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Well ID: 34-031-24588 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Tiverton Township | |
Operator Name: W H PATTEN DRILLING CO | |
Well Pad ID: | |
Farm/Lease Name: EDWARDS TOM | |
License Status: Final Restoration | |
License Date: 2014-09-12 | |
Spud Date: 1982-03-15 | |
Spud Drilling Contractor: | |
Final Drill Date: 1982-05-12 | |
Well Total Depth: 3375.00 ft | |
Configuration: Vertical | |
Latitude: 40.430000 | |
Longitude: -82.140000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-10-13 | 372 PATTEN W H DRLG CO GeoDate 10/13/81 |
Original Spud | 1982-03-15 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
Completed | 1982-05-12 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
Reached Total Depth | 1982-05-12 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
APP | 2014-09-12 | Proposed Formations:CLINTON, Issued Date:9/12/2014, Expired Date:9/11/2016 12:00:00 PM, Drilling unit acres:52.6, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-10-09 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
Construction Permit Expires | 2016-09-11 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
Record Last Modified | 2017-03-29 | UPDATE LOCATION PER SURVEYOR-ALE 03/29/2017. |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2300 Bbl | 28000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | JONSU OIL CORP | 1838.00 | 539.00 | 365 |
1986 | W H PATTEN DRILLING CO | 1217.00 | 458.00 | 156 |
1987 | W H PATTEN DRILLING CO | 1517.00 | 363.00 | 156 |
1988 | W H PATTEN DRILLING CO | 932.00 | 221.00 | 156 |
1989 | W H PATTEN DRILLING CO | 568.00 | 223.00 | 156 |
1990 | W H PATTEN DRILLING CO | 579.00 | 223.00 | 156 |
1991 | W H PATTEN DRILLING CO | 577.00 | 152.00 | 156 |
1992 | W H PATTEN DRILLING CO | 414.00 | 156.00 | 156 |
1993 | W H PATTEN DRILLING CO | 435.00 | 230.00 | 156 |
1994 | W H PATTEN DRILLING CO | 420.00 | 150.00 | 156 |
1995 | W H PATTEN DRILLING CO | 267.00 | 74.00 | 156 |
1996 | W H PATTEN DRILLING CO | 397.00 | 148.00 | 365 |
1997 | W H PATTEN DRILLING CO | 161.00 | 75.00 | 365 |
1998 | W H PATTEN DRILLING CO | 251.00 | 80.00 | 365 |
1999 | W H PATTEN DRILLING CO | 41.00 | 88.00 | 365 |
2000 | W H PATTEN DRILLING CO | 83.00 | 78.00 | 365 |
2001 | W H PATTEN DRILLING CO | 101.00 | 97.00 | 365 |
2002 | W H PATTEN DRILLING CO | 10.00 | 0.00 | 365 |
2003 | W H PATTEN DRILLING CO | 28.00 | 0.00 | 365 |
2004 | W H PATTEN DRILLING CO | 36.00 | 69.00 | 365 |
2005 | W H PATTEN DRILLING CO | 44.00 | 0.00 | 365 |
2006 | W H PATTEN DRILLING CO | 521.00 | 0.00 | 365 |
2007 | W H PATTEN DRILLING CO | 117.00 | 0.00 | 365 |
2008 | W H PATTEN DRILLING CO | 17.00 | 0.00 | 365 |
2009 | W H PATTEN DRILLING CO | 126.00 | 0.00 | 365 |
2010 | W H PATTEN DRILLING CO | 216.00 | 0.00 | 365 |
2011 | W H PATTEN DRILLING CO | 224.00 | 0.00 | 365 |
2012 | W H PATTEN DRILLING CO | 262.00 | 0.00 | 366 |
2013 | W H PATTEN DRILLING CO | 220.00 | 0.00 | 365 |
2014 | W H PATTEN DRILLING CO | 231.00 | 0.00 | 365 |
2015 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1041635192 | 2014-10-7 0:00: | PB | No Violations | |
-1046209796 | 2015-5-6 0:00:0 | FR | No Violations | |
-1224208407 | 2014-10-8 0:00: | PB | No Violations | |
-1254743886 | 2014-1-22 0:00: | PW | No Violations | |
-1381337654 | 2013-5-28 0:00: | PW | No Violations | |
-1644970946 | 2014-4-10 0:00: | PW | No Violations | |
-1649431107 | 2014-9-24 0:00: | PB | No Violations | |
-2069300633 | 2014-9-30 0:00: | PB | No Violations | |
-271849541 | 2015-6-22 0:00: | FR | No Violations | |
0271849541 | 2015-06-22 | Final Restoration | No Violations | On the day of my inspection I found that the well site and lease road were growing with well established tall grasses and broadleaf vegetation. I found no signs of erosion. This site passes final restoration. |
0703910390 | 2014-10-07 | Plug / Plug Back | No Violations | At the request of the Coshocton Co. inspector who had other commitments, I witnessed the perforation of the 7 casing that was eaten off at 63 and unable to be removed from the well. Timco perforated from 860 to 760 every 25. They also perforated from 550 to 100 every 25. There were 3 holes shot at each 25 interval. The cementers were not available to spot the cement plugs over the intervals this date. |
1041635192 | 2014-10-07 | Plug / Plug Back | No Violations | ODNR Inspector Todd Miller witnessed Timco perforating the 7 casing through the Berea and through the Big Injun. |
1046209796 | 2015-05-06 | Final Restoration | No Violations | On the day of my inspection I found that the site had been graded and seeded. The production equipment had been removed. Grass growth was sparse. I called Billy Patten. He claimed that they were recently in to re-seed the site. |
1118466544 | 2014-09-10 | Plug / Plug Back | No Violations | On the day of my inspection I found that Gene Matheney was rigged up ready to plug the well. They are waiting on the permit. |
