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Well ID: 34-005-21651 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: BRETTIN GEO & JO | |
License Status: Active Injection | |
License Date: 1984-08-14 | |
Spud Date: 1984-11-07 | |
Spud Drilling Contractor: P&N DRLG | |
Final Drill Date: 1984-11-09 | |
Well Total Depth: 779.00 ft | |
Configuration: Vertical | |
Latitude: 40.880000 | |
Longitude: -82.160000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1959-01-06 | 133 QUAKER STATE OIL REF CORP GeoDate 1/6/59 |
Oil and Gas | 1959-01-06 | Issued Date 1/6/59 Expired Date Acres 0080000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1984-08-14 | 133 QUAKER STATE OIL REF CORP GeoDate 8/14/84 |
Enhanced Recovery | 1984-08-14 | Issued Date 8/14/84 Expired Date 2/10/85 Acres 0080000 Tool Type CT Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1984-11-07 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
Completed | 1984-11-09 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
Reached Total Depth | 1984-11-09 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
First Injection | 1984-12-06 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
Completion Report Received | 1985-01-14 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
Construction Permit Expires | 1985-02-10 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
Annulus Pressure Monitoring Approved | 1992-03-10 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 8/14/84 |
Last Compliance Report | 1999-12-22 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
Change of Owner | 2002-02-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER |
Change of Owner | 2008-04-24 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Record Last Modified | 2017-02-15 | OTHER DRILLER WAS REX DRILLING CONVERT 8-18-84 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-23 | 712 | 772 | 0 |
2000-05-23 | 720 | 790 | 0 |
720 | 790 | 0 | |
712 | 772 | 0 | |
712 | 772 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 60 Qts | 0 | FOR ERP | ||
NITR | 0 | 60 Qts | 0 | LOGS ATTACHED; FOR PRODUCTION |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | QUAKER STATE OIL REF CORP | 0.00 | 48.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | QUAKER STATE OIL REF CORP | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1184899697 | 2004-4-22 0:00: | ER | No Violations | |
-1188362947 | 2016-1-5 0:00:0 | ER | No Violations | |
-1280724031 | 2017-1-9 0:00:0 | ER | No Violations | |
-1283433751 | 2006-12-29 0:00 | ER | No Violations | 1.00 |
-1315845558 | 2017-4-24 0:00: | ER | No Violations | |
-1349391978 | 2016-11-7 0:00: | ER | No Violations | |
-1400860741 | 2006-12-13 0:00 | ER | No Violations | 0.50 |
-1594395549 | 2020-4-10 0:00: | ER | No Violations | |
-1602314806 | 2014-5-6 0:00:0 | ER | No Violations | |
-1690724949 | 2012-11-27 0:00 | ER | No Violations | |
-1845881616 | 2011-7-12 0:00: | ER | No Violations | |
-1889349560 | 2012-6-7 0:00:0 | ER | No Violations | |
-211344910 | 2018-8-13 0:00: | ER | No Violations | |
-346008551 | 2015-3-31 0:00: | ER | No Violations | |
-388160496 | 2018-10-2 0:00: | ER | No Violations | |
-522666594 | 2005-11-29 0:00 | ER | No Violations | 0.50 |
-663695666 | 2014-3-18 0:00: | ER | No Violations | |
-69524596 | 2016-11-2 0:00: | ER | No Violations | |
-729598879 | 2018-4-9 0:00:0 | ER | No Violations | |
-815975719 | 2016-4-19 0:00: | ER | No Violations | |
-85222667 | 2019-4-11 0:00: | ER | No Violations | |
-877670092 | 2008-2-15 0:00: | ER | No Violations | 0.50 |
-924674260 | 2009-9-30 0:00: | ER | No Violations | 0.50 |
0069524596 | 2016-11-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The well head fittings are in poor condition. |
0167605964 | 2015-10-26 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0208715233 | 2007-05-31 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0211344910 | 2018-08-13 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0229112088 | 2017-10-26 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0268288002 | 2010-04-02 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Pressures equal at 300. Reset packer and test. |
0287950342 | 2013-03-05 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Old style injector valve, did not check. |
0346008551 | 2015-03-31 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0346245615 | 2016-07-11 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Collected a water sample TSB104 for chemical analysis. |
0388160496 | 2018-10-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0451340341 | 2013-04-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Initial test failed due to bad valve replace valve well passed test. |
0463914419 | 2019-01-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0481980485 | 2015-05-20 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0522666594 | 2005-11-29 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0619019734 | 2007-11-01 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0663695666 | 2014-03-18 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0688976811 | 2003-08-14 | Enhanced Recovery Project | No Violations | |
0729598879 | 2018-04-09 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The well head tubing is in fair condition. |
