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| Well ID: 34-009-21166 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Athens | |
| Municipality: Trimble Township | |
| Operator Name: MATT PROD ENTERPRISES | |
| Well Pad ID: | |
| Farm/Lease Name: H N MAXWELL | |
| License Status: Final Restoration | |
| License Date: 2014-09-12 | |
| Spud Date: 1955-01-24 | |
| Spud Drilling Contractor: | |
| Final Drill Date: 1955-02-08 | |
| Well Total Depth: 1071.00 ft | |
| Configuration: Vertical | |
| Latitude: 39.540000 | |
| Longitude: -82.100000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Original Spud | 1955-01-24 | |
| Completed | 1955-02-08 | |
| Reached Total Depth | 1955-02-08 | |
| APP | 2013-03-06 | Proposed Formations:BEREA, Issued Date:3/6/2013, Expired Date:3/6/2015 12:00:00 PM, Drilling unit acres:43, Proposed Well Type:OG, Proposed Well Class: |
| APP | 2014-09-12 | Proposed Formations:BEREA, Issued Date:9/12/2014, Expired Date:9/11/2016 12:00:00 PM, Drilling unit acres:43, Proposed Well Type:OG, Proposed Well Class: |
| Plugged/Abandoned | 2014-10-10 | |
| Construction Permit Expires | 2016-09-11 | |
| Record Last Modified | 2017-02-10 |
For data sources see[2]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| GEL | 0 | 450 Lbs | 0 |
For data sources see[3]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1993 | MATT PROD ENTERPRISES | 0.00 | 87.00 | 180 |
| 1994 | MATT PROD ENTERPRISES | 0.00 | 71.00 | 180 |
| 1995 | MATT PROD ENTERPRISES | 0.00 | 80.00 | 180 |
| 1996 | MATT PROD ENTERPRISES | 0.00 | 61.00 | 240 |
| 1997 | MATT PROD ENTERPRISES | 0.00 | 73.00 | 210 |
| 1998 | MATT PROD ENTERPRISES | 0.00 | 37.00 | 210 |
| 1999 | MATT PROD ENTERPRISES | 0.00 | 62.00 | 275 |
| 2000 | MATT PROD ENTERPRISES | 0.00 | 62.00 | 240 |
| 2001 | MATT PROD ENTERPRISES | 0.00 | 53.00 | 280 |
| 2002 | MATT PROD ENTERPRISES | 0.00 | 37.00 | 270 |
| 2003 | MATT PROD ENTERPRISES | 0.00 | 39.00 | 270 |
| 2004 | MATT PROD ENTERPRISES | 0.00 | 33.00 | 275 |
| 2005 | MATT PROD ENTERPRISES | 0.00 | 45.00 | 275 |
| 2006 | MATT PROD ENTERPRISES | 0.00 | 28.00 | 365 |
| 2007 | MATT PROD ENTERPRISES | 0.00 | 26.00 | 365 |
| 2008 | MATT PROD ENTERPRISES | 0.00 | 37.00 | 365 |
| 2009 | MATT PROD ENTERPRISES | 0.00 | 73.00 | 365 |
| 2011 | MATT PROD ENTERPRISES | 0.00 | 64.00 | 365 |
| 2012 | MATT PROD ENTERPRISES | 0.00 | 43.00 | 180 |
| 2013 | MATT PROD ENTERPRISES | 0.00 | 18.00 | 180 |
| 2014 | MATT PROD ENTERPRISES | 0.00 | 24.00 | 60 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 1993 | MATT PROD ENTERPRISES | Brine | 0 | 180 |
| 1994 | MATT PROD ENTERPRISES | Brine | 0 | 180 |
| 1995 | MATT PROD ENTERPRISES | Brine | 0 | 180 |
| 1996 | MATT PROD ENTERPRISES | Brine | 0 | 240 |
| 1997 | MATT PROD ENTERPRISES | Brine | 0 | 210 |
| 1998 | MATT PROD ENTERPRISES | Brine | 0 | 210 |
| 1999 | MATT PROD ENTERPRISES | Brine | 0 | 275 |
| 2000 | MATT PROD ENTERPRISES | Brine | 0 | 240 |
| 2001 | MATT PROD ENTERPRISES | Brine | 0 | 280 |
| 2002 | MATT PROD ENTERPRISES | Brine | 0 | 270 |
| 2003 | MATT PROD ENTERPRISES | Brine | 0 | 270 |
| 2004 | MATT PROD ENTERPRISES | Brine | 0 | 275 |
| 2005 | MATT PROD ENTERPRISES | Brine | 0 | 275 |
| 2006 | MATT PROD ENTERPRISES | Brine | 0 | 365 |
| 2007 | MATT PROD ENTERPRISES | Brine | 0 | 365 |
| 2008 | MATT PROD ENTERPRISES | Brine | 0 | 365 |
| 2009 | MATT PROD ENTERPRISES | Brine | 0 | 365 |
| 2011 | MATT PROD ENTERPRISES | Brine | 0 | 365 |
| 2012 | MATT PROD ENTERPRISES | Brine | 0 | 180 |
| 2013 | MATT PROD ENTERPRISES | Brine | 0 | 180 |
| 2014 | MATT PROD ENTERPRISES | Brine | 33 | 60 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1243031964 | 2013-3-28 0:00: | PW | No Violations | 0.30 |
| -1311301339 | 2014-10-8 0:00: | PW | No Violations | 10.00 |
| -15850695 | 2013-1-25 0:00: | PW | No Violations | 2.20 |
| -298459173 | 2014-10-10 0:00 | PW | No Violations | 4.50 |
| -31434016 | 2014-9-24 0:00: | PB | No Violations | 2.40 |
| -620460370 | 2014-10-3 0:00: | PB | No Violations | 0.70 |
| -808934057 | 2014-9-23 0:00: | PB | No Violations | 5.50 |
| -94279930 | 2013-1-25 0:00: | PW | No Violations | 2.20 |
