' of 13-3/8 casing and the associated float equipment. Schlumberger cemented it with 580sacks of Class A cement. Good cement was returned to the surface. See the casing ticket for the details.
-271988729 2014-05-15 Rocky Mountain Drilling has a top hole rig on site to drill and set the conductor casing. Ready later today.
-484561075 2014-10-27 The rig ran 2322' of 9-5/8 casing and the associated float equipment. Schlumberger cemented it with 870 sacks of Class A cement. Good cement was returned to the surface. See the casing ticket for the details.
574881462 2014-05-15 On the day of my inspection I found that Rocky Mountain Drilling had drilled a 26 hole to a depth of 120' with and auger rig. They ran new 20 conductor casing to 120'. Universal Well Services cemented the casing to surface with 245 sacks of class A cement. There were approximately 12 barrels of cement circulated to the surface.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.