0732769584 | 2012-02-06 | Enhanced Recovery Project | No Violations | inspect well. |
0753928727 | 2011-10-17 | Enhanced Recovery Project | No Violations | Inspect well. |
0774182290 | 2012-09-20 | Enhanced Recovery Project | No Violations | Inspect Well. Valve on annulus was open and pressure was lost. Injector valve is bad. |
0815975719 | 2016-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0877670092 | 2008-02-15 | Enhanced Recovery Project | No Violations | Annulus and injection prssure test. |
0909014126 | 2010-03-30 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Pressures equal at 290 psi. |
0924674260 | 2009-09-30 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. |
0946626911 | 2013-12-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Pump shut down during inspection. |
0956804894 | 2017-07-18 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0958437042 | 2004-11-18 | Enhanced Recovery Project | No Violations | Injection pressure test. |
1113382117 | 2009-10-20 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1125525676 | 2006-04-06 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Constructd with 2 tubing cemented at Berea cap with 1 tubing on a packer. |
1168628797 | 2007-01-12 | Enhanced Recovery Project | No Violations | Pulled tension on 1 packer. Pressured up on annulus to 200psi. Turned injection tubing on at it pressured to 280psi. Tested annulus for 15 minutes and had 0 psi change in pressure. Test approved. |
1184899697 | 2004-04-22 | Enhanced Recovery Project | No Violations | Injection pressure test. |
1188362947 | 2016-01-05 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1240366082 | 2014-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Injector valve is plugged, cannot take a pressure reading. |
1240854114 | 2009-04-27 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1272027155 | 2010-04-23 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Reset packer and test. 0% drop in pressure in 15 minutes. NOV in compliance. |
1280724031 | 2017-01-09 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1283433751 | 2006-12-29 | Enhanced Recovery Project | No Violations | NOV followup. Ran mini test on annulus . Pressures equalized at 280 psi. One inch packer needs reset. |
1315845558 | 2017-04-24 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1349391978 | 2016-11-07 | Enhanced Recovery Project | No Violations | Operator performed repairs on well and replaced fittings that were in poor condition. |
1372249376 | 2020-7-9 0:00:0 | ER | No Violations | |
1400860741 | 2006-12-13 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Pressures are equalized. |
1441214914 | 2015-08-28 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1445020411 | 2011-04-12 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1602314806 | 2014-05-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1670841508 | 2010-11-26 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
167605964 | 2015-10-26 0:00 | ER | No Violations | |
1688770270 | 2014-10-28 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1690724949 | 2012-11-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1845881616 | 2011-07-12 | Enhanced Recovery Project | No Violations | inspect well |
1879936434 | 2005-04-28 | Enhanced Recovery Project | No Violations | Injection well test. |
1889349560 | 2012-06-07 | Enhanced Recovery Project | No Violations | Operator pulled tubing, packer parted and left in hole. Set new re-built Butler Larkin compression packer. Circulate water and inhibitor. Pressure up to 410 psi. conduct mini test. Passed ok. |
1895072766 | 2012-06-04 | Enhanced Recovery Project | No Violations | Inspect Well. Pressure equilized. Shut in well. |
1972233727 | 2018-01-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
2039537915 | 2008-11-25 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Needs box lid hinges repaired. |
2078468713 | 2019-11-15 0:00 | ER | No Violations | |
208715233 | 2007-5-31 0:00: | ER | No Violations | 0.50 |
229112088 | 2017-10-26 0:00 | ER | No Violations | |
268288002 | 2010-4-2 0:00:0 | ER | No Violations | 0.50 |
287950342 | 2013-3-5 0:00:0 | ER | No Violations | |
346245615 | 2016-7-11 0:00: | ER | No Violations | |
451340341 | 2013-4-4 0:00:0 | ER | No Violations | |
463914419 | 2019-1-4 0:00:0 | ER | No Violations | |
481980485 | 2015-5-20 0:00: | ER | No Violations | |
50417562 | 2020-1-22 0:00: | ER | No Violations | |
619019734 | 2007-11-1 0:00: | ER | No Violations | 0.50 |
688976811 | 2003-8-14 0:00: | ER | No Violations | |
732769584 | 2012-2-6 0:00:0 | ER | No Violations | |
753928727 | 2011-10-17 0:00 | ER | No Violations | |
774182290 | 2012-9-20 0:00: | ER | No Violations | |
815168548 | 2019-7-2 0:00:0 | ER | No Violations | |
909014126 | 2010-3-30 0:00: | ER | No Violations | 1.00 |
946626911 | 2013-12-4 0:00: | ER | No Violations | |
956804894 | 2017-7-18 0:00: | ER | No Violations | |
958437042 | 2004-11-18 0:00 | ER | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0268288002 | US-OH-122770 | 2010-04-02 | Failure to conduct or pass mech. integrity test | |
0924674260 | US-OH-130561 | 2009-09-30 | Failure to conduct or pass mech. integrity test | |
1400860741 | US-OH-111869 | 2006-12-13 | Failure to conduct or pass mech. integrity test |
For data sources see[9]