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34-031-23253

Well Details

Well ID: 34-031-23253
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County: Coshocton
Municipality:
Operator Name: PRIME TIME ENERGY INVEST
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1978-05-22
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.32071512
Longitude: -82.15498461

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2001-0 0.0 359.0
2007-0 0.0 234.0
2008-0 0.0 156.0
2009-0 0.0 155.0
2010-0 0.0 196.0
2011-0 0.0 79.0
2012-0 0.0 155.0
2013-0 0.0 26.0
2014-0 0.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1421075561 2015-01-12 On the day of my inspection I found that there had been no change in the condition of this well. The lines at the wellhead were disconnected. The pulley belts on the pumping unit motor were slack. The polished rod showed no signs of recent use.
1529404490 2014-01-17 FOLLOW UP TO CA #-773610376: On the day of my inspection I found that a motor had been installed on the pump jack. The pulley belts were slack, the polished rod was dry and the bridle was rusted. There was 1 plastic line from permit 3941 connected to this well. Although a motor has been installed, the pump jack does not demonstrate evidence of use. The production records are exactly the same for this well as the Richards 2. The tank battery was freshly painted and identification was posted. I called Primetime Energy and left a voice message.
-601874437 2014-04-14 FOLLOW UP TO CA #-773610376: I have received no further correspondence from Prime Time Energy in regards to the status of this well. The pumping unit does no show any evidence of use. The belts are still slack and the polished rod is still dry. All of the lines from the casing and tubing are disconnected. In its current state this well is not capable of production. I attempted to make contact with the company again. There was no answer so I left another voice message.
-773610376 2013-04-18 On the day of my inspection I found that the well head was equipped with a pumping unit that was overgrown with vines and small trees. There were no belts on the pulley, no motor and the gear box was full of water. In its current state this well is incapable of production. This well shares a tank battery with permit 3941; however, no identification was posted at the well head or tank battery for this permit. Make well capable of commercial production within 30 days; or plugging is required within 90 days. Failure to comply may result in forfeiture of bond.
858352551 2014-08-13 On the day of my inspection I found that the pumping unit still did not show any evidence of use. The belts were still slack and the polished rod was still dry. I took photographs to show that all of the lines from the casing and tubing were still disconnected.
CEN2853 1998-07-13 1509.12

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.