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34-031-24588

Well Details

Well ID: 34-031-24588
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Country: United States
State: Ohio
County: Coshocton
Municipality: Tiverton Township
Operator Name: W H PATTEN DRILLING CO
Well Pad ID:
Farm/Lease Name: EDWARDS TOM
License Status: Final Restoration
License Date: 2014-09-12
Spud Date: 1982-03-15
Spud Drilling Contractor:
Final Drill Date: 1982-05-12
Well Total Depth: 3375 ft
Configuration: Vertical
Latitude: <Latitude>
Longitude: -82.14153951

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-10-13 372 PATTEN W H DRLG CO GeoDate 10/13/81
Original Spud 1982-03-15 UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017.
Completed 1982-05-12 UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017.
Reached Total Depth 1982-05-12 UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017.
APP 2014-09-12 Proposed Formations:CLINTON, Issued Date:9/12/2014, Expired Date:9/11/2016 12:00:00 PM, Drilling unit acres:52.6, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-10-09 UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017.
Construction Permit Expires 2016-09-11 UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017.
Record Last Modified 2017-03-29 UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2300 Bbl 28000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 JONSU OIL CORP 1838 539 365
1986 W H PATTEN DRILLING CO 1217 458 156
1987 W H PATTEN DRILLING CO 1517 363 156
1988 W H PATTEN DRILLING CO 932 221 156
1989 W H PATTEN DRILLING CO 568 223 156
1990 W H PATTEN DRILLING CO 579 223 156
1991 W H PATTEN DRILLING CO 577 152 156
1992 W H PATTEN DRILLING CO 414 156 156
1993 W H PATTEN DRILLING CO 435 230 156
1994 W H PATTEN DRILLING CO 420 150 156
1995 W H PATTEN DRILLING CO 267 74 156
1996 W H PATTEN DRILLING CO 397 148 365
1997 W H PATTEN DRILLING CO 161 75 365
1998 W H PATTEN DRILLING CO 251 80 365
1999 W H PATTEN DRILLING CO 41 88 365
2000 W H PATTEN DRILLING CO 83 78 365
2001 W H PATTEN DRILLING CO 101 97 365
2002 W H PATTEN DRILLING CO 10 0 365
2003 W H PATTEN DRILLING CO 28 0 365
2004 W H PATTEN DRILLING CO 36 69 365
2005 W H PATTEN DRILLING CO 44 0 365
2006 W H PATTEN DRILLING CO 521 0 365
2007 W H PATTEN DRILLING CO 117 0 365
2008 W H PATTEN DRILLING CO 17 0 365
2009 W H PATTEN DRILLING CO 126 0 365
2010 W H PATTEN DRILLING CO 216 0 365
2011 W H PATTEN DRILLING CO 224 0 365
2012 W H PATTEN DRILLING CO 262 0 366
2013 W H PATTEN DRILLING CO 220 0 365
2014 W H PATTEN DRILLING CO 231 0 365
2015 W H PATTEN DRILLING CO 0 0 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 JONSU OIL CORP Brine 18 365
1986 W H PATTEN DRILLING CO Brine 336 156
1987 W H PATTEN DRILLING CO Brine 248 156
1988 W H PATTEN DRILLING CO Brine 280 156
1989 W H PATTEN DRILLING CO Brine 200 156
1990 W H PATTEN DRILLING CO Brine 240 156
1991 W H PATTEN DRILLING CO Brine 160 156
1992 W H PATTEN DRILLING CO Brine 200 156
1993 W H PATTEN DRILLING CO Brine 120 156
1994 W H PATTEN DRILLING CO Brine 168 156
1995 W H PATTEN DRILLING CO Brine 90 156
1996 W H PATTEN DRILLING CO Brine 115 365
1997 W H PATTEN DRILLING CO Brine 150 365
1998 W H PATTEN DRILLING CO Brine 110 365
1999 W H PATTEN DRILLING CO Brine 45 365
2000 W H PATTEN DRILLING CO Brine 170 365
2001 W H PATTEN DRILLING CO Brine 150 365
2002 W H PATTEN DRILLING CO Brine 278 365
2003 W H PATTEN DRILLING CO Brine 45 365
2004 W H PATTEN DRILLING CO Brine 50 365
2005 W H PATTEN DRILLING CO Brine 95 365
2006 W H PATTEN DRILLING CO Brine 0 365
2007 W H PATTEN DRILLING CO Brine 0 365
2008 W H PATTEN DRILLING CO Brine 0 365
2009 W H PATTEN DRILLING CO Brine 0 365
2010 W H PATTEN DRILLING CO Brine 0 365
2011 W H PATTEN DRILLING CO Brine 0 365
2012 W H PATTEN DRILLING CO Brine 0 366
2013 W H PATTEN DRILLING CO Brine 100 365
2014 W H PATTEN DRILLING CO Brine 105 365
2015 W H PATTEN DRILLING CO Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0271849541 2015-06-22 Final Restoration No Violations On the day of my inspection I found that the well site and lease road were growing with well established tall grasses and broadleaf vegetation. I found no signs of erosion. This site passes final restoration.
0703910390 2014-10-07 Plug / Plug Back No Violations At the request of the Coshocton Co. inspector who had other commitments, I witnessed the perforation of the 7 casing that was eaten off at 63 and unable to be removed from the well. Timco perforated from 860 to 760 every 25. They also perforated from 550 to 100 every 25. There were 3 holes shot at each 25 interval. The cementers were not available to spot the cement plugs over the intervals this date.
1041635192 2014-10-07 Plug / Plug Back No Violations ODNR Inspector Todd Miller witnessed Timco perforating the 7 casing through the Berea and through the Big Injun.
1046209796 2015-05-06 Final Restoration No Violations On the day of my inspection I found that the site had been graded and seeded. The production equipment had been removed. Grass growth was sparse. I called Billy Patten. He claimed that they were recently in to re-seed the site.
