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37-129-28459

Well Details

Well ID: 37-129-28459
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Hempfield Township
Operator Name: PENNECO OIL CO INC
Well Pad ID:
Farm/Lease Name: BENYAK 3
License Status: Active
Spud Date: 02/21/2011
Permit Date: 11/5/2010
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.323889
Longitude: -79.661083

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2010 0.00 0.00 0.00
2011 PENNECO OIL CO INC 6,062.00 245 0.00 0.00
2012 PENNECO OIL CO INC 8,982.00 366 0.00 0.00
2013 PENNECO OIL CO INC 9,050.00 365 0.00 0.00
2014 PENNECO OIL CO INC 7,148.00 365 0.00 0.00
2015 PENNECO OIL CO INC 4,291.03 365 0.00 0.00
2016 PENNECO OIL CO INC 6,681.51 366 0.00 0.00
2017 PENNECO OIL CO INC 5,633.00 365 0.00 0.00
2018 PENNECO OIL CO INC 4,913.81 365 0.00 0.00

For data sources see[4]

Waste Data

Period Waste Type Quantity Disposal Method Waste Facility ID
2011-A00 Drilling Fluid Waste (in Barrels) 5,530.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472
2011-A00 Produced Fluid (in Barrels) 180.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2012-A00 Produced Fluid (in Barrels) 265.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508
2013-A00 Produced Fluid (in Barrels) 75.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095443
2014-A00 Produced Fluid (in Barrels) 50.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095443
2017-A00 Produced Fluid (in Barrels) RWC 802 57.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1952073 Primary Facility 02/24/2011 Routine/Complete Inspection No Violations Noted Problems getting Pipe threw Mine . Redrilled hole landed pipe , completed a successful balance job
1956098 Primary Facility 02/23/2011 Drilling/Alteration No Violations Noted US ENERGY DRILLING ON PENNECO PAD, DEPTH 270' TRYING TO GET 95/8"THROUGH THE FLOODED MINE.
1956101 Primary Facility 03/01/2011 Drilling/Alteration No Violations Noted US ENERGY DRILLING ON PENNECO PAD, RAN 270' OF 95/8 BASKET AT 210'. CURRENT DEPTH 1946'
1956123 Primary Facility 03/09/2011 Drilling/Alteration No Violations Noted US ENERGY DRILLING ON PENNECO PAD, RAN 2318' OF 7" CSG. BASKET AT 84'. CURRENT DEPTH 2318'
1959617 Primary Facility 03/16/2011 Routine/Complete Inspection No Violations Noted Site visit was part of routine inspection.
1961057 Primary Facility 03/16/2011 Routine/Complete Inspection No Violations Noted Site visit was part of routine inspection.
1967084 Primary Facility 04/15/2011 Routine/Complete Inspection No Violations Noted Site visit was part of routine inspection.
1967093 Primary Facility 04/15/2011 Routine/Complete Inspection No Violations Noted Site visit was part of routine inspection.
1970652 Primary Facility 04/19/2011 Routine/Complete Inspection No Violations Noted WQS MARK MAESTRA CALLED AND TOLD ME THAT THE WELL HEAD IS LEAKING. I TALKED WITH THE WELL TENDER AND HE SAID HE WOULD LET HIS SUPERVISOR KNOW ABOUT THE PROBLEM.
1971935 Primary Facility 04/19/2011 Routine/Complete Inspection Pending Site visit was in coordination with Jason Branan to check on leaking gas well. Leak appeared to have lessened.

For data sources see[6]

References