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Well ID: 34-007-21579 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashtabula | |
Municipality: Hartsgrove Township | |
Operator Name: BIG SKY ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: BOYCE DK | |
License Status: Producing | |
License Date: 1980-12-31 | |
Spud Date: 1981-02-18 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-02-24 | |
Well Total Depth: 3678.00 ft | |
Configuration: Vertical | |
Latitude: 41.630000 | |
Longitude: -80.940000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-12-31 | 300 PETROLEUM ENERGY PROD COR GeoDate 12/31/80 |
Oil and Gas | 1980-12-31 | Issued Date 12/31/80 Expired Date Acres 0031200 Tool Type RTF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1981-02-18 | LOG TYPE- LASSER LOG |
Completed | 1981-02-24 | LOG TYPE- LASSER LOG |
Reached Total Depth | 1981-02-24 | LOG TYPE- LASSER LOG |
Completion Report Received | 1981-04-29 | LOG TYPE- LASSER LOG |
CO | 1991-10-09 | 201 GREEN GAS CO GeoDate 12/31/80 |
CO | 1992-04-07 | 1453 GREEN ENERGY INC GeoDate 12/31/80 |
Change of Owner | 2001-02-06 | Operator changed from 1453, GREEN ENERGY INC to 1333, BARR ROBT/dba BIG SKY PET |
Record Last Modified | 2013-10-03 | LOG TYPE- LASSER LOG |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | GREEN ENERGY INC | 844.00 | 0.00 | 165 |
1994 | GREEN ENERGY INC | 771.00 | 0.00 | 365 |
1995 | GREEN ENERGY INC | 522.00 | 0.00 | 365 |
1996 | GREEN ENERGY INC | 739.00 | 31.00 | 365 |
1997 | GREEN ENERGY INC | 424.00 | 0.00 | 365 |
1998 | GREEN ENERGY INC | 560.00 | 0.00 | 245 |
1999 | GREEN ENERGY INC | 424.00 | 0.00 | 242 |
2000 | GREEN ENERGY INC | 751.00 | 0.00 | 365 |
2001 | BIG SKY ENERGY INC | 897.00 | 0.00 | 365 |
2002 | BIG SKY ENERGY INC | 24.00 | 0.00 | 365 |
2003 | BIG SKY ENERGY INC | 5.00 | 0.00 | 365 |
2004 | BIG SKY ENERGY INC | 1067.00 | 0.00 | 365 |
2005 | BIG SKY ENERGY INC | 545.00 | 20.00 | 365 |
2006 | BIG SKY ENERGY INC | 650.00 | 0.00 | 365 |
2007 | BIG SKY ENERGY INC | 195.00 | 0.00 | 365 |
2008 | BIG SKY ENERGY INC | 60.00 | 0.00 | 365 |
2009 | BIG SKY ENERGY INC | 281.00 | 0.00 | 365 |
2010 | BIG SKY ENERGY INC | 281.00 | 0.00 | 365 |
2011 | BIG SKY ENERGY INC | 1410.00 | 0.00 | 365 |
2012 | BIG SKY ENERGY INC | 1529.00 | 0.00 | 366 |
2013 | BIG SKY ENERGY INC | 225.00 | 18.00 | 280 |
2014 | BIG SKY ENERGY INC | 116.00 | 8.00 | 365 |
2016 | BIG SKY ENERGY INC | 0.00 | 0.00 | 0 |
2017 | BIG SKY ENERGY INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | GREEN ENERGY INC | Brine | 1462 | 165 |
1994 | GREEN ENERGY INC | Brine | 193 | 365 |
1995 | GREEN ENERGY INC | Brine | 567 | 365 |
1996 | GREEN ENERGY INC | Brine | 273 | 365 |
1997 | GREEN ENERGY INC | Brine | 76 | 365 |
1998 | GREEN ENERGY INC | Brine | 282 | 245 |
1999 | GREEN ENERGY INC | Brine | 50 | 242 |
2000 | GREEN ENERGY INC | Brine | 343 | 365 |
2001 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2002 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2003 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2004 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2005 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2006 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2007 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2008 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2009 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2010 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2011 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2012 | BIG SKY ENERGY INC | Brine | 0 | 366 |
2013 | BIG SKY ENERGY INC | Brine | 0 | 280 |
2014 | BIG SKY ENERGY INC | Brine | 0 | 365 |
2016 | BIG SKY ENERGY INC | Brine | 0 | 0 |
2017 | BIG SKY ENERGY INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-899386314 | 2018-3-6 0:00:0 | PW | No Violations | |
0039094647 | 2016-05-03 | Production Wells | Violations Noted | My inspection found the tank battery was equipped with one separator. There was a 210 barrel steel tank outside the earthen dike area on the east side. The tank was not connected to anything. There was no identification posted at the tank battery location. There was a oil saturated area at the base of the tank in an area 1.5 x 4 on the south side of the tank. I took one photo of the oil saturated area by the tank. There was a steel tank ladder lying on the ground outside the tank battery area on the south side. While traveling to the well location I observed a plastic flow line on the surface in several areas. The well was equipped with a pumping unit. There was a gas leak from a pressure release valve on the line supplying gas to the pump-jack motor. The valves from the well to the flow line were closed. This well was not in production at the time of my inspection. REQUIRED REMEDIAL WORK: Remove the oil saturated soil from the base of the tank, post identification at the tank battery location for this well, bury the flow line from the tank battery area to the well location and repair the gas leak at the well. |
0599243902 | 2016-12-27 | Production Wells | No Violations | My inspection of this well found there has been no remedial work done to resolve the compliance issues with this well. |
0899386314 | 2018-03-06 | Production Wells | No Violations | I conducted a compliance notice follow-up inspection for compliance notice 39094647. At the time of this inspection, the well was equipped with a pumpjack and the annulus and flow line valves were closed. No leak was observed at the well location. There was a 210 BBL production tank, a mechanical separator, and sales line on site at the tank battery. The 210 BBL tank was outside of the diked battery and disconnected from the other production equipment. The oil impacted area at the base of the 210 BBL tank has not been cleaned up. The flow line from the well to the tank battery location was still above ground and no signage has been added at the well or tank battery location. |
0900193444 | 2005-11-18 | Production Wells | No Violations | Remedial completed . No violations , RESOLVED . |
0905902941 | 2005-11-09 | Production Wells | Violations Noted | Complaintant - Beth Sacerich . Inspection showed a very small gas leak from tubing head packing . |
1474304230 | 2016-09-13 | Production Wells | No Violations | My inspection of this well found the oil saturated area at the base of the production tank has not been removed. Identification has not been posted at the tank battery location. The flow line from the tank battery to the well has not been buried. There was still gas leaking from the supply line to the pump jack motor. |
39094647 | 2016-5-3 0:00:0 | PW | No Violations | |
599243902 | 2016-12-27 0:00 | PW | No Violations | |
900193444 | 2005-11-18 0:00 | PW | No Violations | |
905902941 | 2005-11-9 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0039094647 | US-OH-124153 | 2016-09-14 | Failure to properly bury pipeline | |
0039094647 | US-OH-124154 | 2016-09-14 | Well operation causing pollution and contamination | |
0039094647 | US-OH-124155 | 2016-09-14 | Well insufficiently equipped to prevent escape of oil and gas | |
0039094647 | US-OH-124156 | 2016-09-14 | Failure to legibly identify well | |
0905902941 | US-OH-130339 | 2005-12-11 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[7]