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Well ID: 34-005-23066 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: MANN GLADYS C | |
License Status: Active Injection | |
License Date: 1975-04-11 | |
Spud Date: 1975-04-16 | |
Spud Drilling Contractor: SHORTS DRLG | |
Final Drill Date: 1975-05-02 | |
Well Total Depth: 720.00 ft | |
Configuration: Vertical | |
Latitude: 40.890000 | |
Longitude: -82.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1975-04-16 | RE-ISSUE & SEC. RECOV. 4-16-75 |
CO | 1975-04-21 | 133 QUAKER STATE OIL REF CORP GeoDate 4/21/75 |
Enhanced Recovery | 1975-04-21 | Issued Date 4/21/75 Expired Date Acres 0000000 Tool Type RTAF Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
Completed | 1975-05-02 | RE-ISSUE & SEC. RECOV. 4-16-75 |
Reached Total Depth | 1975-05-02 | RE-ISSUE & SEC. RECOV. 4-16-75 |
Annulus Pressure Monitoring Approved | 1994-09-21 | RE-ISSUE & SEC. RECOV. 4-16-75 |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 4/21/75 |
Change of Owner | 2002-02-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER |
Last Compliance Report | 2003-08-11 | RE-ISSUE & SEC. RECOV. 4-16-75 |
Change of Owner | 2009-02-04 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Record Last Modified | 2017-02-15 | RE-ISSUE & SEC. RECOV. 4-16-75 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-22 | 600 | 668 | 0 |
600 | 668 | 0 | |
600 | 668 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 102 Qts | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | DEEP RESOURCES LLC | 0.00 | 13.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | DEEP RESOURCES LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1031105108 | 2015-5-21 0:00: | ER | No Violations | |
-1041141469 | 2011-7-12 0:00: | ER | No Violations | |
-1054169670 | 2019-4-18 0:00: | ER | No Violations | |
-1069527216 | 2007-3-30 0:00: | ER | No Violations | 0.50 |
-1216707566 | 2013-8-29 0:00: | ER | No Violations | |
-1334367035 | 2013-5-22 0:00: | ER | No Violations | |
-1361616018 | 2009-10-7 0:00: | ER | No Violations | 0.50 |
-1566499520 | 2020-5-13 0:00: | ER | No Violations | |
-1705465076 | 2012-2-27 0:00: | ER | No Violations | |
-1743871280 | 2016-5-9 0:00:0 | ER | No Violations | |
-1803895427 | 2019-11-18 0:00 | ER | No Violations | |
-1921762814 | 2008-3-25 0:00: | ER | No Violations | 1.00 |
-2031215637 | 2010-11-27 0:00 | ER | No Violations | 0.50 |
-2107294959 | 2016-7-11 0:00: | ER | No Violations | |
-372943447 | 2004-4-22 0:00: | ER | No Violations | |
-481841461 | 2016-1-7 0:00:0 | ER | No Violations | |
-492495910 | 2017-4-27 0:00: | ER | No Violations | |
-538301848 | 2017-10-19 0:00 | ER | No Violations | |
-566621851 | 2004-11-18 0:00 | ER | No Violations | |
-579453604 | 2020-2-24 0:00: | ER | No Violations | |
-617103789 | 2012-6-4 0:00:0 | ER | No Violations | |
-674437916 | 2014-7-17 0:00: | ER | No Violations | |
-734942749 | 2018-10-2 0:00: | ER | No Violations | |
-770595211 | 2006-4-24 0:00: | ER | No Violations | 0.50 |
-793250628 | 2014-3-18 0:00: | ER | No Violations | |
-973291797 | 2018-1-4 0:00:0 | ER | No Violations | |
0006696153 | 2012-12-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0149616241 | 2013-10-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0214649012 | 2013-03-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The initial pressure on annulus was similar to line pressure. Annulus was pressured up to 400 psi and a 15 minute mini pressure test conducted. The final pressure was 400 psi. Well passes test. |
0313025122 | 2014-05-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0352558729 | 2015-08-31 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. The annulus and the injection tubing have equalized. Pressure testing of well head annulus is required. |
0372943447 | 2004-04-22 | Enhanced Recovery Project | No Violations | Injection pressure test. Annular and tubing pressures are equalized. Advised Len rex to repressure annular space and test. Report results to Tom Tomastik. |
0481841461 | 2016-01-07 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0492495910 | 2017-04-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0538301848 | 2017-10-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The operator conducted a monthly pressure test that was witnessed. The annulus had zero pressure loss over fifteen minutes. |
0566621851 | 2004-11-18 | Enhanced Recovery Project | No Violations | Injection pressure test. |
0617103789 | 2012-06-04 | Enhanced Recovery Project | No Violations | Inspect Well. |
0625908752 | 2015-11-12 | Work Over Reconditioning | No Violations | The well is constructed with 2 3/8 inch tubing at a depth of 590 feet cemented to the surface. The well is open hole to the total depth of 720 feet. The J hook pin was missing on the packer causing the failure. The packer was replaced. Two feet of the top most joint of PVC lined tubing was cut off and then re-threaded. Total of 18 joints of 25 foot sections of PVC lined one Inch tubing and one 23 foot joint of PVC lined tubing was run in the hole with a parmaco style packer set in compression. Approximately 300 gallon of fresh water were pumped through the tubing and circulated to the surface prior to setting the packer. The packer was set and the annulus was pressured up to 390 psi. The pressure was monitored for 15 minutes with zero pressure loss. The well passes the Mechanical Integrity Test. The well head was reconstructed with new parts and put into production. |
0630334402 | 2017-07-14 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The operator discovered a leak with the flexible flow line. The line was dug up and replaced. The well is in compliance. |
0651547493 | 2015-11-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The injection tubing and annulus have equalized. Notified operator, the service rig was subsequently mobilized to well to replace the packer and top joint. Passed Mechanical integrity test on 11/12/2015. |
