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Well ID: 34-059-24336 | Loading map...
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County: Guernsey | |
Municipality: | |
Operator Name: PDC ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2014-03-22 | |
Unconventional: | |
Configuration: | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 39.97828799 | |
Longitude: -81.42030285 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2015-1 | 91358.0 | 90.0 | 27315.0 | 90.0 | ||
2014-4 | 12374.0 | 13.0 | 3666.0 | 13.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1362768952 | 2014-10-21 | On the day of my inspection I witnessed that Halliburton Services was on site fracing stage 7 of 64 total stages. 104645lbs of propant was used at average treating rate of 30.7bpm and an average treating pressure of 7608psi. | ||||
1804821220 | 2014-09-15 | On the day of my inspection I witnessed that H&P Drilling Rig #385 had cemented their production string and was setting slips, preparing to rig down and begin move to the Cole pad. The site passed preliminary restoration according to ORC 1509.072A. | ||||
-2028188604 | 2015-02-27 | On the day of my inspection I witnessed that the well is online and equipped with a production tree with valves in the open position. Production equipment included a sand trap, a GP Unit, a vapor recovery system and a total of 12-500bbl tanks all within containment and shared with the 2H, 3H and 4H. The site passed preliminary restoration according to ORC 1509.072A. |
For data sources see[2]