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34-007-22701

Well Details

Well ID: 34-007-22701
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Country: United States
State: Ohio
County: Ashtabula
Municipality: Andover Township
Operator Name: STMX GAS INC DBA AUTUMN RIDGE
Well Pad ID:
Farm/Lease Name: GREGORY
License Status: Producing
License Date: 1995-01-13
Spud Date: 1984-05-19
Spud Drilling Contractor: H.L.H. DRLG
Final Drill Date: 1984-05-23
Well Total Depth: 4113.00 ft
Configuration: Vertical
Latitude: 41.620000
Longitude: -80.570000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1984-04-10 Issued Date 4/10/84 Expired Date 10/7/84 Acres 0040100 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1984-05-17 3184 ASSET RESOURCES INC GeoDate 5/17/84
Oil and Gas 1984-05-17 Issued Date 4/10/84 Expired Date 10/7/84 Acres 0040100 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04113 Proposed Drill Depth 04113
Original Spud 1984-05-19 R.I 5-19-84
Completed 1984-05-23 R.I 5-19-84
Reached Total Depth 1984-05-23 R.I 5-19-84
Completion Report Received 1984-07-26 R.I 5-19-84
CO 1985-03-25 152 ROYAL PETROLEUM PROP INC GeoDate 4/10/84
CO 1995-01-13 3184 ASSET RESOURCES INC GeoDate 1/13/95
Unknown 1995-01-13 Issued Date 1/13/95 Expired Date 1/13/96 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Construction Permit Expires 1996-01-13 R.I 5-19-84
Change of Owner 2010-06-15 Operator changed from 3184, ASSET RESOURCES INC to 2026, SUMMIT PETROLEUM INC
Change of Owner 2015-06-24 Operator changed from 2026, SUMMIT PETROLEUM INC to 8506, AUTUMN RIDGE ENTERPRISES LLC
Change of Owner 2018-04-06 Operator changed from 8506, AUTUMN RIDGE ENTERPRISES LLC to 10108, STMX GAS INC
Record Last Modified 2018-04-06 R.I 5-19-84

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3852 3972 0
3852 3972 0
2006-09-11 3882 3970 29
3882 3970 29
3852 3972 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 1309 Bbl 50000 FRAC:H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 ROYAL PETROLEUM PROP INC 9364.00 388.00 279
1988 ASSET RESOURCES INC 3065.00 78.00 365
1989 ASSET RESOURCES INC 1842.00 97.00 365
1990 ASSET RESOURCES INC 728.00 73.00 365
1991 ASSET RESOURCES INC 411.00 0.00 365
1992 ASSET RESOURCES INC 3.00 0.00 365
1993 ASSET RESOURCES INC 0.00 0.00 0
1994 ASSET RESOURCES INC 0.00 0.00 0
1995 ASSET RESOURCES INC 0.00 0.00 0
2015 AUTUMN RIDGE ENTERPRISES LLC 0.00 0.00 0
2016 AUTUMN RIDGE ENTERPRISES LLC 0.00 0.00 0
2017 AUTUMN RIDGE ENTERPRISES LLC 0.00 0.00 0
2018 STMX GAS INC DBA AUTUMN RIDGE 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 ROYAL PETROLEUM PROP INC Brine 630 279
1988 ASSET RESOURCES INC Brine 374 365
1989 ASSET RESOURCES INC Brine 205 365
1990 ASSET RESOURCES INC Brine 68 365
1991 ASSET RESOURCES INC Brine 0 365
1992 ASSET RESOURCES INC Brine 0 365
1993 ASSET RESOURCES INC Brine 0 0
1994 ASSET RESOURCES INC Brine 0 0
1995 ASSET RESOURCES INC Brine 70 0
2015 AUTUMN RIDGE ENTERPRISES LLC Brine 0 0
2016 AUTUMN RIDGE ENTERPRISES LLC Brine 0 0
2017 AUTUMN RIDGE ENTERPRISES LLC Brine 0 0
2018 STMX GAS INC DBA AUTUMN RIDGE Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1083483272 2019-04-08 Production Wells No Violations I conducted a compliance notice follow---inch casing swage. The production valve was closed at well. There was a one--inch casing swage with two regulators. Flow line has been disconnected from the well. No tank battery is associated with the well. No identification was posted at the well head. Well has not been plugged.
1486046614 2017-01-13 Production Wells Violations Noted My inspection of this well found the equipment at the tank battery location has been removed. There was two 2 inch steel pipes above the ground and were open ended at the tank battery area. The well had the surface casing above the ground level with the production casing in the surface casing head. The production casing had a swage to two inch with a valve. The valve was closed. There was a one inch pipe off of the valve in the swage with big and little joes on the one inch line. The one inch line went underground at the well location. The well was disconnected from the flow line. There was no identification posted for this well at the well or the tank battery locations. REQUIRED REMEDIAL ACTION FROM AUTUMN RIDGE ENTERPRISES LLC: Autumn Ridge Enterprises LLC shall submit a written plugging schedule to Jerry Kohl at The Ohio Department of Natural Resources, Division of Oil & Gas Resources Management, 3575 Forest Lake Drive, Suite 150, Uniontown, Ohio 44685-8116 within 30 days, per OAC 1501: 9-11-05[ B ], and plug the well within 180 days. Autumn Ridge Enterprises LLC will be notified if the plugging schedule is approved or denied. Also post identification at the well location. I contacted Jesse Mullner with Autumn Ridge and told him of the compliance issues with the well. He told me he was not aware of this well but would check into it.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1486046614 US-OH-113807 2017-02-27 Failure to legibly identify well
1486046614 US-OH-113808 2017-02-27 Well shall be plugged

For data sources see[9]

References