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Well ID: 34-005-22628 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: GORTNER R & P | |
License Status: Active Injection | |
License Date: 1976-02-18 | |
Spud Date: 1967-10-31 | |
Spud Drilling Contractor: ROSS WELL SERVICE | |
Final Drill Date: 1976-02-11 | |
Well Total Depth: 627.00 ft | |
Configuration: Vertical | |
Latitude: 40.890000 | |
Longitude: -82.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1967-10-31 | DRILLED BY KLAEGER DRLG CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-18-76 IP. WTR. INJ. |
Completed | 1976-02-11 | DRILLED BY KLAEGER DRLG CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-18-76 IP. WTR. INJ. |
Reached Total Depth | 1976-02-11 | DRILLED BY KLAEGER DRLG CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-18-76 IP. WTR. INJ. |
CO | 1976-02-18 | 133 QUAKER STATE OIL REF CORP GeoDate 2/18/76 |
Oil and Gas | 1976-02-18 | Issued Date 2/18/76 Expired Date 2/17/77 Acres 0133750 Tool Type NT Proposed Formation BEDFORD Proposed Depth 00000 Proposed Drill Depth 00000 |
Completion Report Received | 1976-03-23 | DRILLED BY KLAEGER DRLG CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-18-76 IP. WTR. INJ. |
Construction Permit Expires | 1977-02-17 | DRILLED BY KLAEGER DRLG CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-18-76 IP. WTR. INJ. |
Annulus Pressure Monitoring Approved | 1990-10-02 | DRILLED BY KLAEGER DRLG CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-18-76 IP. WTR. INJ. |
CO | 1995-10-18 | 133 QUAKER STATE OIL REF CORP |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 2/18/76 |
Last Compliance Report | 1999-10-18 | DRILLED BY KLAEGER DRLG CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-18-76 IP. WTR. INJ. |
Change of Owner | 2002-02-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER |
Change of Owner | 2008-04-24 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Record Last Modified | 2017-02-15 | DRILLED BY KLAEGER DRLG CON. SEC. RECOVERY 3-26-75, RE-ISSUE 2-18-76 IP. WTR. INJ. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-22 | 562 | 592 | 0 |
562 | 592 | 0 | |
562 | 592 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 180 Qts | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | DEEP RESOURCES LLC | 0.00 | 133.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | DEEP RESOURCES LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1042901026 | 2013-12-4 0:00: | ER | No Violations | |
-1134418969 | 2018-5-1 0:00:0 | ER | No Violations | |
-1259891477 | 2007-3-30 0:00: | ER | No Violations | |
-1262269411 | 2017-4-13 0:00: | ER | No Violations | |
-1320090323 | 2014-3-17 0:00: | ER | No Violations | |
-1394672284 | 2016-4-19 0:00: | ER | No Violations | |
-1415026647 | 2009-4-23 0:00: | ER | No Violations | 0.50 |
-1474882551 | 2006-1-25 0:00: | ER | No Violations | 0.50 |
-1485940833 | 2019-4-10 0:00: | ER | No Violations | |
-1546345122 | 2008-12-10 0:00 | ER | No Violations | 0.50 |
-1631765708 | 2014-7-17 0:00: | ER | No Violations | |
-1796491404 | 2012-9-20 0:00: | ER | No Violations | |
-1811150436 | 2018-4-19 0:00: | ER | No Violations | |
-1919374082 | 2016-1-6 0:00:0 | ER | No Violations | |
-2017427023 | 2004-4-22 0:00: | ER | No Violations | |
-2066121071 | 2016-5-9 0:00:0 | ER | No Violations | |
-2139689332 | 2015-9-23 0:00: | ER | No Violations | |
-375379003 | 2013-3-4 0:00:0 | ER | No Violations | |
-403336061 | 2018-7-6 0:00:0 | ER | No Violations | |
-450948117 | 2011-7-12 0:00: | ER | No Violations | |
-455254126 | 2019-10-23 0:00 | ER | No Violations | |
-490887710 | 2016-10-19 0:00 | ER | No Violations | |
-610489520 | 2015-3-31 0:00: | ER | No Violations | |
-750950603 | 2006-12-14 0:00 | ER | No Violations | 1.00 |
-967315308 | 2019-1-10 0:00: | ER | No Violations | |
0000003803 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 6/6/91 INSPECTOR WESLEY,MARTIN DATE 06/0619/91 DATA FROM OLD VAX INFO | |
0091455839 | 2012-02-02 | Enhanced Recovery Project | No Violations | inspect well. Conduct 15 minute test on well and pass. |
0308657798 | 2013-05-22 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0326694579 | 2015-05-15 | Enhanced Recovery Project | No Violations | The well is an injection well for the waterflood ERP. ID posted. The well is in use. |
0375379003 | 2013-03-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0392354607 | 2017-07-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0403336061 | 2018-07-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0450948117 | 2011-07-12 | Enhanced Recovery Project | No Violations | inspect well. |
0490887710 | 2016-10-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0497519709 | 2006-04-13 | Enhanced Recovery Project | No Violations | Injection annulus pressure test. Pressures were equalized. Ran test buggy on annulus and pressured up to 470 psi for 15 minutes. Pressure dropped 0 psi in 15 minutes. Test approved. |
0610489520 | 2015-03-31 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0616195596 | 2016-07-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The well head fittings have recently been replaced. |
0639846795 | 2015-10-26 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Well head is in good condition. No leaks. |
0750950603 | 2006-12-14 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0753958522 | 2008-12-03 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Pressures are equal at 320 psi. |
0899893591 | 2005-04-28 | Enhanced Recovery Project | No Violations | Injection pressure test. |
0930826973 | 2011-04-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0986652117 | 2009-10-07 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. |
1000692238 | 2008-02-21 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
1042901026 | 2013-12-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Pump shut down during inspection. |