| 0015850695 | 2013-01-25 | Production Wells | Violations Noted | The production tank was set less than 20 from the well head. The tank battery consisted of one 50 Barrel (Bbl) steel tank, one 2100 gallon (gal) plastic tank, and one water knock out. There was no dike around the tanks. The 2100 gal plastic tank had over flown with oil and brine and had contaminated an area around the tank battery roughly 30 x 12. The flow had moved into a field drain and moved through the field, and under the road through a culvert roughly 500 feet. There was no evidence of contamination reaching Sunday Creek. The company had already begun clean up but had not removed all the contaminants. All contaminated soils along the field drain and around the tanks shall be removed and disposed of properly. The affected area shall have soils replaced. The affected area shall be reseeded, mulched, and steps shall be taken to encourage vegetative growth. Any remaining contaminants shall be removed from the field drain. |
| 0031434016 | 2014-09-24 | Plug / Plug Back | No Violations | The 5 3/16 casing had parted at the collar last night, so the casing was set back down and screwed back on. The remainder of the bottom hole plug was placed through the casing and the casing was ripped at 277 feet and pulled using a packer. Clay is being washed down the 6 casing now. |
| 0094279930 | 2013-01-25 | Production Wells | Violations Noted | The production tank was set less than 20 from the well head. The tank battery consisted of one 50 Barrel (Bbl) steel tank, one 2100 gallon (gal) plastic tank, and one water knock out. There was no dike around the tanks. The 2100 gal plastic tank had over flown with oil and brine and had contaminated an area around the tank battery roughly 30 x 12. The flow had moved into a field drain and moved through the field, and under the road through a culvert roughly 500 feet. There was no evidence of contamination reaching Sunday Creek. The company had begun clean up operations but had not yet finished removing all the contaminants. Production tanks shall be set at least 50 from any well and inside a dike. The dike shall be constructed with a capacity of at least 110% of the largest tank for the purpose of containing contaminants. I spoke with the owner in the field and we discussed the violation. |
| 0298459173 | 2014-10-10 | Production Wells | No Violations | MH Well Service is removing contamined soil. I have requested they excavate to determine the extent of the contamination. |
| 0387986256 | 2013-02-08 | Production Wells | No Violations | Follow up to -15850695. Most of the contaminated soils and vegetation from along the field drain had been bagged up but not removed from the site yet. |
| 0465129066 | 2014-09-25 | Plug / Plug Back | No Violations | Washing in Clay. |
| 0491858626 | 2013-02-25 | Production Wells | No Violations | Follow up to -15850695. The oil contaminants as well as the contaminated soils and vegetation have been removed from the field drain. The area under the old tank still needs to have the soils removed. I spoke with Mr. Kelly in the field and we reviewed the clean up requirements. |
| 0585196434 | 2013-03-13 | Production Wells | No Violations | Follow up to -15850695. There were still contaminated soils around the area of the tank and the field drain. I field tested the water running off the soil and it was found to have a 5664 ppm Chloride content. I spoke with the producer and the soils will be removed immediately and the smaller ditch will be filled in order to prevent further contamination. |
| 0620460370 | 2014-10-03 | Plug / Plug Back | No Violations | The area was graded off with no visible casing at the surface. |
| 0808934057 | 2014-09-23 | Plug / Plug Back | No Violations | Witnessed roughly 250 feet of clay placed in the bottom of the hole. 5 3/16 casing was parted around 60 feet while trying to pull it from the hole. |
