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34-005-23070

Well Details

Well ID: 34-005-23070
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: GORTNER ROBERT & PAULINE (ERP #12)
License Status: Active Injection
License Date: 1974-08-21
Spud Date: 1974-10-24
Spud Drilling Contractor:
Final Drill Date: 1974-11-13
Well Total Depth: 695.00 ft
Configuration: Vertical
Latitude: 40.890000
Longitude: -82.160000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 133 QUAKER STATE OIL REF CORP
Unknown 1802-01-01 Issued Date 8/7/74 Expired Date Acres Tool Type Proposed Formation Proposed Depth Proposed Drill Depth
Original Spud 1974-10-24 DRILLED BY KLAEGER AND BLODGETT
Completed 1974-11-13 DRILLED BY KLAEGER AND BLODGETT
Reached Total Depth 1974-11-13 DRILLED BY KLAEGER AND BLODGETT
Construction Permit Expires 1975-08-07 DRILLED BY KLAEGER AND BLODGETT
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate
Annulus Pressure Monitoring Approved 1996-04-15 DRILLED BY KLAEGER AND BLODGETT
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Last Compliance Report 2010-04-28 DRILLED BY KLAEGER AND BLODGETT
Record Last Modified 2018-03-05 DRILLED BY KLAEGER AND BLODGETT

