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34-005-22117

Well Details

Well ID: 34-005-22117
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: GORTNER R & P
License Status: Active Injection
License Date: 1976-02-18
Spud Date: 1976-02-05
Spud Drilling Contractor: SHORTS DRLG
Final Drill Date: 1976-10-13
Well Total Depth: 710.00 ft
Configuration: Vertical
Latitude: 40.890000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1976-02-05 SECOND OWNER WAS QUAKER STATE CONVERT TO SEC. REC. 3-26-75, R.I. 2-18-76
CO 1976-02-18 133 QUAKER STATE OIL REF CORP GeoDate 2/18/76
Enhanced Recovery 1976-02-18 Issued Date 2/18/76 Expired Date Acres 0203000 Tool Type CT Proposed Formation BEDFORD Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1976-10-13 SECOND OWNER WAS QUAKER STATE CONVERT TO SEC. REC. 3-26-75, R.I. 2-18-76
Reached Total Depth 1976-10-13 SECOND OWNER WAS QUAKER STATE CONVERT TO SEC. REC. 3-26-75, R.I. 2-18-76
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 2/18/76
Annulus Pressure Monitoring Approved 1998-06-12 SECOND OWNER WAS QUAKER STATE CONVERT TO SEC. REC. 3-26-75, R.I. 2-18-76
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Last Compliance Report 2010-05-04 SECOND OWNER WAS QUAKER STATE CONVERT TO SEC. REC. 3-26-75, R.I. 2-18-76
Record Last Modified 2018-12-31 SECOND OWNER WAS QUAKER STATE CONVERT TO SEC. REC. 3-26-75, R.I. 2-18-76