1224208407 | 2014-10-08 | Plug / Plug Back | No Violations | On the day of my inspection Gene Matheny ran 1.5 tubing to 1160. Petroset established circulation and pumped 100 sacks of class A cement to set a Berea plug in perforated 7 casing. Good circulation was maintained throughout the job. |
1254743886 | 2014-01-22 | Production Wells | Violations Noted | On the day of my inspection I found that there was a gas leak at the well head from a rusted fitting. There was a slow drip of brine from the plug in the stock tank, and there was no identification posted. I contacted Billy Patten to request that he fix the leaks at the well head and tank battery, and post proper identification. |
1298045717 | 2014-01-22 | Production Wells | No Violations | I received a request from Amy Edwards to inspect an unknown well on her property. She had knowledge of permit 4588, but claimed that there was another well there that was not on ODNR oil and gas well maps. I conducted an inspection of the site and found only one well. I contacted Ms. Edwards to get a better description of the location of the unknown well. Through conversation I came to the realization that she was referring to the storage tanks in the tank battery as individual wells. The mystery of the unknown well was solved once I educated Ms. Edwards on the correct nomenclature of an oil & gas well. |
1362670101 | 2013-03-07 | Production Wells | Violations Noted | On the day of my inspection I found that the well head was equipped with a pumping unit. The tank battery consisted of two 100 barrel stock tanks, one 30 barrel brine tank, one separator and an earthen dike. There were no leaks or spills and proper identification was posted. One of the stock tanks was heavily rusted and had multiple holes in it. I called Billy Patten to request that the tank be removed. |
1367516684 | 2013-05-02 | Production Wells | No Violations | FOLLOW UP TO CA # 1362670101: On the day of my inspection I found that nothing had been done to correct the issued described in the compliance notice. I called Billy Patten, who claimed that it was on the list of things to do. |
1381337654 | 2013-05-28 | Production Wells | No Violations | FOLLOW UP TO CA # 1362670101: On the day of my inspection I found that the rusted stock tank had been removed. This violation is resolved. |
1412172345 | 2014-10-01 | Plug / Plug Back | No Violations | Gene Matheny reported that the top joint of the 7 casing had been removed at some point in the wells history. The top of the 7 casing was visible approximately 15 down. Matheny went in with a joint equipped with a steel die nipple to screw into the top of the 7 casing. When they started to pull the casing came freely with no significant reading on the weight indicator. They pulled up to the nipple and found that they were screwed into the casing. The lack of weight indicated that the 7 casing is parted further down the hole. |
1412606973 | 2014-10-06 | Plug / Plug Back | No Violations | On the day of my inspection Gene Matheny pulled the 7 casing and found that the casing was rotted off 63 down hole. They went in with 8 casing and got over the top of the 7 where it was parted. Then they went in with their 4 tools and was able to get inside of the 7 casing. The casing will need to be perforated through the Berea and through the Big Injun in order to open the casing up for cement plugs. |
1412887785 | 2014-10-09 | Plug / Plug Back | No Violations | On the day of my inspection Gene Matheny tagged the Berea plug at 713. They pulled the tubing up to 570. Petroset established circulation and pumped till cement was circulated to surface. The job took 245 sacks of class A cement. The cement had fallen approximately 30 feet by the time Matheny pulled the tubing. They topped the well off with fire clay. |
1644970946 | 2014-04-10 | Production Wells | No Violations | FOLLOW UP TO CA # -1254743886: On the day of my inspection I found that the leaks had been stopped and identification was posted on the storage tank. This violation is resolved. |
1649431107 | 2014-09-24 | Plug / Plug Back | No Violations | On the day of my inspection Gene Matheny washed 2 tons of clay down the 4.5 casing. |
1667701977 | 2016-10-12 | Final Restoration | No Violations | On the day of my inspection I escorted surveyor Tom Smith to the plugged well site in order to mark the location with a flagged stake at the final recorded GPS coordinates. I found that the vegetation was well established and there were no signs of erosion. There was no evidence that the plugged well was leaking. |
2069300633 | 2014-09-30 | Plug / Plug Back | No Violations | On the day of my inspection Gene Matheny ripped the 4.5 casing at 1736. They pulled 15 joints and washed another 3 tons of clay down the well for the bottom plug. |
703910390 | 2014-10-7 0:00: | PB | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1254743886 | US-OH-106863 | 2014-04-23 | Well operation causing pollution and contamination | |
1254743886 | US-OH-106864 | 2014-04-23 | Failure to legibly identify well | |
1362670101 | US-OH-110596 | 2013-05-28 | General Safety |
For data sources see[8]