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34-155-23128

Well Details

Well ID: 34-155-23128
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County: Trumbull
Municipality:
Operator Name: PAC DRILLING LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2012-02-11
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.18968987
Longitude: -80.55691029

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-0 10923.0 960.0
2013-0 14288.0 638.0
2014-0 12441.0 360.0 264.0 360.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1330438200 2012-02-17 The 4.5 production casing was successfully cemented. All conditions were satisfactory.
1333742789 2012-03-08 My inspection of this well site found that the pits were solidified using two loads of dust. There were no violations noted.
-134891047 2012-02-16 The rig was drilling on air at 4957'. There was a show of gas encountered at 4878'. All preparations have been made to convert to fluid, if needed. There were no violations.
1416250308 2012-02-27 The pits were in good condition. No problems were found.
1885617342 2012-02-13 The blowout preventer (BOP) was tested with 330 PSI for 20 minutes. During this test, a 10 PSI decline was observed. The drilling contractor was given instructions to repair leak and ensure the BOP would perform properly.
-911122073 2012-02-12 The surface casing installation and cementing was witnessed. The 8.675 casing was set at 723' and cemented with 260 sacks of cement. The cement operation and site conditions were acceptable.
957577052 2013-05-29 My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery contained one, 210 barrel production tank, one, 50 barrel brine tank, and a separator. It was surrounded by a locked chain link fence and the proper dike capable of meeting containment requirements. There was a plug on the load line. The proper safety equipment was installed on the production tank. An identification sign was properly posted at the wellhead and tank battery. There was a 7 day production chart at the separator. The site was graded and vegetated. All drainage and erosion controls were in place and working properly. The lease road was in good condition.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.