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Well ID: 34-005-23070 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: GORTNER ROBERT & PAULINE (ERP #12) | |
License Status: Active Injection | |
License Date: 1974-08-21 | |
Spud Date: 1974-10-24 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-11-13 | |
Well Total Depth: 695.00 ft | |
Configuration: Vertical | |
Latitude: 40.890000 | |
Longitude: -82.160000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1801-01-02 | 133 QUAKER STATE OIL REF CORP |
Unknown | 1802-01-01 | Issued Date 8/7/74 Expired Date Acres Tool Type Proposed Formation Proposed Depth Proposed Drill Depth |
Original Spud | 1974-10-24 | DRILLED BY KLAEGER AND BLODGETT |
Completed | 1974-11-13 | DRILLED BY KLAEGER AND BLODGETT |
Reached Total Depth | 1974-11-13 | DRILLED BY KLAEGER AND BLODGETT |
Construction Permit Expires | 1975-08-07 | DRILLED BY KLAEGER AND BLODGETT |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate |
Annulus Pressure Monitoring Approved | 1996-04-15 | DRILLED BY KLAEGER AND BLODGETT |
Change of Owner | 2002-02-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER |
Change of Owner | 2008-04-24 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Last Compliance Report | 2010-04-28 | DRILLED BY KLAEGER AND BLODGETT |
Record Last Modified | 2018-03-05 | DRILLED BY KLAEGER AND BLODGETT |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-22 | 555 | 600 | 0 |
2000-05-22 | 600 | 669 | 0 |
600 | 669 | 0 | |
555 | 600 | 0 | |
555 | 600 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 165 Qts | 0 | |||
NITR | 0 | 171 Qts | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | DEEP RESOURCES LLC | 0.00 | 133.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | DEEP RESOURCES LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1103265926 | 2019-9-17 0:00: | ER | No Violations | |
-1145270852 | 2017-4-13 0:00: | ER | No Violations | |
-1148007059 | 2015-10-26 0:00 | ER | No Violations | |
-1195296621 | 2012-2-27 0:00: | ER | No Violations | |
-1282148972 | 2016-10-19 0:00 | ER | No Violations | |
-1284235227 | 2014-7-17 0:00: | ER | No Violations | |
-1286441862 | 2020-4-22 0:00: | ER | No Violations | |
-1317446064 | 2016-1-6 0:00:0 | ER | No Violations | |
-1323718202 | 2016-4-19 0:00: | ER | No Violations | |
-1348610193 | 2006-12-14 0:00 | ER | No Violations | 0.50 |
-1384208609 | 2012-11-27 0:00 | ER | No Violations | |
-1603011311 | 2015-3-31 0:00: | ER | No Violations | |
-1777184423 | 2017-7-19 0:00: | ER | No Violations | |
-1783086140 | 2019-10-23 0:00 | ER | No Violations | |
-1874455973 | 2010-4-27 0:00: | ER | No Violations | 2.00 |
-1994117389 | 2014-10-28 0:00 | ER | No Violations | |
-2134462168 | 2006-1-25 0:00: | ER | No Violations | 0.50 |
-252390129 | 2009-10-7 0:00: | ER | No Violations | 1.00 |
-345877647 | 2004-11-18 0:00 | ER | No Violations | |
-705241194 | 2011-7-12 0:00: | ER | No Violations | |
-793071710 | 2013-3-4 0:00:0 | ER | No Violations | |
-986695682 | 2018-1-4 0:00:0 | ER | No Violations | |
-995059370 | 2012-9-20 0:00: | ER | No Violations | |
0011150855 | 2013-12-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Pump shut down during inspection. |
0107490693 | 2018-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0154650848 | 2008-02-21 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
0162233483 | 2004-04-22 | Enhanced Recovery Project | No Violations | Injection pressure test. |
0167008043 | 2015-09-23 | Enhanced Recovery Project | No Violations | Operator attempted to perform pressure test on well. Pressure bled off during test. |
0240249329 | 2008-12-10 | Enhanced Recovery Project | No Violations | Mini test on annulus. Pressured up to 400 psi and 0 psi decline in 15 minutes. |
0252390129 | 2009-10-07 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0345877647 | 2004-11-18 | Enhanced Recovery Project | No Violations | Injection pressure test. |
0495965848 | 2009-04-25 | Enhanced Recovery Project | No Violations | Brine leak has been repaired. 2 tubing collar replaced. NOV in compliance. |
