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34-005-22287

Well Details

Well ID: 34-005-22287
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: GORTNER R & P
License Status: Active Injection
License Date: 1976-02-18
Spud Date: 1976-07-29
Spud Drilling Contractor: SHORTS DRLG
Final Drill Date: 1976-08-13
Well Total Depth: 662.00 ft
Configuration: Vertical
Latitude: 40.890000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-02-18 133 QUAKER STATE OIL REF CORP GeoDate 2/18/76
Enhanced Recovery 1976-02-18 Issued Date 2/18/76 Expired Date Acres 0205000 Tool Type CT Proposed Formation BEDFORD Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1976-07-29 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
Completed 1976-08-13 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
Reached Total Depth 1976-08-13 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
Annulus Pressure Monitoring Approved 1991-02-14 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 2/18/76
Last Compliance Report 1999-10-12 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Record Last Modified 2017-02-15 CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-11-76

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-22 530 664 0
530 664 0
530 664 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 47 Qts 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC 0.00 133.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1049026533 2012-9-20 0:00: ER No Violations
-1114476436 2014-3-17 0:00: ER No Violations
-1242803224 2020-1-17 0:00: ER No Violations
-1258684697 2017-10-19 0:00 ER No Violations
-1291052782 2017-7-19 0:00: ER No Violations
-1379701780 2014-10-28 0:00 ER No Violations
-1464504478 2016-1-6 0:00:0 ER No Violations
-1737900116 2011-7-12 0:00: ER No Violations
-1886316879 2015-10-27 0:00 ER No Violations
-1904658110 2018-5-2 0:00:0 ER No Violations
-1924790087 2013-5-22 0:00: ER No Violations
-1946436228 2004-4-22 0:00: ER No Violations
-21293033 2012-5-31 0:00: ER No Violations
-31842977 2006-1-25 0:00: ER No Violations 0.50
-371922489 2009-4-23 0:00: ER No Violations 0.50
-386744629 2016-4-19 0:00: ER No Violations
-418832021 2015-5-13 0:00: ER No Violations
-568944192 2012-11-27 0:00 ER No Violations
-646447400 2018-10-12 0:00 ER No Violations
-717925981 2013-10-29 0:00 ER No Violations
-833332698 2008-12-3 0:00: ER No Violations 0.50
-925975555 2003-11-13 0:00 ER No Violations
-942140712 2017-4-13 0:00: ER No Violations
0021293033 2012-05-31 Enhanced Recovery Project No Violations Inspect Well. No valve on injector.
0031842977 2006-01-25 Enhanced Recovery Project No Violations
0041667905 2009-10-20 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0168696428 2007-03-08 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0195862876 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The valve for the annulus is frozen. Solvent tank is attached to the injection line, preventing collection of injection pressure.
0333821281 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0371922489 2009-04-23 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0386744629 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0418832021 2015-05-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well is shut in.
0431199068 2016-01-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Annulus fitting was frozen due to cold weather.
0568944192 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0646447400 2018-10-12 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0665182943 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head has a slight leak.
0717925981 2013-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0739258259 2016-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0822220070 2007-10-12 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0833332698 2008-12-03 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0837507412 2013-03-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0856908066 2018-04-23 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0889800243 2006-12-14 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0925975555 2003-11-13 Enhanced Recovery Project No Violations PRESSURE EQUALIZATION ON TUBING AND CASING/TUBING ANNULUS. COMPANY REQUIRED TO PERFORM A MINITEST TO DEMONSTRATE MECHANICAL INTEGRITY
0942140712 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1049026533 2012-09-20 Enhanced Recovery Project No Violations Inspect Well. The injector line is plugged.
1101147124 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
1101303813 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
1108442186 2011-10-17 Enhanced Recovery Project No Violations Inspect well.
1114476436 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The valve for the annulus was frozen during previous days inspection. Re-test annulus on well.
