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34-031-27224

Well Details

Well ID: 34-031-27224
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County: Coshocton
Municipality:
Operator Name: SAMPLES JAMES F
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-07-26
Unconventional: No
Configuration: Vertical
Well Status: Well Drilled
Violations: 0
Latitude: 40.33543101
Longitude: -82.13312185

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2014-0 0.0 365.0 581.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1061852334 2013-08-26 On the day of my inspection I found that the well was shut in with a 4 to 2 swedge and ball valve. The drilling pits were still open and full of fluid. There were no sags or tears in the pit liners and I found no leaks or spills around the drill site.
1123545125 2013-08-07 On the day of my inspection I found that H&D Drilling was making repairs to the drilling rig. They topped off the surface casing annulus with 10 bags of sack cement. They had not yet drilled out from under the surface casing. The permit was on display, the pit liner was in good shape and there were no leaks or spills.
1236489807 2013-08-01 On the day of my inspection I found that H&D Drilling had drilled a 10 hole to 594'. They ran new 7 casing. Formation Cementing pumped gel, cotton seed hulls and cello flake. They established circulation and pumped 210 sacks of cement. Good circulation was maintained throughout the job and there were approximately 3 barrels of cement returns. The casing passed the pressure test once the plug was landed.
-124661259 2013-08-19 On the day of my inspection I found that H&D Drilling was in the process of rigging down. They set 4.5 production casing at 3487' on 8/17/13. The well head was shut in with a 4 to 2 swedge, equipped with a ball valve. The permit was on display, there were no sags or tears in the pit liner and there were no leaks or spills.
-1903167957 2013-08-13 On the day of my inspection H&D Drilling was drilling a 6.5 hole on air with a power swivel. They were at a depth of 2177'. The permit was on display, the pit liner was in good shape and there were no leaks or spills.
-2045896771 2013-10-29 On the day of my inspection I found that the drill site was graded out and the pit was closed. All drilling equipment and materials were removed from the location. The well was equipped with a pumping unit. There was no vegetative cover. This site does not pass preliminary restoration at this time.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.