0539252458 | 2014-03-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0601250857 | 2010-11-26 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0626026498 | 2012-05-30 | Enhanced Recovery Project | No Violations | Inspect Well. |
0680452495 | 2013-04-15 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Passed test. |
0705241194 | 2011-07-12 | Enhanced Recovery Project | No Violations | inspect well. |
0723479086 | 2011-11-17 | Enhanced Recovery Project | No Violations | Inspect well. |
0724794435 | 2009-04-23 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. 2 3/8 tubing leaking at ground level. Shut well in until repaired. Install 1/2 nipple on injection tubing it has a 1, cannot screw in gauge. |
0793071710 | 2013-03-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0986695682 | 2018-01-04 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. Upon inspection the injection tubing was leaking through a split in the pipe. The operator installed a clamp patch and stopped the leak. The annulus and the injection tubing were equalized. The well needs to be serviced. The well was shut in. Compliance notice issued. |
0992905456 | 2010-03-30 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Leak in annular pipe. |
0995059370 | 2012-09-20 | Enhanced Recovery Project | No Violations | Inspect Well. Site ok. |
1068818272 | 2003-11-13 | Enhanced Recovery Project | No Violations | |
107490693 | 2018-4-19 0:00: | ER | No Violations | |
1115045185 | 2005-04-28 | Enhanced Recovery Project | No Violations | Injection pressure test. Tested pressure inside pump house at primary pump and reading is 350 psi. |
11150855 | 2013-12-4 0:00: | ER | No Violations | |
1144939095 | 2006-04-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Constructed with 2 tubing cemented at Berea cap with 1 tubing on a packer used for injection. |
1145270852 | 2017-04-13 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1148007059 | 2015-10-26 | Enhanced Recovery Project | No Violations | The operator originally installed 20 one inch joints of tubing at 25 feet long and one five foot long joint. The packer was originally set at 505 feet below grade. On May 22, 2001 the tubing was pulled from the well and run into the hole on June 1, 2001 a total of 20 joints and one 5 foot joint; the packer was set at 505 feet below grade. On May 27, 2010 workover on the well a total of 19 joints of one inch at 25 feet long tubing were run in the hole with two six foot joints. The packer was set at 487 feet below grade. On October 22, 2015 the PVC was showing at the well head. The operator released the packer and pulled the tubing up one foot and cut off the deteriorated section and re-threaded the tubing. The annulus was filled with water and inhibitor; reset the packer and pressure tested well. The operator installed a tie down hanger to hold packer in compression. A mechanical integrity test was conducted on the well on October 26, 2015. Well annulus was pressured to 375 psi and held for 15 minutes with zero pressure loss. Well passes. Well is put into production. Compliance notice has been resolved. |
1192540508 | 2007-10-16 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1195296621 | 2012-02-27 | Enhanced Recovery Project | No Violations | Inspect well. |
1228317292 | 2008-12-03 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. |
1228891428 | 2017-01-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1254156478 | 2018-10-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1270237224 | 2010-04-02 | Enhanced Recovery Project | Violations Noted | Reset packer and test annulus pressure @ 370 psi. Pressures equalized @ 370 psi. Leak has been repaired. Shut well in until packer is replaced. |
1282148972 | 2016-10-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1284235227 | 2014-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1302697519 | 2011-04-13 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1306765971 | 2015-05-21 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. The leaking nipple was replaced. A nipple that was not replaced began to leak. Operator went to location to perform repairs. |
1317446064 | 2016-01-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1323718202 | 2016-04-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1343574965 | 2007-03-30 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
