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Well ID: 34-005-22688 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Vermillion Township | |
Operator Name: JR ME LLC | |
Well Pad ID: | |
Farm/Lease Name: FOX DONALD & CATHERINE | |
License Status: Final Restoration | |
License Date: 2017-01-10 | |
Spud Date: 1970-09-01 | |
Spud Drilling Contractor: DON RIDGWAY | |
Final Drill Date: 1970-10-16 | |
Well Total Depth: 2710.00 ft | |
Configuration: Vertical | |
Latitude: 40.790000 | |
Longitude: -82.260000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1969-05-20 | 722 FOX DONALD GeoDate 5/20/69 |
Oil and Gas | 1969-05-20 | Issued Date 5/20/69 Expired Date Acres 0158600 Tool Type CT Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1970-09-01 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17 |
Completed | 1970-10-16 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17 |
Reached Total Depth | 1970-10-16 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17 |
Change of Owner | 2016-10-03 | Operator changed from 722, FOX DONALD to 9214, JR ME LLC |
APP | 2017-01-10 | Proposed Formations:CLINTON SAND, Issued Date:1/10/2017, Expired Date:1/10/2019 12:00:00 PM, Drilling unit acres:158.6, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2017-06-12 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17 |
Record Last Modified | 2018-01-19 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17 |
Construction Permit Expires | 2019-01-10 | UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1002 Bbl | 21300 | BW=1002.5 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2016 | JR ME LLC | 0.00 | 0.00 | 0 |
2017 | JR ME LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2016 | JR ME LLC | Brine | 0 | 0 |
2017 | JR ME LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1842290340 | 2017-6-8 0:00:0 | PB | No Violations | 4.00 |
0672154925 | 2017-06-09 | Plug / Plug Back | No Violations | Appalalchian Well Service was on site to bond log and cut the 7 inch casing. The top of the lime plug was tagged at 950 feet. 7 inch casing was cut at 630 feet, just below the Berea sand and pulled from the well. Tubing was ran in to set a Berea plug. Circulation was established and maintained through the plugging. A 200 foot plug was set at the Berea. |
0853325748 | 2017-06-06 | Plug / Plug Back | No Violations | Arrive on location for bottom plug 7:45 AM. No personnel on site. Wait on callback from rig crew. They advised they had to change out their tubing due to paraffin buildup and would be late. Left location. Return to location 11:30 AM. Attempt to sting in to retainer and took several tries. Stung in and attempted injection test. Pressure spiked to 2000psi and shut down with no fluid volume pumped. A 500 foot plug was placed on top of the retainer. No gas was reported when the rig crew opened up the well. |
0928242060 | 2017-04-17 | Production Wells | No Violations | The well is unidentified. The valve on the flow line is open. The well is equipped with a separator and 5.5 inch production casing with an orbit valve. The well has recently transferred ownership and the new operator has obtained a plugging permit. |
1078803753 | 2015-03-30 | Production Wells | No Violations | The well is supplying domestic gas. It is equipped with a storage well type separator and an orbit valve on the production casing. There is no ID at the well. An attempt was made to contact the owner at the address listed on the registration, however no one was home. A followup attempt will be made to advise the owner to identify the well. 1837 SR 60 is the registered address. |
1496949087 | 2017-06-05 | Plug / Plug Back | No Violations | Kill water was bullheaded down the production casing. The well was gauged at 780 psi prior to the job. 54 barrels were pumped away and the well locked up at 1400 psi. Appalachian Well Services was contaced to set a cement retainer in the casing. Cement retainer was set on wireline at 2480 feet. The tool hung up several times in the 5.5 inch casing as it was running in. A gas pocket was present in the killed well. Gas wsa blown down and the well was topped up with fresh water from surface. Hydrostatic pressure with fresh water calculated at 1074 psi to retainer. The orbit valve was removed from the casing head and the well was shut in with a swage and 2 inch valve. |
1497025041 | 2017-06-07 | Plug / Plug Back | No Violations | The plug set at bottom above the retainer was tagged at 2120 feet. Appalachian Well Service ran a bond log on the well and found cement behind the 5.5 inch casing at 2040 feet. The casing was cut with a wireline cutting tool at 1810 feet and pulled from the well. 7 inch casing was found to be present when the 5.5 was removed. |
1497350310 | 2017-06-12 | Plug / Plug Back | No Violations | Bishop Well Service rig contacted the inspector to advise they measured the top of the Berea plug at 528 feet. Planned top was 430 feet and the Berea sand extends from 618 to 595 feet. Additional cement was required on top of the Berea plug and the surface casing was pulled so the well owner opted to cement the well solid to surface from the Berea plug. A 120 sack plug was set and 320 feet of tubing was pulled. Had to wait on a second bulk truck of cement to finish the job. Cement was pumped until it returned to surface. Circulation was established and maintained through plugging operations. Cement was down about 20 to 25 feet at the end of the day. The operator is going to top up the well with bagged cement. |
1497448133 | 2017-06-13 | Plug / Plug Back | No Violations | The well has been cut off and buried. The operator stated they topped up the plug with 5 bags of Quikrete. |
1497962172 | 2017-06-15 | Final Restoration | No Violations | The pit has been closed and the well is cut off and buried. There was an ID plate on location at the end of plugging. The landowner submitted a waiver for buried gas line, access road and grading of the location. The waiver and final restoration are approved. |
1499699458 | 2017-07-10 | Final Restoration | No Violations | The landowner has completed finish grading of the well location. Vegetation is establishing on the location. The waiver for the lease road and buried gas lines has been approved. Final restoration has been approved. |
1842290340 | 2017-06-08 | Plug / Plug Back | No Violations | The operator requested inspection to perforate 7 inch casing at the lime and set a plug. The casing was perforated from 1750 to 1740 and 1450 to 1440. Tubing was ran to 1752 and cement was pumped and displaced for a 500 foot plug. Circulation was established and maintained through the job. Oil and gas circulated up the outside of the 7 inch casing. |
672154925 | 2017-6-9 0:00:0 | PB | No Violations | 5.00 |
853325748 | 2017-6-6 0:00:0 | PB | No Violations | 5.00 |
928242060 | 2017-4-17 0:00: | PW | No Violations | 0.50 |
For data sources see[8]