0674437916 | 2014-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Well head has a slight leak. |
0722519662 | 2012-09-11 | Enhanced Recovery Project | No Violations | Inspect Well. Site ok. |
0729700632 | 2011-04-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0734942749 | 2018-10-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0770595211 | 2006-04-24 | Enhanced Recovery Project | No Violations | Injection and annular pressure test. |
0788906684 | 2008-12-10 | Enhanced Recovery Project | No Violations | Mini test on annulus. Pressured up to 400 psi and 0 psi decline in 15 minutes. |
0793250628 | 2014-03-18 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0806968416 | 2003-08-07 | Enhanced Recovery Project | No Violations | |
0973291797 | 2018-01-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0996438880 | 2018-05-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Upon inspection the annulus valve was in very poor condition. The operator replaced the valve and pressured the annulus. The pressure was monitored for 15 minutes with less than 3 percent pressure loss. The well is in compliance. |
1031105108 | 2015-05-21 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. The annulus inspection test valve is rusted shut. |
1041141469 | 2011-07-12 | Enhanced Recovery Project | No Violations | inspect well. |
1069527216 | 2007-03-30 | Enhanced Recovery Project | Violations Noted | Annulus and injection pressure test. Annular side is reading 0 psi and injection pressure is 350 psi. Pressure up on annular side to 200 psi and report. |
1072400491 | 2017-01-09 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1116375683 | 2005-05-17 | Enhanced Recovery Project | No Violations | Injection well test. GPS location and update to RBDMS. |
1118565035 | 2018-08-20 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1120402922 | 2015-03-31 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Pressure was equalized, well was temporarily shut in. The annulus was pressure tested at 387 PSI with no pressure loss over 15 minutes. Test passed and well was put back into production. |
1130729312 | 2007-10-12 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. No box around well. |
1133454819 | 2005-12-01 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressures are equalized at 340psi. |
1138223262 | 2006-01-25 | Enhanced Recovery Project | Violations Noted | Packer has been set and pressures are ann. 340 & inj. 350. Snow, 27 degrees. |
1166188995 | 2006-12-15 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1177085956 | 2007-04-20 | Enhanced Recovery Project | No Violations | Pressure test. Annular side held at 310 psi for 15 minutes with no decline. Injection pressure is 330 psi. NOV in compliance. |
1216707566 | 2013-08-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1266381658 | 2020-1-28 0:00: | ER | No Violations | |
1270558102 | 2010-04-06 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1286382173 | 2010-10-06 | Enhanced Recovery Project | No Violations | Installing a separator at injection well head. PSI at 350. |
1334367035 | 2013-05-22 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Well head injector line valve is seeping. |
1361616018 | 2009-10-07 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1478704206 | 2016-11-07 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
149616241 | 2013-10-29 0:00 | ER | No Violations | |
1556778093 | 2015-09-23 | Enhanced Recovery Project | No Violations | Operator conducted pressure test on well. The well was pressure tested for 15 minutes. The pressure loss was less than 1 percent. Well is incompliance. Compliance notice of 8/31/2015 can be resolved. |
1671661143 | 2014-10-28 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1705465076 | 2012-02-27 | Enhanced Recovery Project | No Violations | inspect well. |
1743871280 | 2016-05-09 | Enhanced Recovery Project | No Violations | Follow up inspection from April 25, 2016. The operator has replaced the fitting that were in poor condition. |
1893125547 | 2008-12-03 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. Pressures are equal at 320 psi. |
1921762814 | 2008-03-25 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
1958601843 | 2011-10-17 | Enhanced Recovery Project | No Violations | Inspect well. |
2031215637 | 2010-11-27 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
2107294959 | 2016-07-11 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The well head fittings have been repaired recently. |
2139217621 | 2016-04-25 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The Injection line nipple is in poor condition. |
214649012 | 2013-3-4 0:00:0 | ER | No Violations | |
313025122 | 2014-5-6 0:00:0 | ER | No Violations | |
352106306 | 2019-1-14 0:00: | ER | No Violations | |
352558729 | 2015-8-31 0:00: | ER | No Violations | |
625908752 | 2015-11-12 0:00 | WR | No Violations | |
630334402 | 2017-7-14 0:00: | ER | No Violations | |
651547493 | 2015-11-2 0:00: | ER | No Violations | |
6696153 | 2012-12-4 0:00: | ER | No Violations | |
722519662 | 2012-9-11 0:00: | ER | No Violations | |
729700632 | 2011-4-13 0:00: | ER | No Violations | 0.50 |
788906684 | 2008-12-10 0:00 | ER | No Violations | 0.50 |
806968416 | 2003-8-7 0:00:0 | ER | No Violations | |
963087416 | 2019-7-24 0:00: | ER | No Violations | |
996438880 | 2018-5-2 0:00:0 | ER | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0352558729 | US-OH-123704 | 2015-10-07 | Failure to conduct or pass mech. integrity test | |
1031105108 | US-OH-100504 | 2015-07-17 | Failure to monitor annulus pressure | |
1069527216 | US-OH-101437 | 2007-03-30 | Failure to conduct or pass mech. integrity test | |
1133454819 | US-OH-103391 | 2005-12-01 | Mechanical failure/contamination | |
1138223262 | US-OH-103503 | 2005-12-01 | Mechanical failure/contamination | |
1893125547 | US-OH-119016 | 2008-12-03 | Failure to conduct or pass mech. integrity test |
For data sources see[9]