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Well ID: 34-005-22287 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: GORTNER R & P | |
License Status: Active Injection | |
License Date: 1976-02-18 | |
Spud Date: 1976-07-29 | |
Spud Drilling Contractor: SHORTS DRLG | |
Final Drill Date: 1976-08-13 | |
Well Total Depth: 662.00 ft | |
Configuration: Vertical | |
Latitude: 40.890000 | |
Longitude: -82.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-02-18 | 133 QUAKER STATE OIL REF CORP GeoDate 2/18/76 |
Enhanced Recovery | 1976-02-18 | Issued Date 2/18/76 Expired Date Acres 0205000 Tool Type CT Proposed Formation BEDFORD Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1976-07-29 | CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76 |
Completed | 1976-08-13 | CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76 |
Reached Total Depth | 1976-08-13 | CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76 |
Annulus Pressure Monitoring Approved | 1991-02-14 | CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76 |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 2/18/76 |
Last Compliance Report | 1999-10-12 | CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76 |
Change of Owner | 2002-02-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER |
Change of Owner | 2008-04-24 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Record Last Modified | 2017-02-15 | CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-22 | 530 | 664 | 0 |
530 | 664 | 0 | |
530 | 664 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 47 Qts | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | DEEP RESOURCES LLC | 0.00 | 133.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | DEEP RESOURCES LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1049026533 | 2012-9-20 0:00: | ER | No Violations | |
-1114476436 | 2014-3-17 0:00: | ER | No Violations | |
-1242803224 | 2020-1-17 0:00: | ER | No Violations | |
-1258684697 | 2017-10-19 0:00 | ER | No Violations | |
-1291052782 | 2017-7-19 0:00: | ER | No Violations | |
-1379701780 | 2014-10-28 0:00 | ER | No Violations | |
-1464504478 | 2016-1-6 0:00:0 | ER | No Violations | |
-1737900116 | 2011-7-12 0:00: | ER | No Violations | |
-1886316879 | 2015-10-27 0:00 | ER | No Violations | |
-1904658110 | 2018-5-2 0:00:0 | ER | No Violations | |
-1924790087 | 2013-5-22 0:00: | ER | No Violations | |
-1946436228 | 2004-4-22 0:00: | ER | No Violations | |
-21293033 | 2012-5-31 0:00: | ER | No Violations | |
-31842977 | 2006-1-25 0:00: | ER | No Violations | 0.50 |
-371922489 | 2009-4-23 0:00: | ER | No Violations | 0.50 |
-386744629 | 2016-4-19 0:00: | ER | No Violations | |
-418832021 | 2015-5-13 0:00: | ER | No Violations | |
-568944192 | 2012-11-27 0:00 | ER | No Violations | |
-646447400 | 2018-10-12 0:00 | ER | No Violations | |
-717925981 | 2013-10-29 0:00 | ER | No Violations | |
-833332698 | 2008-12-3 0:00: | ER | No Violations | 0.50 |
-925975555 | 2003-11-13 0:00 | ER | No Violations | |
-942140712 | 2017-4-13 0:00: | ER | No Violations | |
0021293033 | 2012-05-31 | Enhanced Recovery Project | No Violations | Inspect Well. No valve on injector. |
0031842977 | 2006-01-25 | Enhanced Recovery Project | No Violations | |
0041667905 | 2009-10-20 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0168696428 | 2007-03-08 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0195862876 | 2014-03-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The valve for the annulus is frozen. Solvent tank is attached to the injection line, preventing collection of injection pressure. |
0333821281 | 2016-10-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0371922489 | 2009-04-23 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0386744629 | 2016-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0418832021 | 2015-05-13 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Well is shut in. |
0431199068 | 2016-01-05 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Annulus fitting was frozen due to cold weather. |
0568944192 | 2012-11-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0646447400 | 2018-10-12 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0665182943 | 2014-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Well head has a slight leak. |
0717925981 | 2013-10-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0739258259 | 2016-07-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0822220070 | 2007-10-12 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0833332698 | 2008-12-03 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0837507412 | 2013-03-05 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0856908066 | 2018-04-23 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0889800243 | 2006-12-14 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0925975555 | 2003-11-13 | Enhanced Recovery Project | No Violations | PRESSURE EQUALIZATION ON TUBING AND CASING/TUBING ANNULUS. COMPANY REQUIRED TO PERFORM A MINITEST TO DEMONSTRATE MECHANICAL INTEGRITY |
0942140712 | 2017-04-13 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1049026533 | 2012-09-20 | Enhanced Recovery Project | No Violations | Inspect Well. The injector line is plugged. |
1101147124 | 2004-11-18 | Enhanced Recovery Project | No Violations | Injection pressure test. |
1101303813 | 2004-11-18 | Enhanced Recovery Project | No Violations | Injection pressure test. |
