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Well ID: 34-119-25737 | Loading map...
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County: Muskingum | |
Municipality: | |
Operator Name: KING PETROLEUM 2 | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1982-12-15 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 40.08728238 | |
Longitude: -82.1754246 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1999-0 | 0.0 | 416.0 | ||||
2000-0 | 0.0 | 159.0 | ||||
2003-0 | 0.0 | 0.0 | ||||
2004-0 | 0.0 | 0.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2006-0 | 0.0 | 0.0 | ||||
2007-0 | 0.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 0.0 | 87.0 | ||||
2011-0 | 0.0 | 42.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1179186610 | 2011-07-18 | Phil Moran called and stated that they placed a 350' clay plug in and then ripped the 4.5 casing at 2450'. I did not witness this activity. The clay plug would have been from 2786'-2436'. | ||||
-1790408168 | 2011-07-22 | Stopped at the well site and found cement level down 15'. Moran will let set and top off. | ||||
1822713130 | 2008-04-18 | Honda engine on well now. Producing. | ||||
35623379 | 2003-09-15 | |||||
-504133228 | 2011-07-19 | Moran had set 350' clay plug at 2786'-2436' in 4.5' casing and then ripped 4.5 casing at 2450'. Pulled up to 900.8'. Cemenco set cement plug at 900'-700'. Pulled 4.5 casing out. The 8 5/8 head was loose. Will spear casing tomorrow. | ||||
-59479903 | 2011-07-15 | Moran Drilling called and said that packer would not come out. The 2 3/8 tubing is good, so placed the cement plug thru it and spotted a 200' plug on bottom. Then Jet Wireline shot the tubing off at 2786'. | ||||
-703266861 | 2011-07-21 | Rig is pulling 8 5/8 casing. Will check back tomorrow. | ||||
788698638 | 2011-12-28 | Final Restoration passed on 12-28-11 by Patrick Shreve. | ||||
PL8700 | Preliminary Restoration done information from Data Point |
For data sources see[2]