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Well ID: 0425153113020 | |
Location: 02/13-31-042-15W5/0 | |
Location Alias: 02/13-31-42-15 W5M | |
Location Alias 2: 02/13-31-042-15 W5/00 | |
Country: Canada | |
Province: Alberta | |
Township: 042 | |
Meridian: 5 | |
Range: 15 | |
Section: 31 | |
County/Municipality: Clearwater County | |
Well Name: PERSIST OIL STOLBERG 13-31-42-15 | |
Operator Name: Persist Oil And Gas Inc. | |
License Number: 0448124 | |
License Date: 2012-08-30 | |
License Status: Amended | |
Spud Date: 2013-02-11 | |
Final Drill Date: 2013-03-08 | |
Well Total Depth: 3163.00 m | |
Surface Hole Latitude: 52.660479 | |
Surface Hole Longitude: -116.138511 |
Date | Event |
---|---|
2012-08-30 | Obtained License |
2013-02-11 | Lost Circulation Occurred |
2013-02-15 | Surface Casing Operation Performed |
2013-02-18 | Lost Circulation Occurred |
2013-02-19 | Direction Drilling Operation Performed - Deviate |
2013-02-22 | Direction Drilling Operation Performed - Horizontal |
2013-02-26 | Well Log Performed |
2013-02-27 | Intermediate Casing Operation Performed |
2013-03-07 | Well Log Performed |
2013-03-08 | Finished Drilling |
2013-03-08 | Well Log Performed |
2013-03-08 | Well Mode changed to Drilled and Cased |
2013-03-09 | Liner Casing Operation Performed |
2013-03-09 | Perforation Treatment Performed - Slotted Liner or Casing |
2013-03-09 | Well Log Performed |
2013-03-10 | Perforation Treatment Performed - Open-Hole Completion |
2013-03-10 | Rig Released |
2013-03-27 | Well Began Production |
2013-03-27 | Well Fluid changed to Crude Oil |
2013-03-27 | Well Mode changed to Flowing |
2013-08-24 | Perforation Treatment Performed - Fractured |
2014-01-23 | Perforation Treatment Performed - Jet Perforation |
2014-01-24 | Perforation Treatment Performed - Jet Perforation |
For data sources see[3]
Spud Date | Contractor | Rig Number | New Projected Depth (m) | Activity Type |
---|---|---|---|---|
2013-02-11 | Precision Drilling Corporation | 285 | N/A | Drill To LD |
For data sources see[4]
Start Date | Depth (m) | Reason |
---|---|---|
2013-02-19 | 1467.50 | Deviate (5 - 79 degrees) |
2013-02-22 | 2112.50 | Horizontal |
For data sources see[5]
Perforation Date | Perforation Type | Interval Top (m) | Interval Base (m) | Number of Shots |
---|---|---|---|---|
2013-03-09 | Slotted Liner | 2372.40 | 2825.00 | 0 |
2013-03-10 | Open Hole/Barefoot Completion | 2825.00 | 3163.00 | 0 |
2013-08-24 | Fracture | 2840.00 | 2840.10 | 0 |
2014-01-23 | Perforation | 2365.00 | 2403.00 | 7 |
2014-01-24 | Perforation | 2280.00 | 2310.00 | 7 |
For data sources see[6]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2013-08-24 | 2013-08-24 | 2,003 | 0 | N/A |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Hydrocarbon | Not Available | 100 | 69.0185 | N/A | |||
FRAC SAND. 30/50 WHITE | Baker Hughes | Crystalline Silica (Quartz) | 14808-60-7 | 100 | 10.4337 | N/A | ||
FRAC SAND.70/140 OR 50/140 CANADIAN | Baker Hughes | Crystalline Silica (Quartz) | 14808-60-7 | 100 | 1.059 | N/A | ||
PR6000 20/40 | Baker Hughes | Crystalline Silica (Quartz) | 14808-60-7 | 100 | 10.3763 | N/A | ||
RG-35SLR | Baker Hughes | Breaker | Fuels. diesel | 68334-30-5 | 100 | 1.3202 | N/A | |
Magnesium oxide | 1309-48-4 | 100 | 1.3202 | N/A | ||||
XLO-5 | Baker Hughes | Crosslinker | 2-Dibutylaminoethanol | 102-81-8 | 100 | 1.0469 | N/A | |
Ethoxylated oleyl amine | 13127-82-7 | 100 | 1.0469 | N/A | ||||
Ferric sulphate | 10028-22-5 | 100 | 1.0469 | N/A | ||||
NE-118 | Baker Hughes | Demulsifier | 1.2.4-Trimethyl benzene | 95-63-6 | 100 | 0.0673 | N/A | |
1.3.5-Trimethyl benzene | 108-67-8 | 100 | 0.0673 | N/A | ||||
Ethoxylated alcohols. C6-C12 | 68439-45-2 | 100 | 0.0673 | N/A | ||||
Isopropanol | 67-63-0 | 100 | 0.0672 | N/A | ||||
Light aromatic solvent naphtha | 64742-95-6 | 100 | 0.0673 | N/A | ||||
Oxyalkylated phenolic resin | 63428-92-2 | 100 | 0.0672 | N/A | ||||
Xylene | 1330-20-7 | 100 | 0.0673 | N/A | ||||
Nitrogen | Baker Hughes | Energizing Fluid | Nitrogen | 7727-37-9 | 100 | 5.855 | N/A | |
F-100 | Baker Hughes | Friction Reducer | Ethylene glycol | 107-21-1 | 100 | 0.0084 | N/A | |
Isopropanol | 67-63-0 | 100 | 0.0084 | N/A | ||||
Kerosene | 8008-20-6 | 100 | 0.0084 | N/A | ||||
GO-64 | Baker Hughes | Gelling Agent | Phosphoric acid. mixed polyoxyalkylene. esters | Not Available | 100 | 0.8142 | N/A |
For data sources see[7]
Period | Total Production Hours | Gas Quantity (m3) | Oil Quantity (m3) | Water Quantity (m3) |
---|---|---|---|---|
2013 | 1782 | 0.0 | 0.0 | 0.0 |
2014 | 8345 | 0.0 | 0.0 | 0.0 |
2015 | 8615 | 0.0 | 0.0 | 0.0 |
2016 | 8423 | 0.0 | 0.0 | 0.0 |
2017 | 8443 | 0.0 | 0.0 | 0.0 |
2018 | 5136 | 0.0 | 0.0 | 0.0 |
2019 | 8279 | 0.0 | 0.0 | 0.0 |
2020 | 1920 | 0.0 | 0.0 | 0.0 |
For data sources see[8]
Occurence Date | Occurence Type | Occurence Depth (m) | Occurence Control Depth (m) |
---|---|---|---|
2013-02-11 | Lost Circulation | 36.00 | 96.00 |
2013-02-18 | Lost Circulation | 1324.00 | 2420.00 |
2013-09-04 | No Incident Encountered | 0.00 | 0.00 |
2014-01-28 | No Incident Encountered | 0.00 | 0.00 |
For data sources see[9]