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Well ID: 34-155-23128 | Loading map...
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County: Trumbull | |
Municipality: | |
Operator Name: PAC DRILLING LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2012-02-11 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.18968987 | |
Longitude: -80.55691029 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-0 | 10923.0 | 960.0 | ||||
2013-0 | 14288.0 | 638.0 | ||||
2014-0 | 12441.0 | 360.0 | 264.0 | 360.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1330438200 | 2012-02-17 | The 4.5 production casing was successfully cemented. All conditions were satisfactory. | ||||
1333742789 | 2012-03-08 | My inspection of this well site found that the pits were solidified using two loads of dust. There were no violations noted. | ||||
-134891047 | 2012-02-16 | The rig was drilling on air at 4957'. There was a show of gas encountered at 4878'. All preparations have been made to convert to fluid, if needed. There were no violations. | ||||
1416250308 | 2012-02-27 | The pits were in good condition. No problems were found. | ||||
1885617342 | 2012-02-13 | The blowout preventer (BOP) was tested with 330 PSI for 20 minutes. During this test, a 10 PSI decline was observed. The drilling contractor was given instructions to repair leak and ensure the BOP would perform properly. | ||||
-911122073 | 2012-02-12 | The surface casing installation and cementing was witnessed. The 8.675 casing was set at 723' and cemented with 260 sacks of cement. The cement operation and site conditions were acceptable. | ||||
957577052 | 2013-05-29 | My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery contained one, 210 barrel production tank, one, 50 barrel brine tank, and a separator. It was surrounded by a locked chain link fence and the proper dike capable of meeting containment requirements. There was a plug on the load line. The proper safety equipment was installed on the production tank. An identification sign was properly posted at the wellhead and tank battery. There was a 7 day production chart at the separator. The site was graded and vegetated. All drainage and erosion controls were in place and working properly. The lease road was in good condition. |
For data sources see[2]