1202624177 2017-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1206460681 2008-03-25 Enhanced Recovery Project No Violations Annulus and injection pressure test.
1219649602 2019-4-10 0:00: ER No Violations
1238686417 2019-10-23 0:00 ER No Violations
1258684697 2017-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The annulus test valve was replaced. The operator conducted a monthly pressure test that was witnessed. The annulus had zero pressure loss over fifteen minutes.
1267815392 2013-08-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1268813649 2019-1-14 0:00: ER No Violations
1269868044 2012-03-07 Enhanced Recovery Project No Violations Inspect Well. Well has been shut in by oporator because injector is plugged off.
1290796681 2010-11-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1291052782 2017-07-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The annulus valve broken due to winter freeze. Notified operator to replace parts.
1296483377 2009-04-23 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1333024796 2012-03-28 Enhanced Recovery Project No Violations Inspect well. injection line was plugged and has been cleaned.
1354470433 2005-05-19 Enhanced Recovery Project No Violations Injection well test. Updated GPS readings.
1379701780 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. This well will need to be pressure tested.
1443181697 2015-09-24 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The well is shut in. The injection tubing is heavily rusted. The annulus test valve has failed. The well failed integrity during the 10/29/2014 Inspection.
1447939243 2015-11-05 Work Over Reconditioning No Violations The well is constructed with 2 3/8 inch tubing at a depth of 535 feet cemented to the surface. The well is open hole to the total depth of 662 feet. The packer failed and was replaced. The top most joint of PVC lined tubing was replaced with new pipe. Total of 19 joints of 25 foot sections of PVC lined one Inch tubing was run in the hole with a parmaco style packer set in compression. Approximately 300 gallon of fresh water were pumped through the tubing and circulated to the surface prior to setting the packer. The packer was set and the annulus was pressured up to 385 psi. The pressure was monitored for 15 minutes with 3.8% pressure loss. This is within the stated margin of 5% pressure loss. The well passes the Mechanical Integrity Test. The well head was reconstructed with new parts and put into production.
1464504478 2016-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Retest wellhead. Fittings have thawed out after freezing due to cold weather.
1533202456 2006-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1565091191 2019-8-5 0:00:0 ER No Violations
1644393359 2011-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
168696428 2007-3-8 0:00:0 ER No Violations 0.50
1737900116 2011-07-12 Enhanced Recovery Project No Violations inspect well.
1802659538 2018-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1860803662 2014-05-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1886316879 2015-10-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in poor condition and is shut in.
1904658110 2018-05-02 Enhanced Recovery Project No Violations Inspect well with operator to preform monthly pressure test of the annulus on the well.
1924790087 2013-05-22 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1946436228 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test. Annular and injection pressures are equalized. Advised len Rex to repressure annulus and re-test. Send results to Tom Tomastik.
195862876 2014-3-17 0:00: ER No Violations
2015044194 2020-7-15 0:00: ER No Violations
2047389417 2019-2-8 0:00:0 ER No Violations
2088868470 2018-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2102395005 2014-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Attempt to pressure test well. Annulus is flowing water when valve is opened. Well is not capable of holding pressure. The well was shut in. Well currently has a tension packer.
333821281 2016-10-19 0:00 ER No Violations
41667905 2009-10-20 0:00 ER No Violations 0.50
431199068 2016-1-5 0:00:0 ER No Violations
665182943 2014-7-17 0:00: ER No Violations
739258259 2016-7-6 0:00:0 ER No Violations
770446582 2019-2-11 0:00: ER No Violations
808234194 2019-4-22 0:00: ER No Violations
822220070 2007-10-12 0:00 ER No Violations 0.50
837507412 2013-3-5 0:00:0 ER No Violations
856908066 2018-4-23 0:00: ER No Violations
889800243 2006-12-14 0:00 ER No Violations 0.50
997443559 2020-5-13 0:00: ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1443181697 US-OH-112882 2015-12-15 Violation of injection tubing/fitting requirements

For data sources see[9]

References