1348610193 | 2006-12-14 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1355895596 | 2014-05-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1384208609 | 2012-11-27 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1446622877 | 2015-09-23 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1469623342 | 2016-07-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1518550964 | 2018-02-13 | Work Over Reconditioning | No Violations | An integrity test was conducted on January 4, 2018. The well failed the test. On February 13, 2018 the operator tripped the tubing and packer out of the hole and replaced the packer and change over. There were 19 joints at 25 feet long joints and one six foot joint of PVC lined tubing with a new packer and change over were run in the hole. The packer was set at 481 feet below grade. The annulus was loaded with about 60 gallons of fresh water and inhibitor from the surface. The well head was constructed and the annulus was pressured. The annulus was monitored for 15 minutes at 410 psi with zero pressure loss. The well passed the pressure test. The operator was notified that the well was in compliance and could be put into operation. The compliance notice of January 4, 2018 has been complied with and resolved. |
1533317005 | 2018-07-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
154650848 | 2008-2-21 0:00: | ER | No Violations | 1.00 |
1563210015 | 2019-7-10 0:00: | ER | No Violations | |
1599669854 | 2020-7-14 0:00: | ER | No Violations | |
1603011311 | 2015-03-31 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Pressure has equalized well temporarily shut in until annulus can be pressure tested. |
1622028689 | 2015-05-20 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. The injection line nipple at the connection union is leaking. |
162233483 | 2004-4-22 0:00: | ER | No Violations | |
167008043 | 2015-9-23 0:00: | ER | No Violations | |
1777184423 | 2017-07-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1874455973 | 2010-04-27 | Enhanced Recovery Project | No Violations | Pulled old packer and replaced with a rebuilt Butler Larkin packer. Added inhibitor to and filled annulus. Pressure tested at 250 psi for 15 minutes and 0 psi decline. NOV in compliance. |
1890045374 | 2017-10-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1922061385 | 2019-4-10 0:00: | ER | No Violations | |
1968764278 | 2019-1-10 0:00: | ER | No Violations | |
1994117389 | 2014-10-28 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
2047079568 | 2015-09-28 | Enhanced Recovery Project | Violations Noted | Inspect well at request of operator. The annulus and well have equalized. Bled off some pressure from annulus. Pressure gradually increased. Packer is leaking and may require resetting. Mechanical integrity has failed. NOTE: The well was worked on and MIT passed on 10/26/2015. |
2134462168 | 2006-01-25 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
240249329 | 2008-12-10 0:00 | ER | No Violations | 0.50 |
495965848 | 2009-4-25 0:00: | ER | No Violations | 0.50 |
539252458 | 2014-3-17 0:00: | ER | No Violations | |
601250857 | 2010-11-26 0:00 | ER | No Violations | 0.50 |
626026498 | 2012-5-30 0:00: | ER | No Violations | |
680452495 | 2013-4-15 0:00: | ER | No Violations | |
723479086 | 2011-11-17 0:00 | ER | No Violations | |
724794435 | 2009-4-23 0:00: | ER | No Violations | 1.00 |
992905456 | 2010-3-30 0:00: | ER | No Violations | 1.00 |
998627185 | 2020-1-23 0:00: | ER | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0724794435 | US-OH-128245 | 2009-04-23 | Failure to conduct or pass mech. integrity test | |
0986695682 | US-OH-131298 | 2018-03-06 | 9-5-10(H) | Mechanical failure/contamination |
1228317292 | US-OH-106158 | 2008-12-03 | Failure to conduct or pass mech. integrity test | |
1270237224 | US-OH-107536 | 2010-04-02 | Failure to conduct or pass mech. integrity test | |
1622028689 | US-OH-115941 | 2015-07-17 | Mechanical failure/contamination | |
2047079568 | US-OH-120848 | 2015-12-15 | Mechanical failure/contamination |
For data sources see[9]