1101142842 | 2004-11-18 | Enhanced Recovery Project | No Violations | Injection pressure test. Equal pressures. Re- test in 30 days and report. |
1129133340 | 2018-10-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1132634652 | 2017-10-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1134418969 | 2018-05-01 | Enhanced Recovery Project | No Violations | Inspect well with operator to preform monthly pressure test of the annulus on the well. The annuls pressure loss was within the five percent margin. The well is in compliance. |
1175685483 | 2007-04-03 | Enhanced Recovery Project | No Violations | Retest annulus and injection pressures. Pressured up annulus to 340 psi and it held for 15 minutes. Annular side is 340 psi and injection side is 300 psi. Plant was down on 4-2-2007 and injection pressures are down. Advised Matt Miller to retest in 30 days and report to inspector. |
1225816867 | 2007-10-16 | Enhanced Recovery Project | No Violations | Line leak has been repaired and well back to injection. NOV in compliance. |
1252467327 | 2010-11-26 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Pressures are equal at 340 psi, Reset packer and test. |
1259891477 | 2007-03-30 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. Pressures are equalized at 360 psi. Shut in well until repairs are made to packer. |
1262269411 | 2017-04-13 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1295963676 | 2011-01-25 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Re-set packer. Pressured up annulus to 200 psi. 0 psi decline in 15 minutes. |
1320090323 | 2014-03-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1322228315 | 2011-11-17 | Enhanced Recovery Project | No Violations | Inspect well. Shut well in. tubing equalized with annulus. |
1394672284 | 2016-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The annulus test port shut off valve has failed. |
1415026647 | 2009-04-23 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1415643600 | 2015-05-20 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. The injection line nipple at the shutoff valve is leaking. |
1438671866 | 2014-10-28 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1474882551 | 2006-01-25 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1515767026 | 2018-01-03 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1546345122 | 2008-12-10 | Enhanced Recovery Project | No Violations | Mini test on annulus. Pressured up to 400 psi and pressure dropped to 390 psi in 15 minutes. |
1559420914 | 2017-01-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1587577210 | 2020-4-22 0:00: | ER | No Violations | |
1588853746 | 2020-5-6 0:00:0 | WR | No Violations | |
1596600042 | 2007-10-16 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Injection line spraying brine before shut off valve. Called Len Rex to shut down line and repair leak as soon as possible. |
1631765708 | 2014-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1687246336 | 2012-05-30 | Enhanced Recovery Project | No Violations | Inspect Well. |
1757642341 | 2012-11-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1796491404 | 2012-09-20 | Enhanced Recovery Project | No Violations | Inspect Well. Site ok. |
1801945733 | 2016-01-07 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Retest well after well head fittings have been replaced. The injection valve was partially opened and put into production. |
1811150436 | 2018-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Request operator to conduct pressure test on well. |
1862176183 | 2014-05-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1886540942 | 2003-11-13 | Enhanced Recovery Project | No Violations | PRESSURE EQUALIZATION ON TUBING AND TUBING CASING ANNULUS. COMPANY IS REQUIRED TO PERFORM A MINITEST TO DEMONSTRATE MECHANICAL INTEGRITY. |
1919374082 | 2016-01-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Well was shut in upon inspection. The shut off valve was dripping from the valve stem. Notified operator and Well head fitting were replaced. The well was put into production. |
2017427023 | 2004-04-22 | Enhanced Recovery Project | No Violations | Injection pressure test. Annular and injection pressures equalized. Advised Len Rex to pressure test annular space and re-test. Report to Tom Tomastik in 30 days. |
2018056116 | 2012-02-27 | Enhanced Recovery Project | No Violations | inspect well. |
2066121071 | 2016-05-09 | Enhanced Recovery Project | No Violations | Follow up inspection from April 19, 2016. The operator has replaced the fitting that were in poor condition. Operator pressured annulus on well head and conducted at test. Measure pressure on annulus and tubing. |
2139689332 | 2015-09-23 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
308657798 | 2013-5-22 0:00: | ER | No Violations | |
326694579 | 2015-5-15 0:00: | ER | No Violations | 0.50 |
3803 | PL | No Violations | ||
392354607 | 2017-7-19 0:00: | ER | No Violations | |
497519709 | 2006-4-13 0:00: | ER | No Violations | 1.00 |
581899626 | 2019-7-10 0:00: | ER | No Violations | |
616195596 | 2016-7-6 0:00:0 | ER | No Violations | |
639846795 | 2015-10-26 0:00 | ER | No Violations | |
676278023 | 2020-1-23 0:00: | ER | No Violations | |
753958522 | 2008-12-3 0:00: | ER | No Violations | 0.50 |
814025660 | 2020-7-14 0:00: | ER | No Violations | |
899893591 | 2005-4-28 0:00: | ER | No Violations | 0.50 |
91455839 | 2012-2-2 0:00:0 | ER | No Violations | |
930826973 | 2011-4-13 0:00: | ER | No Violations | 1.00 |
986652117 | 2009-10-7 0:00: | ER | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0753958522 | US-OH-128568 | 2008-12-03 | Failure to conduct or pass mech. integrity test | |
0986652117 | US-OH-131342 | 2009-10-07 | Failure to conduct or pass mech. integrity test | |
1252467327 | US-OH-106768 | 2010-11-26 | Failure to conduct or pass mech. integrity test | |
1415643600 | US-OH-112206 | 2015-07-17 | Mechanical failure/contamination | |
1596600042 | US-OH-115625 | 2007-10-16 | Mechanical failure/contamination |
For data sources see[9]