| 0911678336 | 2014-10-13 | Administrative Inspection | No Violations | I received a call from MH Well Service concerning the clean-up of crude oil. The oil had pooled at the base of the sandstone rock face. The excavation was 6 deep. MH Well Service removed this material and continued to follow the stained soil until it was completely removed. The area has been seeded and mulched. |
| 1243031964 | 2013-03-28 | Production Wells | No Violations | Follow up to -15850695. There were still contaminated soils around the area of the tank and the field drain. I met with the producers and the drainage ditch was shoveled out and a small impoundment was made. Lime will be applied to the scalded area. The area below the dike on the hill will have the contaminated soil removed with in 2 weeks. |
| 1311301339 | 2014-10-08 | Production Wells | No Violations | MH Well Service on site, they have removed the soil and rock that was contaminated on the side of the hill. The soil is being removed at the base of the hill and will continue until all the oil contaminated soil has been removed. |
| 1359643033 | 2013-01-31 | Production Wells | No Violations | Follow up to -15850695. No clean up efforts have been made as of yet. |
| 1360873077 | 2013-02-14 | Production Wells | No Violations | Follow up to -15850695. The bags of contaminants have been removed. There is still oily materials and sheen in the field drain. I attempted to contact the owner of the well to go over steps to bring the well into compliance. |
| 1364310158 | 2013-03-26 | Production Wells | No Violations | Follow up to -15850695. No more clean up along the field drain and around the contaminated tank area since last inspection. There has been no more clean up in the area below the tanks on the hill. The pumping unit has been removed from the well. There is no sign of contamination reaching Sunday Creek. |
| 1392150026 | 2014-02-11 | Administrative Inspection | No Violations | Extension granted verbally by Supervisor. |
| 1411479150 | 2014-09-22 | Plug / Plug Back | No Violations | Not currently working. |
| 1585650626 | 2013-02-20 | Production Wells | No Violations | Follow up to -15850695. Upon inspection I noticed not as much of the contaminated soils around the tank that leaked had been removed as I originally thought. There is still a small amount of oily vegetation along the banks of the field drain. There is still a small amount of mouse and sheen in the water in the field drain and it has now moved further along towards Sunday Creek. I was able to follow the sheen and mouse through the drain to Sunday Creek. There is no evidence of any recoverable amounts ever reaching Sunday Creek or any sheen along the banks of the creek but a small sheen was seen in the drain that empties directly into the creek. I spoke with Bruce Kelley and he will have someone out here as soon as possible to clean the sheen and mouse from the creek. Monday morning he and I will be meeting to discuss and begin remediation of the site. |
| 1918087136 | 2015-08-18 | Final Restoration | No Violations | On my inspection I found that the location had been restored according to 1509.072. I passed the final restoration at this time. |
| 1972372209 | 2013-03-28 | Production Wells | No Violations | GPS of well taken to verify location. No violations. Past violations with this well may need to be moved to API # 1082. Will verify locations with geologists in Columbus. |
| 2112217140 | 2014-10-07 | Production Wells | No Violations | MH Well Service on site working on removing soil and rock that is contaminated with crude oil. Heavy rain at 12:30 PM. Work finished for today. |
| 387986256 | 2013-2-8 0:00:0 | PW | No Violations | 0.50 |
| 465129066 | 2014-9-25 0:00: | PB | No Violations | 2.00 |
| 491858626 | 2013-2-25 0:00: | PW | No Violations | |
| 585196434 | 2013-3-13 0:00: | PW | No Violations | 1.50 |
| 911678336 | 2014-10-13 0:00 | AM | No Violations | 1.00 |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0015850695 | US-OH-115504 | 2015-01-12 | Well operation causing pollution and contamination | |
| 0094279930 | US-OH-130778 | 2015-01-12 | Violation of tank spacing requirements | |
| 0094279930 | US-OH-130779 | 2015-01-12 | No SPCC dike/or failure to keep dike free of water or oil |
For data sources see[8]