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34-059-23971

Well Details

Well ID: 34-059-23971
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County: Guernsey
Municipality:
Operator Name: HILL DAVID R INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2004-09-08
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.9220235
Longitude: -81.55642123

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2005-0 4619.0 424.0
2006-0 605.0 242.0
2007-0 514.0 77.0
2008-0 621.0 199.0
2009-0 610.0 101.0
2010-0 505.0 0.0
2011-0 421.0 99.0
2012-0 322.0 0.0
2013-0 317.0 0.0
2014-0 254.0 365.0 73.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1006172039 2005-10-13 PRELIMINARY RESTORATION
1095203615 2004-09-14 PINNACLE DRILLING, DRILLING AT 2460'
1275163929 2010-05-28 Received phone call from local authorities concerning lightening striking oil tank and tank exploded releasing contents within dike area. Upon arriving on site along with local fire departments found tank on fire and contents running toward local creek, we contained oil before it entered creek up until the point that water and foam forced flames into creek bed .30-40 bbl oil was thought to have been in tank at time of storm, stayed on site until fire was out, called Dennis Deaver of Ohio EPA and informed him of accident and what clean up efforts were being applied at scene, will check on site tomorrow and check creek and dike area for oil and witness clean up efforts.
-1458274770 2008-07-08 WELLIS BACK IN PRODUCTION. CATTLE TEARING UP LEASE ROAD.
-545144446 2013-04-10 On the day of my inspection I reviewed the Divisions production records and found they were current, there is a pumping unit at the well and all the valves are open, there is a separator/ drip/ chart/ compressor setting out side of the containment dike, there is (1) one hundred barrel production tank and (1) fifty barrel plastic brine tank setting inside the containment dike, the I.D. is posted on the tank.
-768240495 2010-06-08 Inspection revealed that tank site has been recently changed from original position to current site, owner decided to move tank site in light of recent lightning strike and tank fire.

Well is equipped with pumping unit and tubing and rods and 1-100 bbltank and 1-50 bbl water tank with dike in place.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.