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Well ID: 34-013-20923 | Loading map...
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Last Permit Date: | |
Spud Date: 2015-03-01 | |
Unconventional: | |
Configuration: | |
Well Status: Well Drilled | |
Violations: 0 | |
Latitude: 40.12046485 | |
Longitude: -81.17384981 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1224450560 | 2015-03-03 | On this day the 18.625 casing was cemented in a 24 open hole to a depth of 326'. Calfrac ran 1500 sks of class A cement with cement to surface established. See cement ticket for details. No violations noted. | ||||
1423956268 | 2015-02-14 | On the date of inspection I was informed by Antero consultant Jason Bussey that Rocky Mountain Drilling has drilled a 32 inch diameter hole to a depth of 103 feet. According to Jason, no water was encountered during drilling. Rocky Mountain set 103 feet of 26 inch diameter, 102.5lbs/ft conductor pipe on bottom. I field titrated the mix/displacement water for chlorides which were at a level of 125ppm. Allied Oil & Gas services pumped 242sk of Class A cement, 15.6ppg, 1.18 yield, 2% CaCl2, and 0.25lbs/sk of flake. Allied displaced cement with 55bbl of fresh water. 5bbl of cement returned to surface. | ||||
1626477872 | 2015-03-02 | Current operations are drilling in the 24 |
For data sources see[1]