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34-005-23780

Well Details

Well ID: 34-005-23780
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Country: United States
State: Ohio
County: Ashland
Municipality: Sullivan Township
Operator Name: KILLBUCK CREEK OIL CO LLC
Well Pad ID:
Farm/Lease Name: RICE FARMS
License Status: Producing
License Date: 1985-06-05
Spud Date: 1985-06-08
Spud Drilling Contractor: H & S DRLG
Final Drill Date: 1985-07-06
Well Total Depth: 2731.00 ft
Configuration: Vertical
Latitude: 41.020000
Longitude: -82.200000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-12-17 130 LESLIE OIL & GAS CO INC GeoDate 12/17/84
Oil and Gas 1984-12-17 Issued Date 12/17/84 Expired Date 6/15/85 Acres 0129880 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1985-06-05 130 LESLIE OIL & GAS CO INC GeoDate 6/5/85
Oil and Gas 1985-06-05 Issued Date 12/17/84 Expired Date 6/15/85 Acres 0080000 Tool Type CT Proposed Formation CLINTON Proposed Depth 02731 Proposed Drill Depth 02731
Original Spud 1985-06-08 RL 6-8-85
Construction Permit Expires 1985-06-15 RL 6-8-85
Completed 1985-07-06 RL 6-8-85
Reached Total Depth 1985-07-06 RL 6-8-85
Completion Report Received 1985-12-24 RL 6-8-85
CO 1993-09-27 54 TITAN ENERGY CORP GeoDate 6/5/85
Change of Owner 2009-06-08 Operator changed from 54, TITAN ENERGY CORP to 8026, KILLBUCK CREEK OIL CO LLC
Record Last Modified 2017-02-15 RL 6-8-85

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2685 2692 6
2685 2692 6
2685 2692 6

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 50000 Gal 50000 FRAC;H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 LESLIE OIL & GAS CO INC 123339.00 0.00 343
1989 LESLIE OIL & GAS CO INC 4425.00 0.00 365
1990 LESLIE OIL & GAS CO INC 3423.00 0.00 365
1991 LESLIE OIL & GAS CO INC 2696.00 0.00 365
1992 TITAN ENERGY CORP 1808.00 0.00 365
1994 TITAN ENERGY CORP 1165.00 0.00 365
1997 TITAN ENERGY CORP 0.00 0.00 365
2010 KILLBUCK CREEK OIL CO LLC 0.00 0.00 0
2012 KILLBUCK CREEK OIL CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 LESLIE OIL & GAS CO INC Brine 0 343
1989 LESLIE OIL & GAS CO INC Brine 0 365
1990 LESLIE OIL & GAS CO INC Brine 0 365
1991 LESLIE OIL & GAS CO INC Brine 0 365
1992 TITAN ENERGY CORP Brine 0 365
1994 TITAN ENERGY CORP Brine 0 365
1997 TITAN ENERGY CORP Brine 365
2010 KILLBUCK CREEK OIL CO LLC Brine 0 0
2012 KILLBUCK CREEK OIL CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1104782480 2015-11-5 0:00: PW No Violations 1.00
-1180417863 2016-5-11 0:00: PW No Violations 1.00
-1671120918 2016-5-2 0:00:0 PW No Violations 0.50
-1860775542 2020-6-12 0:00: PW No Violations
-1933045686 2014-3-18 0:00: PW No Violations 1.00
-470857316 2018-9-20 0:00: PW No Violations
-950838349 2019-12-10 0:00 PW No Violations
0470857316 2018-09-20 Production Wells No Violations Inspection of the well was made with Steve Ochs, Northwest Region Supervisor. The well location was not accessible due to thick brush. Gas was heard leaking from the well during attempts to access it. The operator is not in compliance with Chiefs Order 2016-37.
0819243891 2014-12-16 Production Wells No Violations There are tire tracks in the farm field back to the entrance to the well location in the woods. There has been no work done at the well location. The well is equipped with tubing and a gate valve. The well head is leaking gas. ID has not been posted, vegetation has not been cleared around the tank, production unit or well.
1092435895 2014-07-15 Production Wells No Violations The operator has not made any repairs at the well location. ID has not been posted. The operator stated that he is waiting for Gatherco to install pipeline. He was advised that work can be done on the well and ID posted without waiting on pipeline to be installed. He has been stating that he is waiting on pipeline for over a year. I reminded him of the plug notice on the well and that it is due to be done by 12/20/14.
1104782480 2015-11-05 Production Wells No Violations The well is shut in and unidentified. There is a 100 barrel tank in the tank battery. The tank is rusted. Gas is leaking from the wellhead. There is a swage with a gate valve on the 4.5 inch casing. The swage goes to 2 inch flowline. The well and tank are overgrown with brush and trees.
1180417863 2016-05-11 Production Wells No Violations The well is unidentified. The well is equipped with a gate valve on the production casing. Gas is leaking from the wellhead on the surface-production annulus. The tank battery and well location are overgrown with trees and brush. The operator is not in compliance with Chiefs Order 2016-37.
1316006180 2014-06-19 Production Wells Violations Noted The well is not in production. There is no ID at the well or tank battery. The location is overgrown with trees and brush and there is a gas leak from the well head. The well is not in compliance and needs to be plugged. Complete plugging and restoration of the location by December 20, 2014.
1516205911 2018-01-17 Production Wells No Violations The well is unidentified and idle. Gas is leaking from the slips on the wellhead around the production casing. The leak can be heard from the lease road. The gas detector was reading 5 to 7 on the LEL 12 feet from the wellhead. The detector alarmed for LEL at the wellhead within 3 feet of the leak. No hydrogen sulfide detected. The tank battery and wellhead are overgrown with trees and brush. Chiefs Order 2016-37 requiring plugging within 30 days was issued to Killbuck Creek on February 11, 2016 via certified mail. The operator has not complied with the order or corrected deficiencies at the well.
1671120918 2016-05-02 Production Wells No Violations The operator has not made any corrective actions at the location. They have not obtained a plug permit. No appeal of the order was filed. They are not in compliance with Chiefs Order 2016-37.
1933045686 2014-03-18 Production Wells No Violations Requested by Columbus office to verify well location. The well is equipped with a 100 Bbl fluid tank and a production unit. The production unit is overgrown with brush and trees. The well is equipped with a full opening gate valve on the tubing. The well is not in operation, no ID is posted at the location, and the well site is not being tended. The well head is overgrown with brush.
81037600 2019-6-25 0:00: PW No Violations
819243891 2014-12-16 0:00 PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1316006180 US-OH-109002 2014-07-07 Well shall be plugged

For data sources see[9]

References