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Well ID: 34-005-61837 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: MILLER THOMAS JR | |
License Status: Producing | |
License Date: 1963-11-22 | |
Spud Date: 1963-11-04 | |
Spud Drilling Contractor: | |
Final Drill Date: 1963-11-16 | |
Well Total Depth: 715.00 ft | |
Configuration: Vertical | |
Latitude: 40.890000 | |
Longitude: -82.150000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Completed | 1963-11-16 | WATERFLOOD |
Reached Total Depth | 1963-11-16 | WATERFLOOD |
Change of Owner | 2008-05-05 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Record Last Modified | 2017-02-15 | WATERFLOOD |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1899-12-30 | 570 | 700 | 0 |
570 | 700 | 0 | |
570 | 700 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 0 | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | DEEP RESOURCES LLC | 0.00 | 139.00 | 365 |
2009 | DEEP RESOURCES LLC | 0.00 | 138.00 | 365 |
2010 | DEEP RESOURCES LLC | 0.00 | 110.00 | 365 |
2011 | DEEP RESOURCES LLC | 0.00 | 104.00 | 365 |
2012 | DEEP RESOURCES LLC | 0.00 | 111.00 | 366 |
2013 | DEEP RESOURCES LLC | 0.00 | 103.00 | 365 |
2014 | DEEP RESOURCES LLC | 0.00 | 95.00 | 365 |
2015 | DEEP RESOURCES LLC | 0.00 | 83.00 | 365 |
2016 | DEEP RESOURCES LLC | 0.00 | 44.00 | 365 |
2017 | DEEP RESOURCES LLC | 0.00 | 61.00 | 365 |
2018 | DEEP RESOURCES LLC | 0.00 | 74.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | DEEP RESOURCES LLC | Brine | 0 | 365 |
2009 | DEEP RESOURCES LLC | Brine | 0 | 365 |
2010 | DEEP RESOURCES LLC | Brine | 0 | 365 |
2011 | DEEP RESOURCES LLC | Brine | 0 | 365 |
2012 | DEEP RESOURCES LLC | Brine | 0 | 366 |
2013 | DEEP RESOURCES LLC | Brine | 365 | |
2014 | DEEP RESOURCES LLC | Brine | 0 | 365 |
2015 | DEEP RESOURCES LLC | Brine | 365 | |
2016 | DEEP RESOURCES LLC | Brine | 0 | 365 |
2017 | DEEP RESOURCES LLC | Brine | 0 | 365 |
2018 | DEEP RESOURCES LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0200560060 | 2015-02-25 | Production Wells | No Violations | The well is equipped with a pump jack and is in production. ID posted. There are 2-200 Bbl tanks and a vault in the tank battery. The vault is due to be replaced with an above ground tank inside the concrete containment structure. The well was pumping during inspection. |
1238084890 | 2009-03-26 | Production Wells | Violations Noted | Landowner was plowing thru waterway in field and broke an underground production line leading from well to tank battery. Crude entered field tile and drained in stream leading to the Muddy Fork River. Len Rex called Division Inspector. I advised to call OEPA due to oil in stream. Owner of company Randy Metheny did not call EPA until 3-26-2009. Spill occurred 3-25-2009. Siphon dam was constructed in stream after I responded to site on 3-26-2009. Oil sheen remains on water from entry point to siphon dam 300 down stream. I walked downstream 1000 and no sheen was visable below dam. Approximately 3 barrels of oil was reported spilled. Photographed stream for EPA and e-mailed. Wes Drake of OEPA responded later. Rain, 40 degrees. |
1238501137 | 2009-03-31 | Production Wells | No Violations | Crude oil is still collecting in siphon dam. Debris has been removed out of stream to allow oil to release. Cleanup to continue on creek bank. Sun, 30 degrees. |
1238769822 | 2009-04-03 | Production Wells | No Violations | All contaminated soil has been removed and graded. Stream is cleaned and siphon dam partially removed. OEPA to instructing company on dam removal.Leak was repaired. NOV in compliance. Rain, 50 degrees. |
200560060 | 2015-2-25 0:00: | PW | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1238084890 | US-OH-106349 | 2009-03-26 | Well operation causing pollution and contamination | |
1238084890 | US-OH-106350 | 2009-03-26 | General Safety | |
1238084890 | US-OH-106351 | 2009-03-26 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[9]