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| Well ID: 0174131414020 | Loading map...
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| Location: 02/14-14-017-13W4/0 | |
| Location Alias: 02/14-14-17-13 W4M | |
| Location Alias 2: 02/14-14-017-13 W4/00 | |
| Country: Canada | |
| Province: Alberta | |
| Township: 017 | |
| Meridian: 4 | |
| Range: 13 | |
| Section: 14 | |
| County/Municipality: County of Newell | |
| Well Name: CARDINAL 102 BANTRY 14-14-17-13 | |
| Operator Name: Cardinal Energy Ltd. | |
| License Number: 0481460 | |
| License Date: 2016-11-16 | |
| License Status: Issued | |
| Spud Date: 2016-11-18 | |
| Final Drill Date: 2016-11-26 | |
| Well Total Depth: 2621.00 m | |
| Surface Hole Latitude: 50.423722 | |
| Surface Hole Longitude: -111.694564 |
| Date | Event |
|---|---|
| 2016-11-16 | Obtained License |
| 2016-11-19 | Surface Casing Operation Performed |
| 2016-11-20 | Direction Drilling Operation Performed - Deviate |
| 2016-11-22 | Direction Drilling Operation Performed - Horizontal |
| 2016-11-22 | Intermediate Casing Operation Performed |
| 2016-11-22 | Well Log Performed |
| 2016-11-26 | Finished Drilling |
| 2016-11-26 | Well Log Performed |
| 2016-11-26 | Well Mode changed to Drilled and Cased |
| 2016-11-27 | Liner Casing Operation Performed |
| 2016-11-28 | Perforation Treatment Performed - Open-Hole Completion |
| 2016-11-28 | Rig Released |
| 2016-12-09 | Perforation Treatment Performed - Multi-Stage Fracture |
| 2016-12-19 | Well Began Production |
| 2016-12-19 | Well Fluid changed to Crude Oil |
| 2016-12-19 | Well Mode changed to Pumping |
| 2018-07-06 | Perforation Treatment Performed - Acid Squeeze - Press Used |
For data sources see[3]
| Spud Date | Contractor | Rig Number | New Projected Depth (m) | Activity Type |
|---|---|---|---|---|
| 2016-11-18 | Quintera Drilling Ltd. | 3 | N/A | Drill To LD |
For data sources see[4]
| Start Date | Depth (m) | Reason |
|---|---|---|
| 2016-11-20 | 670.60 | Deviate (5 - 79 degrees) |
| 2016-11-22 | 1182.30 | Horizontal |
For data sources see[5]
| Perforation Date | Perforation Type | Interval Top (m) | Interval Base (m) | Number of Shots |
|---|---|---|---|---|
| 2016-11-28 | Open Hole/Barefoot Completion | 2611.00 | 2621.00 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 1941.40 | 1942.30 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 1858.50 | 1859.40 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 1529.10 | 1530.00 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 1457.00 | 1457.80 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 1371.10 | 1371.90 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 1298.60 | 1299.50 | 0 |
| 2018-07-06 | Acid Treatment | 1298.60 | 2621.00 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 2601.80 | 2603.10 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 2500.40 | 2501.30 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 2414.30 | 2415.10 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 2328.90 | 2329.70 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 2256.40 | 2257.20 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 2170.40 | 2171.30 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 2097.40 | 2098.20 | 0 |
| 2016-12-09 | Multi-Stage Fracture | 2011.70 | 2012.60 | 0 |
For data sources see[6]
| Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
|---|---|---|---|---|---|
| 1 | 2016-12-09 | 2016-12-09 | 963 | 1,226 | N/A |
| Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
|---|---|---|---|---|---|---|---|---|
| 1 | N2 | 7727-37-9 | 100 | 2.1712 | N/A | |||
| water | Not Available | 100 | 73.9058 | N/A | ||||
| CRC-LT (20/40) | Trican | phenolic resin | 9003-35-4 | 100 | 22.9787 | N/A | ||
| silica crystalline | 14808-60-7 | 100 | 22.9787 | N/A | ||||
| Activator-W | Trican | Activator | alcohols. C12-14-secondary. ethoxylated | 84133-50-6 | 100 | 0.2865 | N/A | |
| methanol | 67-56-1 | 100 | 0.2865 | N/A | ||||
| polyethylene glycol | 25322-68-3 | 100 | 0.2865 | N/A | ||||
| BXL-A | Trican | Breaker | diethanolamine | 111-42-2 | 100 | 0.0789 | N/A | |
| non-hazardous ingredients | Not Available | 100 | 0.0789 | N/A | ||||
| triethanolamine | 102-71-6 | 100 | 0.0789 | N/A | ||||
| WBO-2 | Trican | Breaker | sodium persulfate | 7775-27-1 | 100 | 0.0365 | N/A | |
| CC-8 | Trican | Clay Control | choline chloride | 67-48-1 | 100 | 0.1382 | N/A | |
| non-hazardous ingredients | Not Available | 100 | 0.1382 | N/A | ||||
| WXB-10 | Trican | Crosslinker | borate salts | 1319-33-1 | 100 | 0.1841 | N/A | |
| distillates (petroleum). hydrotreated light | 64742-47-8 | 100 | 0.1841 | N/A | ||||
| DF-2W | Trican | Defoamer | non-hazardous ingredients | Not Available | 100 | 0.0075 | N/A | |
| propylene glycol | 57-55-6 | 100 | 0.0075 | N/A | ||||
| WG-111DA | Trican | Gelling Agent | fumaric acid | 110-17-8 | 100 | 0.1753 | N/A | |
| guar gum | 9000-30-0 | 100 | 0.1753 | N/A | ||||
| S-17W | Trican | Surfactant | ethylene/propylene oxide polymer | Not Available | 100 | 0.0367 | N/A | |
| methanol | 67-56-1 | 100 | 0.0367 | N/A | ||||
| water | Not Available | 100 | 0.0367 | N/A |
For data sources see[7]
| Water Diversion Start Date | Water Diversion End Date | Water Source Type | Total Water Volume (m3) |
|---|---|---|---|
| 2016-12-01 | 2016-12-09 | Municipal Water | 386 |
| 2016-12-01 | 2016-12-01 | Recycled Fracturing Water (treated at well site) | 402 |
| 2016-12-01 | 2016-12-03 | Municipal Water | 527 |
For data sources see[8]
| Period | Total Production Hours | Gas Quantity (m3) | Oil Quantity (m3) | Water Quantity (m3) |
|---|---|---|---|---|
| 2016 | 360 | 0.0 | 0.0 | 0.0 |
| 2017 | 8583 | 0.0 | 0.0 | 0.0 |
| 2018 | 8312 | 0.0 | 0.0 | 0.0 |
| 2019 | 8182 | 0.0 | 0.0 | 0.0 |
| 2020 | 1868 | 0.0 | 0.0 | 0.0 |
For data sources see[9]
| Occurence Date | Occurence Type | Occurence Depth (m) | Occurence Control Depth (m) |
|---|---|---|---|
| 2016-11-28 | No Incident Encountered | 0.00 | 0.00 |
| 2018-07-06 | No Incident Encountered | 0.00 | 0.00 |
For data sources see[10]