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-22 555 600 0
2000-05-22 600 669 0
600 669 0
555 600 0
555 600 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 165 Qts 0
NITR 0 171 Qts 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC 0.00 133.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1103265926 2019-9-17 0:00: ER No Violations
-1145270852 2017-4-13 0:00: ER No Violations
-1148007059 2015-10-26 0:00 ER No Violations
-1195296621 2012-2-27 0:00: ER No Violations
-1282148972 2016-10-19 0:00 ER No Violations
-1284235227 2014-7-17 0:00: ER No Violations
-1286441862 2020-4-22 0:00: ER No Violations
-1317446064 2016-1-6 0:00:0 ER No Violations
-1323718202 2016-4-19 0:00: ER No Violations
-1348610193 2006-12-14 0:00 ER No Violations 0.50
-1384208609 2012-11-27 0:00 ER No Violations
-1603011311 2015-3-31 0:00: ER No Violations
-1777184423 2017-7-19 0:00: ER No Violations
-1783086140 2019-10-23 0:00 ER No Violations
-1874455973 2010-4-27 0:00: ER No Violations 2.00
-1994117389 2014-10-28 0:00 ER No Violations
-2134462168 2006-1-25 0:00: ER No Violations 0.50
-252390129 2009-10-7 0:00: ER No Violations 1.00
-345877647 2004-11-18 0:00 ER No Violations
-705241194 2011-7-12 0:00: ER No Violations
-793071710 2013-3-4 0:00:0 ER No Violations
-986695682 2018-1-4 0:00:0 ER No Violations
-995059370 2012-9-20 0:00: ER No Violations
0011150855 2013-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pump shut down during inspection.
0107490693 2018-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0154650848 2008-02-21 Enhanced Recovery Project No Violations Annulus and injection pressure test.
0162233483 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test.
0167008043 2015-09-23 Enhanced Recovery Project No Violations Operator attempted to perform pressure test on well. Pressure bled off during test.
0240249329 2008-12-10 Enhanced Recovery Project No Violations Mini test on annulus. Pressured up to 400 psi and 0 psi decline in 15 minutes.
0252390129 2009-10-07 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0345877647 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
0495965848 2009-04-25 Enhanced Recovery Project No Violations Brine leak has been repaired. 2 tubing collar replaced. NOV in compliance.
0539252458 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0601250857 2010-11-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0626026498 2012-05-30 Enhanced Recovery Project No Violations Inspect Well.
0680452495 2013-04-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Passed test.
0705241194 2011-07-12 Enhanced Recovery Project No Violations inspect well.
0723479086 2011-11-17 Enhanced Recovery Project No Violations Inspect well.
0724794435 2009-04-23 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. 2 3/8 tubing leaking at ground level. Shut well in until repaired. Install 1/2 nipple on injection tubing it has a 1, cannot screw in gauge.
0793071710 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0986695682 2018-01-04 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. Upon inspection the injection tubing was leaking through a split in the pipe. The operator installed a clamp patch and stopped the leak. The annulus and the injection tubing were equalized. The well needs to be serviced. The well was shut in. Compliance notice issued.
0992905456 2010-03-30 Enhanced Recovery Project No Violations Injection and annulus pressure test. Leak in annular pipe.
0995059370 2012-09-20 Enhanced Recovery Project No Violations Inspect Well. Site ok.
1068818272 2003-11-13 Enhanced Recovery Project No Violations
107490693 2018-4-19 0:00: ER No Violations
1115045185 2005-04-28 Enhanced Recovery Project No Violations Injection pressure test. Tested pressure inside pump house at primary pump and reading is 350 psi.
11150855 2013-12-4 0:00: ER No Violations
1144939095 2006-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test. Constructed with 2 tubing cemented at Berea cap with 1 tubing on a packer used for injection.
1145270852 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1148007059 2015-10-26 Enhanced Recovery Project No Violations The operator originally installed 20 one inch joints of tubing at 25 feet long and one five foot long joint. The packer was originally set at 505 feet below grade. On May 22, 2001 the tubing was pulled from the well and run into the hole on June 1, 2001 a total of 20 joints and one 5 foot joint; the packer was set at 505 feet below grade. On May 27, 2010 workover on the well a total of 19 joints of one inch at 25 feet long tubing were run in the hole with two six foot joints. The packer was set at 487 feet below grade. On October 22, 2015 the PVC was showing at the well head. The operator released the packer and pulled the tubing up one foot and cut off the deteriorated section and re-threaded the tubing. The annulus was filled with water and inhibitor; reset the packer and pressure tested well. The operator installed a tie down hanger to hold packer in compression. A mechanical integrity test was conducted on the well on October 26, 2015. Well annulus was pressured to 375 psi and held for 15 minutes with zero pressure loss. Well passes. Well is put into production. Compliance notice has been resolved.
1192540508 2007-10-16 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1195296621 2012-02-27 Enhanced Recovery Project No Violations Inspect well.
1228317292 2008-12-03 Enhanced Recovery Project Violations Noted Injection and annulus pressure test.
1228891428 2017-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1254156478 2018-10-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1270237224 2010-04-02 Enhanced Recovery Project Violations Noted Reset packer and test annulus pressure @ 370 psi. Pressures equalized @ 370 psi. Leak has been repaired. Shut well in until packer is replaced.
1282148972 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1284235227 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1302697519 2011-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1306765971 2015-05-21 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The leaking nipple was replaced. A nipple that was not replaced began to leak. Operator went to location to perform repairs.
1317446064 2016-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1323718202 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1343574965 2007-03-30 Enhanced Recovery Project No Violations Annulus and injection pressure test.
1348610193 2006-12-14 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1355895596 2014-05-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1384208609 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1446622877 2015-09-23 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1469623342 2016-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1518550964 2018-02-13 Work Over Reconditioning No Violations An integrity test was conducted on January 4, 2018. The well failed the test. On February 13, 2018 the operator tripped the tubing and packer out of the hole and replaced the packer and change over. There were 19 joints at 25 feet long joints and one six foot joint of PVC lined tubing with a new packer and change over were run in the hole. The packer was set at 481 feet below grade. The annulus was loaded with about 60 gallons of fresh water and inhibitor from the surface. The well head was constructed and the annulus was pressured. The annulus was monitored for 15 minutes at 410 psi with zero pressure loss. The well passed the pressure test. The operator was notified that the well was in compliance and could be put into operation. The compliance notice of January 4, 2018 has been complied with and resolved.
1533317005 2018-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
154650848 2008-2-21 0:00: ER No Violations 1.00
1563210015 2019-7-10 0:00: ER No Violations
1599669854 2020-7-14 0:00: ER No Violations
1603011311 2015-03-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pressure has equalized well temporarily shut in until annulus can be pressure tested.
1622028689 2015-05-20 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The injection line nipple at the connection union is leaking.
162233483 2004-4-22 0:00: ER No Violations
167008043 2015-9-23 0:00: ER No Violations
1777184423 2017-07-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1874455973 2010-04-27 Enhanced Recovery Project No Violations Pulled old packer and replaced with a rebuilt Butler Larkin packer. Added inhibitor to and filled annulus. Pressure tested at 250 psi for 15 minutes and 0 psi decline. NOV in compliance.
1890045374 2017-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1922061385 2019-4-10 0:00: ER No Violations
1968764278 2019-1-10 0:00: ER No Violations
1994117389 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2047079568 2015-09-28 Enhanced Recovery Project Violations Noted Inspect well at request of operator. The annulus and well have equalized. Bled off some pressure from annulus. Pressure gradually increased. Packer is leaking and may require resetting. Mechanical integrity has failed. NOTE: The well was worked on and MIT passed on 10/26/2015.
2134462168 2006-01-25 Enhanced Recovery Project No Violations Annulus and injection pressure test.
240249329 2008-12-10 0:00 ER No Violations 0.50
495965848 2009-4-25 0:00: ER No Violations 0.50
539252458 2014-3-17 0:00: ER No Violations
601250857 2010-11-26 0:00 ER No Violations 0.50
626026498 2012-5-30 0:00: ER No Violations
680452495 2013-4-15 0:00: ER No Violations
723479086 2011-11-17 0:00 ER No Violations
724794435 2009-4-23 0:00: ER No Violations 1.00
992905456 2010-3-30 0:00: ER No Violations 1.00
998627185 2020-1-23 0:00: ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0724794435 US-OH-128245 2009-04-23 Failure to conduct or pass mech. integrity test
0986695682 US-OH-131298 2018-03-06 9-5-10(H) Mechanical failure/contamination
1228317292 US-OH-106158 2008-12-03 Failure to conduct or pass mech. integrity test
1270237224 US-OH-107536 2010-04-02 Failure to conduct or pass mech. integrity test
1622028689 US-OH-115941 2015-07-17 Mechanical failure/contamination
2047079568 US-OH-120848 2015-12-15 Mechanical failure/contamination

For data sources see[9]

References