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-19 563 632 0
662 695 0
2006-09-11 565 632 0
563 632 0
565 632 0
563 632 0
1999-10-12 662 695 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 63 Qts 0
Not Treated 0 43 Qts 0
Not Treated 0 20 Qts 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC 0.00 133.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1026153773 2020-1-30 0:00: ER No Violations
-1037537157 2010-11-26 0:00 ER No Violations 0.50
-1037659093 2017-7-19 0:00: ER No Violations
-1057186869 2011-10-17 0:00 ER No Violations
-1089528123 2011-7-12 0:00: ER No Violations
-1150623509 2015-3-31 0:00: ER No Violations
-1183531639 2014-7-17 0:00: ER No Violations
-119666550 2009-4-23 0:00: ER No Violations 0.50
-1257465622 2016-1-7 0:00:0 ER No Violations
-1269133839 2016-4-19 0:00: ER No Violations
-1319125171 2006-1-25 0:00: ER No Violations 0.50
-147648575 2012-9-20 0:00: ER No Violations
-1568453286 2005-4-28 0:00: ER No Violations 0.50
-1714490785 2008-3-25 0:00: ER No Violations 1.00
-1786409341 2010-4-5 0:00:0 ER No Violations 0.50
-1957377351 2011-4-13 0:00: ER No Violations 1.00
-2076906450 2012-3-7 0:00:0 ER No Violations
-229416906 2013-3-4 0:00:0 ER No Violations
-38385156 2005-6-23 0:00: ER No Violations 1.00
-499417156 2018-8-15 0:00: ER No Violations
-629963385 2008-12-10 0:00 ER No Violations 0.50
-637326622 2013-8-29 0:00: ER No Violations
-702949079 2018-1-26 0:00: ER No Violations
-71688779 2016-7-11 0:00: ER No Violations
-752347666 2012-11-27 0:00 ER No Violations
-944694137 2008-4-16 0:00: ER No Violations 1.00
-973600406 2015-8-31 0:00: ER No Violations
-993052070 2006-4-13 0:00: ER No Violations 0.50
0038385156 2005-06-23 Enhanced Recovery Project Violations Noted Retested tubing and annulus pressure. It remains equalized. Advised Matt Miller to re-set packer by 6-30-2005
0071688779 2016-07-11 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0119666550 2009-04-23 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0144801863 2015-10-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in good condition.
0147648575 2012-09-20 Enhanced Recovery Project No Violations Inspect Well. Site ok.
0155439392 2014-05-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The Injection line is plugged.
0156383261 2012-06-04 Enhanced Recovery Project No Violations Inspect Well.
0229416906 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0307323078 2018-10-12 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0321293054 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0345005903 2017-01-30 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head fittings are in fair condition.
0364861043 2003-11-13 Enhanced Recovery Project No Violations
0425612674 2018-12-20 Work Over Reconditioning No Violations The operator originally installed 20 one inch joints of tubing at 25 feet long, on April 30, 2010. On December 19, 2018 the tubing and packer were tripped out of the hole and 19 joints of used tubing and one new joint of sealtite lined tubing at 25 feet long were run in the hole with a new rebuilt parmaco packer setup in compression. The annulus was circulated and filled with fresh water and inhibitor. The packer was then set in compression at 500 feet below grade. A mechanical integrity test was conducted on the well and was pressured to 410 psi and held for 15 minutes with zero pressure loss. Well passes. Well is put into production. Compliance notice has been resolved.
0495004725 2015-05-21 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head repairs were made and well is in production.
0499417156 2018-08-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0544519802 2007-03-08 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0551835717 2018-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The supply line was frozen and a pressure on the tubing and annulus could not be determined. The landowner is increasing the size of the cattle barn. The addition is currently under construction. The support posts, rafters and purlins have been installed. This structure has been constructed over the vertical air space of this well. Without modifications to the structure servicing and plugging of the well will be hindered.
0604304677 2018-12-19 Work Over Reconditioning No Violations The operator rigged up on the well and tripped the tubing and packer out of the hole. The top joint was replaced and a new rebuild paramo packer with the used Sealtite lined one inch tubing was run in the hole.
0614048598 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
0629963385 2008-12-10 Enhanced Recovery Project No Violations Mini test on annulus. Pressured up to 200 psi and 0 psi decline in 15 minutes.
0637326622 2013-08-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0646919950 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0702949079 2018-01-26 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Inspect well for integrity and pressure.
0714378835 2013-05-22 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0747982858 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test.
0752347666 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0944694137 2008-04-16 Enhanced Recovery Project No Violations Annulus and injection pressure test.
0973600406 2015-08-31 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The union and injection line fitting were leaking.
0989762782 2015-09-24 Enhanced Recovery Project No Violations Inspect well. Well head fittings were replaced and are in compliance.
0993052070 2006-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test. Constructed with 2 tubing cemented at Berea cap with 1 tubing used for injection.
0994621488 2018-04-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1037537157 2010-11-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1037659093 2017-07-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1057186869 2011-10-17 Enhanced Recovery Project No Violations Inspect well.
1083513452 2017-10-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1089528123 2011-07-12 Enhanced Recovery Project No Violations inspect well.
1150623509 2015-03-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pressure has equalized well temporarily shut in until annulus can be pressure tested.
1178704415 2019-10-24 0:00 ER No Violations
1183531639 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Injector is plugged, well shut in.
1207160860 2008-04-02 Enhanced Recovery Project No Violations Reset packer and pressured up on annulus to 260 psi and had 0 psi drop. NOV in compliance.
1233097926 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1257465622 2016-01-07 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head is in poor condition.
1269133839 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1272562344 2010-04-29 Enhanced Recovery Project No Violations Pulled tubing and packer remained in 2 3/8 tubing. Could not fish out. Set new packer above old packer @ 497 and pressure tested. 0 % decline in 15 minutes. NOV in compliance. Sun, 70 degrees.
1319125171 2006-01-25 Enhanced Recovery Project Violations Noted Packer has been reset and pressures are ann. 310 psi and inj. 350 psi. Snow, 30 degrees.
1443458607 2015-09-28 Enhanced Recovery Project No Violations Inspect well at request of operator. Well head fittings have been replaced and are not leaking.
144801863 2015-10-27 0:00 ER No Violations
1462095789 2013-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1537124498 2008-12-03 Enhanced Recovery Project Violations Noted Injection and annulus pressure test.,
1545160986 2018-12-18 Enhanced Recovery Project Violations Noted The operator conducted a mechanical integrity pressure test on the well. The test failed the required parameters. The well was shut in for workover.
155439392 2014-5-27 0:00: ER No Violations
156383261 2012-6-4 0:00:0 ER No Violations
1568453286 2005-04-28 Enhanced Recovery Project Violations Noted Pressures have equalized in annular space and tubing. Pressure up on annulus and re-test by 5-28-2005. Advised Matt Miller of findings.
1613678195 2007-10-12 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1714490785 2008-03-25 Enhanced Recovery Project Violations Noted Annulus and injection pressure test. Annular side pressure is 0 psi. Pressure up to 200 psi and retest.
1786409341 2010-04-05 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Pressures equal at 350 psi. Reset packer and test.
1932274151 2019-1-14 0:00: ER No Violations
1957377351 2011-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1995621501 2019-8-5 0:00:0 ER No Violations
2048654967 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2073015764 2006-12-15 Enhanced Recovery Project No Violations Injection and annulus pressure test.
2076906450 2012-03-07 Enhanced Recovery Project No Violations Inspect Well. Injector valve plugged off. No reading.
307323078 2018-10-12 0:00 ER No Violations
321293054 2014-3-17 0:00: ER No Violations
345005903 2017-1-30 0:00: ER No Violations
364861043 2003-11-13 0:00 ER No Violations
425612674 2018-12-20 0:00 WR No Violations
495004725 2015-5-21 0:00: ER No Violations
544519802 2007-3-8 0:00:0 ER No Violations 0.50
551835717 2018-1-4 0:00:0 ER No Violations
604304677 2018-12-19 0:00 WR No Violations
614048598 2004-11-18 0:00 ER No Violations
646919950 2014-10-28 0:00 ER No Violations
714378835 2013-5-22 0:00: ER No Violations
730836077 2020-5-13 0:00: ER No Violations
747982858 2004-4-22 0:00: ER No Violations
899615979 2019-4-22 0:00: ER No Violations
989762782 2015-9-24 0:00: ER No Violations
994621488 2018-4-27 0:00: ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0038385156 US-OH-124061 2005-06-27 Mechanical failure/contamination
0973600406 US-OH-131163 2015-10-07 Violation of injection tubing/fitting requirements
1319125171 US-OH-109103 2005-05-02 Mechanical failure/contamination
1537124498 US-OH-114824 2008-12-03 Failure to conduct or pass mech. integrity test
1545160986 US-OH-114981 2018-12-31 9-5-10(H) Mechanical failure/contamination
1568453286 US-OH-115324 2005-05-02 Mechanical failure/contamination
1714490785 US-OH-116999 2008-03-25 Failure to conduct or pass mech. integrity test
1786409341 US-OH-117807 2010-04-06 Failure to conduct or pass mech. integrity test

For data sources see[9]

References