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34-059-24395

Well Details

Well ID: 34-059-24395
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County: Guernsey
Municipality:
Operator Name: PDC ENERGY INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-07-03
Unconventional: No
Configuration: Vertical
Well Status: Drilling
Violations: 0
Latitude: 40.04359996
Longitude: -81.38108794

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1520680408 2015-04-06 On the day of my inspection accompanied by ODNR Inspector Matt Fulk, I witnessed that Mountain States Pressure Services & Well Services Rig # 168-03 was replacing rams on the BOP with drilling out the 1st kill plug set at 7080 feet to follow. The 2nd kill plug is set at 7120 feet and the 1st frac plug set at 7980 feet.
-1650802951 2014-07-29 On the day of my inspection accompanied by ODNR Southeast Regional Supervisor Rocky King, I met with Company Man Randall Downen and discussed upcoming surface string and cementing. First Class Drilling Rig #6 was drilling a 24 inch diameter hole on air at 103 feet with a planned td of 544 feet.
1779677126 2014-07-30 On the day of my inspection accompanied by ODNR Inspector Justin Smith, I witnessed that First Class Drilling Rig #6 had drilled a 24 inch diameter surface hole to the depth of 544 feet and ran 544 feet of 20 inch 94#/ft. casing and had to wash down the last 5 feet . Universal Well Services was on site and gained circulation with 25bbls of gel, 5bbls of fresh water and cemented casing with 706 sacks of Type 1 cement with 3% CaCl and .25#/sk. of cello flake. While dropping the plug they believed it kicked sideways so the cement was displaced with 183bbls of fresh water. Had good cement returns of 35bbls to surface and no pressure test was performed. Cement head was shut in and they were instructed to leave shut in for 8 hours and complete pressure test.
-1853968162 2014-07-30 I accompanied Doug Bennett on the inspection of this well today.
-428770419 2014-11-17 On the day of my inspection I witnessed that H&P Flex Rig #385 had completed running and cementing their production string on the Cole 1H and successfully skidded back to the Cole 2H. BOP stack has been moved and preparations being made to begin testing.
789526840 2015-04-22 On the day of my inspection the site passed preliminary restoration according to ORC 1509.072A.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.