1118466544 2014-09-10 Plug / Plug Back No Violations On the day of my inspection I found that Gene Matheney was rigged up ready to plug the well. They are waiting on the permit.
1224208407 2014-10-08 Plug / Plug Back No Violations On the day of my inspection Gene Matheny ran 1.5 tubing to 1160. Petroset established circulation and pumped 100 sacks of class A cement to set a Berea plug in perforated 7 casing. Good circulation was maintained throughout the job.
1254743886 2014-01-22 Production Wells Violations Noted On the day of my inspection I found that there was a gas leak at the well head from a rusted fitting. There was a slow drip of brine from the plug in the stock tank, and there was no identification posted. I contacted Billy Patten to request that he fix the leaks at the well head and tank battery, and post proper identification.
1298045717 2014-01-22 Production Wells No Violations I received a request from Amy Edwards to inspect an unknown well on her property. She had knowledge of permit 4588, but claimed that there was another well there that was not on ODNR oil and gas well maps. I conducted an inspection of the site and found only one well. I contacted Ms. Edwards to get a better description of the location of the unknown well. Through conversation I came to the realization that she was referring to the storage tanks in the tank battery as individual wells. The mystery of the unknown well was solved once I educated Ms. Edwards on the correct nomenclature of an oil & gas well.
1362670101 2013-03-07 Production Wells Violations Noted On the day of my inspection I found that the well head was equipped with a pumping unit. The tank battery consisted of two 100 barrel stock tanks, one 30 barrel brine tank, one separator and an earthen dike. There were no leaks or spills and proper identification was posted. One of the stock tanks was heavily rusted and had multiple holes in it. I called Billy Patten to request that the tank be removed.
1367516684 2013-05-02 Production Wells No Violations FOLLOW UP TO CA # 1362670101: On the day of my inspection I found that nothing had been done to correct the issued described in the compliance notice. I called Billy Patten, who claimed that it was on the list of things to do.
1381337654 2013-05-28 Production Wells No Violations FOLLOW UP TO CA # 1362670101: On the day of my inspection I found that the rusted stock tank had been removed. This violation is resolved.
1412172345 2014-10-01 Plug / Plug Back No Violations Gene Matheny reported that the top joint of the 7 casing had been removed at some point in the wells history. The top of the 7 casing was visible approximately 15 down. Matheny went in with a joint equipped with a steel die nipple to screw into the top of the 7 casing. When they started to pull the casing came freely with no significant reading on the weight indicator. They pulled up to the nipple and found that they were screwed into the casing. The lack of weight indicated that the 7 casing is parted further down the hole.
1412606973 2014-10-06 Plug / Plug Back No Violations On the day of my inspection Gene Matheny pulled the 7 casing and found that the casing was rotted off 63 down hole. They went in with 8 casing and got over the top of the 7 where it was parted. Then they went in with their 4 tools and was able to get inside of the 7 casing. The casing will need to be perforated through the Berea and through the Big Injun in order to open the casing up for cement plugs.
1412887785 2014-10-09 Plug / Plug Back No Violations On the day of my inspection Gene Matheny tagged the Berea plug at 713. They pulled the tubing up to 570. Petroset established circulation and pumped till cement was circulated to surface. The job took 245 sacks of class A cement. The cement had fallen approximately 30 feet by the time Matheny pulled the tubing. They topped the well off with fire clay.
1644970946 2014-04-10 Production Wells No Violations FOLLOW UP TO CA # -1254743886: On the day of my inspection I found that the leaks had been stopped and identification was posted on the storage tank. This violation is resolved.
1649431107 2014-09-24 Plug / Plug Back No Violations On the day of my inspection Gene Matheny washed 2 tons of clay down the 4.5 casing.
1667701977 2016-10-12 Final Restoration No Violations On the day of my inspection I escorted surveyor Tom Smith to the plugged well site in order to mark the location with a flagged stake at the final recorded GPS coordinates. I found that the vegetation was well established and there were no signs of erosion. There was no evidence that the plugged well was leaking.
2069300633 2014-09-30 Plug / Plug Back No Violations On the day of my inspection Gene Matheny ripped the 4.5 casing at 1736. They pulled 15 joints and washed another 3 tons of clay down the well for the bottom plug.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1254743886 US-OH-106863 2014-04-23 Well operation causing pollution and contamination
1254743886 US-OH-106864 2014-04-23 Failure to legibly identify well
1362670101 US-OH-110596 2013-05-28 General Safety

For data sources see[8]

References