1108442186 | 2011-10-17 | Enhanced Recovery Project | No Violations | Inspect well. |
1114476436 | 2014-03-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The valve for the annulus was frozen during previous days inspection. Re-test annulus on well. |
1202624177 | 2017-01-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1206460681 | 2008-03-25 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
1219649602 | 2019-4-10 0:00: | ER | No Violations | |
1238686417 | 2019-10-23 0:00 | ER | No Violations | |
1258684697 | 2017-10-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The annulus test valve was replaced. The operator conducted a monthly pressure test that was witnessed. The annulus had zero pressure loss over fifteen minutes. |
1267815392 | 2013-08-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1268813649 | 2019-1-14 0:00: | ER | No Violations | |
1269868044 | 2012-03-07 | Enhanced Recovery Project | No Violations | Inspect Well. Well has been shut in by oporator because injector is plugged off. |
1290796681 | 2010-11-26 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1291052782 | 2017-07-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The annulus valve broken due to winter freeze. Notified operator to replace parts. |
1296483377 | 2009-04-23 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1333024796 | 2012-03-28 | Enhanced Recovery Project | No Violations | Inspect well. injection line was plugged and has been cleaned. |
1354470433 | 2005-05-19 | Enhanced Recovery Project | No Violations | Injection well test. Updated GPS readings. |
1379701780 | 2014-10-28 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. This well will need to be pressure tested. |
1443181697 | 2015-09-24 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. The well is shut in. The injection tubing is heavily rusted. The annulus test valve has failed. The well failed integrity during the 10/29/2014 Inspection. |
1447939243 | 2015-11-05 | Work Over Reconditioning | No Violations | The well is constructed with 2 3/8 inch tubing at a depth of 535 feet cemented to the surface. The well is open hole to the total depth of 662 feet. The packer failed and was replaced. The top most joint of PVC lined tubing was replaced with new pipe. Total of 19 joints of 25 foot sections of PVC lined one Inch tubing was run in the hole with a parmaco style packer set in compression. Approximately 300 gallon of fresh water were pumped through the tubing and circulated to the surface prior to setting the packer. The packer was set and the annulus was pressured up to 385 psi. The pressure was monitored for 15 minutes with 3.8% pressure loss. This is within the stated margin of 5% pressure loss. The well passes the Mechanical Integrity Test. The well head was reconstructed with new parts and put into production. |
1464504478 | 2016-01-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Retest wellhead. Fittings have thawed out after freezing due to cold weather. |
1533202456 | 2006-04-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1565091191 | 2019-8-5 0:00:0 | ER | No Violations | |
1644393359 | 2011-04-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
168696428 | 2007-3-8 0:00:0 | ER | No Violations | 0.50 |
1737900116 | 2011-07-12 | Enhanced Recovery Project | No Violations | inspect well. |
1802659538 | 2018-01-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1860803662 | 2014-05-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1886316879 | 2015-10-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The well head is in poor condition and is shut in. |
1904658110 | 2018-05-02 | Enhanced Recovery Project | No Violations | Inspect well with operator to preform monthly pressure test of the annulus on the well. |
1924790087 | 2013-05-22 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1946436228 | 2004-04-22 | Enhanced Recovery Project | No Violations | Injection pressure test. Annular and injection pressures are equalized. Advised len Rex to repressure annulus and re-test. Send results to Tom Tomastik. |
195862876 | 2014-3-17 0:00: | ER | No Violations | |
2015044194 | 2020-7-15 0:00: | ER | No Violations | |
2047389417 | 2019-2-8 0:00:0 | ER | No Violations | |
2088868470 | 2018-07-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
2102395005 | 2014-10-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Attempt to pressure test well. Annulus is flowing water when valve is opened. Well is not capable of holding pressure. The well was shut in. Well currently has a tension packer. |
333821281 | 2016-10-19 0:00 | ER | No Violations | |
41667905 | 2009-10-20 0:00 | ER | No Violations | 0.50 |
431199068 | 2016-1-5 0:00:0 | ER | No Violations | |
665182943 | 2014-7-17 0:00: | ER | No Violations | |
739258259 | 2016-7-6 0:00:0 | ER | No Violations | |
770446582 | 2019-2-11 0:00: | ER | No Violations | |
808234194 | 2019-4-22 0:00: | ER | No Violations | |
822220070 | 2007-10-12 0:00 | ER | No Violations | 0.50 |
837507412 | 2013-3-5 0:00:0 | ER | No Violations | |
856908066 | 2018-4-23 0:00: | ER | No Violations | |
889800243 | 2006-12-14 0:00 | ER | No Violations | 0.50 |
997443559 | 2020-5-13 0:00: | ER | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1443181697 | US-OH-112882 | 2015-12-15 | Violation of injection tubing/fitting requirements |
For data sources see[9]